• Title/Summary/Keyword: 날개 길이 각

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Development for Fishing Gear and Method of the Non-Float Midwater Pair Trawl Net (II) - Opening Efficiency of the Model Net according to Front Weight and Wing-end Weight - (무부자 쌍끌이 중층망 어구어법의 개발 (II) - 추와 날개끝 추의 무게에 따른 모형어구의 전개성능 -)

  • 유제범;이주희;이춘우;권병국;김정문
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.39 no.3
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    • pp.189-196
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    • 2003
  • In this study, the vertical opening of the non-float midwater pair trawl net was maintained by controlling the length of upper warp. This was because the head rope was able to be kept linearly and the working depth was not nearly as changed with the variation of flow speed as former experiments in this series of studies have demonstrated. We confirmed that the opening efficiency of the non-float midwater pair trawl net was able to be developed according to the increase in front weight and wing-end weight. In this study, we described the opening efficiency of the non-float midwater pair trawl net according to the variation of front weight and wing-end weight obtained by model experiment in circulation water channel. We compared the opening efficiency of the proto type with that of the non-float type. The results obtained can be summarized as follows:1. The hydrodynamic resistance was almost increased linearly in proportion to the flow speed and was increased in accordance with the increase in front weight and wing-end weight. The increasing rate of hydrodynamic resistance was displayed as an increasing tendency in accordance with the increase in flow speed. 2. The net height of the non-float type was almost decreased linearly in accordance with the increase in flow speed. As the reduced rate of the net height of the non-float type was smaller than that of the net height of the proto type against increase of flow speed, the net height of the non-float type was bigger than that of the proto type over 4.0 knot. The net width of the non-float type was about 10 m bigger than that of the proto type and the change rate of net width varied by no more than 2 m according to the variation of the front weight and wing-end weight. 3. The mouth area of the non-float type was maximized at 1.75 ton of the front weight and 1.11 ton of the wing-end weight, and was smaller than that of the proto type at 2.0∼3.0 knot, but was bigger than that of the proto type at 4.0∼5.0 knot. 4. The filtering volume was maximized at 3.0 knot in the proto type and at 4.0 knot in the non-float type. The optimal front weight was 1.40 ton.

Optimization of ejector for swirl flow using CFD (CFD를 이용한 회전 운동을 하는 이젝터의 최적화)

  • Kang, Sang-Hoon;Park, Young-Chul
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.18 no.2
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    • pp.31-37
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    • 2017
  • This paper investigates the effect of the rotational motion of a driving fluid generated by a rotational motion device at the inlet of a driving nozzle for a gas-liquid ejector, which is the main device used for ozonated ship ballast water treatment. An experimental apparatus was constructed to study the pressure and suction flow rate of each port of the ejector according to the back pressure. Experimental data were acquired for the ejector without rotational motion. Based on the data, a finite element model was then developed. The rotational motion of the driving fluid could improve the suction efficiency of the ejector based on the CFD model. Based on the CFD results, structure optimization was performed for the internal shape of the rotation induction device to increase the suction flow rate of the ejector, which was performed using the kriging technique and a metamodel. The optimized rotation induction device improved the ejector efficiency by about 3% compared to an ejector without rotational motion of the driving fluid.

Development of KD- Propeller Series using a New Blade Section (새로운 날개단면을 이용한 KD-프로펠러 씨리즈 개발)

  • J.T. Lee;M.C. Kim;J.W. Ahn;H.C. Kim
    • Journal of the Society of Naval Architects of Korea
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    • v.28 no.2
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    • pp.52-68
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    • 1991
  • A new propeller series is developed using the newly developed blade section(KH18 section) which behaves better cavitation characteristics and higher lift-drag ratio at wide range of angle-of-attack. The pitch and camber distributions are disigned in order to have the same radial and chordwise loading distribution with the selected circumferentially averaged wake input. Since the geometries of the series propeller, such as chord length, thickness, skew and rate distribations, are selected by regression of the recent full scale propeller geometric data, the performance prediction of a propeller at preliminary design stage can be mure realistic. Number of blades of the series propellers is 4 and the expanded blade area ratios are 0.3, 0.45, 0.6 and 0.75. Mean pitch ratios are selected as 0.5, 0.65, 0.8, 0.75 and 1.1 for each expanded area ratio. The new propeller series is composed of 20 propellers and is named as KD(KRISO-DAEWOO) propeller series. Propeller open water tests are performed at the experimental towing tank, and the cavitation observation tests and fluctuating pressure measurements are carried out at the cavitation tunnel of KRISO. $B_{P}-\delta$ curves, which can be used to select the optimum propeller diameter at the preliminary design stage, are derived from a regression analysis of the propeller often water test results. The KD-cavitation chart is derived from the cavitation observation test results by choosing the local maximum lift coefficient and the local cavitation number as parameters. The caviy extent of a propeller can be predicted more accurately by using the KD-cavitation chart at a preliminary design stage, since it is derived from the results of the cavitation observation tests in the selected ship's wake, whereas the existing cavitation charts, such as the Burrill's cavitation chart, are derived from the test results in uniform flow.

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Parametric Numerical Study on the Performance of Helical Tidal Stream Turbines (헬리컬 터빈의 설계인자에 따른 성능 연구)

  • Han, Jun-Sun;Choi, Da-Hye;Hyun, Beom-Soo;Kim, Moon-Chan;Rhee, Shin-Hyung;Song, Mu-Seok
    • Journal of the Korean Society for Marine Environment & Energy
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    • v.14 no.2
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    • pp.114-120
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    • 2011
  • The characteristics of a helical turbine to be used for tidal stream energy conversion have been numerically studied with varying a few design parameters. The helical turbines were proposed aiming at mitgating the well known poor cut-in characteristics and the structural vibration caused by the fluctuating torque, and the basic concept is introducing some twisting angle of the vertical blade along the rotation axis of the turbine. Among many potential controling parameters, we focused, in this paper, on the twisting angle and the height to diameter ratio of the turbine, and, based on the numerical experiment, We tried to propose a configuration of such turbine for which better performance can be expected. The three-dimensional unsteady RANS equations were solved by using the commercial CFD software, FLUENT with k-${\omega}$ SST turbulence model, and the grid was generated by GAMBIT. It is shown that there are a range of the twisting angle producing better efficiency with less vibration and the minimum height to diameter ratio above which the efficiency does not improve considerably.

Analysis on the Planar Bowtie Antenna for IMT-2000 Handset (IMT-2000 핸드셋용 평면형 Bowtie 안테나 해석)

  • Lee, Hee-Suk;Kim, Nam
    • The Journal of Korean Institute of Electromagnetic Engineering and Science
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    • v.11 no.5
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    • pp.681-688
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    • 2000
  • In this paper, a planar antenna that is small and light, is designed and analyzed aiming handset antenna of IMT-2000. Employing the Ensemble simulator based on a MoM, design-parameters are found to determine a resonant frequency. Therefore, it is analyzed with the Ensemble simulation and FDTD numerical for resonating at the allocated frequency for IMT-2000 in the fixed antenna dimension of 21$^{\circ}$wing angle that is a design parameter. Analyzing with FDTD method, Though the results of FDTD are very exact, this analysis introduces errors due to the staircasing approximation in the slope of bowtie. To reduce this error, it is divided to 4-ranges where the cell contains the boundary of perfect conductor/free space. Then, each range is calculated by different by different equation, which modify the H-field to add the component of the area and length of the cell filled with free space. Therefore, the modified FDTD algorithm provided with a narrow bandwidth of return loss calculated with a standard FDTD algorithm that can be extended to the desired ranges.

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Ecological Studies on the Inhavitation of Artificial Nests by Wild Birds -Especially in Gyeongnam Province- (인공소상가설(人工巢箱架設)에 의(依)한 야생조류(野生鳥類)의 서식생태(棲息生態)에 관(關)한 연구(硏究) -경남지역(慶南地域)을 중심(中心)으로-)

  • Choi, Jai-Sik;Kim, Jai-Saing
    • Journal of Korean Society of Forest Science
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    • v.76 no.2
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    • pp.109-118
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    • 1987
  • The purpose of this study was to investigate the inhabiting ecology of wild birds using artificial nests in Gyeongnam province. The sort of birds, the utilization of artificial nests by the materials, by the sites and by the forest type, and other inhabiting ecology of birds were investigated from 1984 to 1986. The results obtained were as follows; 1. Wild birds in surveyed areas were classified into 20 families and 35 species. Among them the birds inhabiting the artificial nests were 6 species and those using them most frequently were Parus ater (17.2%), P. major (16.7%) and P. palustris (12.2%). 2. The artificial nests installed on the top and at the toot of the mountain were chiefly utilized by P. ater and P. major, but the artificial nests in park area were mostly used by Passer montanus and Sturnus cineraceus. 3. Sixty-one percent of the artificial nests were utilized by the birds; 45.5% were used for breeding and 15.6% were inhabitation only. 4. When different nest materials and shapes were tested, mixed nests (sawdust and cement) were used most frequently, and C type. (Diamond shape) of wood nests was used more frequently compared with the A (Roof shape) and B (Box shape) types of wood nests. Meanwhile, the birds prefered the 3cm hole size (81.1% of utilization) to 4cm of hole (57.8%) and 5cm of hole (24.4%). 5. The artificial nests constructed in mixed forest were more frequently inhabited (73.3%) by the birds than coniferous forest (68.3%) and broad-leaved forest (63.3%). 6. The period of egg-laying in Parus species was from late April to early May, while Eophona migratoria, Lanius bucephalus, Motacilla alba and Passer montanus laid eggs generally in the middle of May. 7. Parus species, Passer montanus and Motacilla alba laid one egg every day for 5-10days, but Eopphona migratoria laied 4 eggs in 7 days and Lanius bucephalus laid 5 eggs in 4 days. The incubation period of Parus species was 16-18 days, while the others were about 11 to 14 days. 8. Thirteen days after the hatch of Parus major, chicks reached 13.9g of body weight, 72.0mm of wing-length and 20.9mm of tarsus length. P. montanus chicks reached 20.3g of weight, 66.2mm of wing-length and 20.2mm of tarsus length during the same period. 9. Food item of feeding chicks almost consisted of creatures (98.2%) with following composition; 55.2% of insect larvae, 37.2% adult insects, 2.8% of pupae and 2.8% of spiders. Vegetable items were 2% only. Among those creature food items, 95.2% were insect pests to forest.

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Development for Fishing Gear and Method of the Non-Float Midwater Pair Trawl Net (III) - Opening Efficiency of the Model Net attaching the Kite - (무부자 쌍끌이 중층망 어구어법의 개발 (III) - 카이트를 부착한 모형어구의 전개성능 -)

  • 유제범;이주희;이춘우;권병국;김정문
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.39 no.3
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    • pp.197-210
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    • 2003
  • The non-float midwater pair trawl was effective in the mouth opening and control of the working depth in midwater and bottom. In contrast, we confirmed that it was difficult to keep the net at surface above 30 m of the depth by means of the full scale experiment in the field and the model test in the circulation water channel. To solve this problem, the kites were attached to the head rope of the non-float midwater pair trawl. In this study, four kinds of the model experiments were carried out with the purpose of applying the kite to the korean midwater pair trawl. The results obtained can be summarized as follows: 1. The working depth of the non-float midwater pair trawl with the kite was shallower than that of the proto type and non-float type. The working depth of the kite type was approximately 20m with 2 kites and about 5m with 4 kites under 4.0 knot. The working depth was almost constant but the depth of the head rope sank approximately 15m and 10m according to the increase in the front weight and the wing-end weight, respectively. The changing aspect of the working depth was constant, but the depth of the head rope sank approximately 22m according to the increase in the lower warp length (dL). 2. The hydrodynamic resistance of the kite type was almost increased in a linear form in accordance with the flow speed increase from 2.0 to 5.0 knot. The increasing grate of the hydrodynamic resistance tended to increase in accordance with the increase in flow speed. The hydrodynamic resistance of the kite type was larger approximately 5~10 ton larger than that of the non-float type and the proto type. The hydrodynamic resistance of the kite type increased approximately 3ton with the changing of the front weight from 1.40 to 3.50 ton and approximately 4 ton with the changing of the wing-end weight from 0 to 1.11 ton and approximately 5.5 ton with the changing lower warp length (dL) from 0 to 40 m, respectively. 3. The net height of the kite type was increased approximately 10 m with the change in the kite area from $2,270mm^2$ to 4,540 $\textrm{mm}^2$. The net height of the kite type was aproximately 50 m and 30 m larger than that of the proto type and the non-float type, respectively. The changed aspect of the net width was approximately 5m with the variation of the flow speed from 2.0 to 5.0 knot. 4. The filtering volume of the kite type was larger than that of the proto type and the non-float type by 28%, 34% at 2.0 knot of the flow speed and 42%, 41% at 3.0 knot, and 62%, 45% at 4.0 knot, and 74%, 54% at 5.0knot, respectively. The optimal towing speed was approximately 3.0 knot for the proto type and was over 4.0 knot for the non-float type, and the optimal towing speed reached 5.0 knot for the kite type. 5. The opening efficiency of the kite type was approximately 50% and 25% larger than that of the proto type and the non-float type, respectively.

A Gear Shape of a Midwater Trawl and Its Change (중층트롤의 어구형상과 그 변화)

  • Park, Hae-Hoon;Yoon, Gab-Dong
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.38 no.3
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    • pp.209-216
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    • 2002
  • How to estimate the shape of trawl net and ropes of a midwater trawl on full scale was described by implementing a three-dimensional semi-analytic treatment of a towing cable system with the field experiments obtained with the Scanmar system. The shape of trawl net from wingend to the beginning of codend was assumed to be of form $\chi$$^2$/ae$^2$+ y$^2$/be$^2$=(z - c)$^2$/c$^2$, and that of the ropes attached behind otter boards be of form yr = $A\chi$rB. In case of warp length 300m long, the volume of trawl net, the ratio of net height to net width at the mouth of the trawl net, and the inclination angle of float rope were estimated according to the change of towing speed. The volume and the distance between wingtips were increased with increasing towing speed. And the inclination angle of float (or ground) rope was slightly decreased with increasing towing speed.

Experimental Study on Pressure Loss of Flow Parallel to Rod Bundle with Spacer Grid (지지격자가 있는 봉다발과 축방향으로 평행한 유동의 압력손실에 관한 실험적 연구)

  • Lee, Chi-Young;Shin, Chang-Hwan;Park, Ju-Yong;In, Wang-Kee
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.36 no.7
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    • pp.689-695
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    • 2012
  • The friction factor in a rod bundle and the loss coefficient at a spacer grid were examined. As a test section, 25 smooth rods, 9.5 mm in diameter and 2000 mm in length, were prepared and installed in a $5{\times}5$ square array in a square channel. In this case, the P/D (Pitch-to-Diameter ratio) was 1.35. In this work, plain (i.e., no mixing vanes), split-vane, and hybrid-vane spacer grids were tested. In a bare rod bundle (i.e., no spacer grid), the measured friction factors were in good agreement with the previous correlations. Among the spacer grids tested, the hybrid-vane spacer grid presented the largest friction factor in the rod bundle and loss coefficient. This may be because of the flow pattern change induced by large relative plugging of the flow cross section and mixing vane geometry. At Re=$5{\times}10^5$, the predicted loss coefficients of plain, splitvane, and hybrid-vane spacer grids were approximately 0.79, 0.80, and 0.88, respectively.

Analysis of Temperature and Humidity Distributions according to Arrangements of Air Circulation Fans in Single-span Tomato Greenhouse (토마토 단동온실에서 공기순환팬 설치 방법에 의한 온실 내 온습도 분포 분석)

  • Lee, Tae Seok;Kang, Geum Choon;Paek, Yee;Moon, Jong Pil;Oh, Sung Sik;Kwon, Jin Kyung
    • Journal of Bio-Environment Control
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    • v.25 no.4
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    • pp.277-282
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    • 2016
  • This study was aimed to investigate the effect of air-circulation fans on air temperature and relative humidity in a single-span tomato greenhouse (W: 7m, L: 25m, H: 3.2m). According to standard of fan layout by ASAE (1997), a total of 10 fans were bilaterally arranged in 2 rows in the experimental greenhouse. The distributions of air temperature and relative humidity were measured from 6 pm to 8 am under different conditions, with and without fans. The measurement heights were 0.7m, 1.7m and 2.7m. Under the condition of "fans off", the spatial differences of air temperature and relative humidity between upper and lower sides were $1.7^{\circ}C$ and 10.8%, respectively. The operation of 10 fans showed their differences to $0.1^{\circ}C$ and 3.2%. The number of fans and installation direction were evaluated their performance on reducing the spatial variation of air temperature and relative humidity. The experimental layouts were 5 and fans in 2 rows (bilaterally) and 10 fans in the one (same) direction. Under the condition of "6 fans on" and "5 fans on", the spatial differences of air temperature and relative humidity between upper and lower side were $0.3^{\circ}C$, 3.4% and $0.3^{\circ}C$ and 4.0%. The operation of 10 fans in the one direction reduced their differences to $0.5^{\circ}C$ and 4.9%. The overall findings of this study showed that there was no significant differences under each condition. Therefore, this study suggested that it is more economic and effective to install five fans in 2 rows (bilaterally) in the greenhouse (W: 7m, L: 25m, H: 3.2m).