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Case Study on the Tunnel Collapse at the Shallow Depth  

Baek Ki-Hyun ((주)대우건설)
Roh Jong-Ryun ((주)대우건설)
Kim Yong-Il ((주)대우건설)
Cho Sang-Kook ((주)대우건설)
Hwang Nag-Youn ((주)대우건설)
Publication Information
Tunnel and Underground Space / v.15, no.2, 2005 , pp. 102-110 More about this Journal
Abstract
○ ○ tunnel that is located at Iksan - Jangsu freeway ○ ○, has collapsed during construction at the valley with shallow depth. Although, the site investigations, such as TSP, drilling exploration and so of indicated the presence of discontinuities in this section. The RMR was upgraded and the construction were carried out because that not only actual rock qualities were relatively good during construction but also the tunnel foe was stabilized. However, the tunnel was collapsed at the same time blasting of full face, and surface and underground water was infiltrated due to the settlement of the upper part of the tunnel face. To restore the collapsed section, 3-d tunnel stability analysis was performed and suitable reinforcement methods were chosen. The cavity of the upper tunnel face was stabilized by means of UAM and ALC injection. And the settlement was restored using L.W grouting method.
Keywords
Shallow depth; Tunnel collapse; TSP; Reinforcement;
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