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http://dx.doi.org/10.18770/KEPCO.2016.02.03.421

Analysis of Insulation Diagnosis and Failure in Stator Windings of Air-Cooled Gas Turbine Generator  

Kim, Hee-Dong (KEPCO Research Institute, Korea Electric Power Corporation)
Kong, Tae-Sik (KEPCO Research Institute, Korea Electric Power Corporation)
Kim, Kyeong-Yeol (KEPCO Research Institute, Korea Electric Power Corporation)
Publication Information
KEPCO Journal on Electric Power and Energy / v.2, no.3, 2016 , pp. 421-424 More about this Journal
Abstract
In order to evaluate the insulation deterioration in the stator windings of air-cooled gas turbine generators(119.2 MVA, 13.8 kV) which has been operating for more than 15 years, diagnostic test and AC dielectric breakdown test were performed on phases A, B and C. Diagnostic test included measurements of AC current, dissipation factor, partial discharge (PD) magnitude and capacitance. ${\Delta}I$ and ${\Delta}tan{\delta}$ in all three phases (A, B, and C) of generator stator windings showed that they were in good condition but PD magnitude indicated marginally serviceable condition. After the diagnostic test, an AC overvoltage test was performed by gradually increasing the voltage applied to the generator stator windings until electrical insulation failure occurred, in order to determine the breakdown voltage. Although phase A of generator stator windings failed at breakdown voltage of 29.0 kV, phases B and C endured the 29.0 kV. The breakdown voltage in all three phases was higher than that expected for good-quality windings (28.6 kV) in a 13.8 kV class generator.
Keywords
Insulation deterioration; stator windings; Fault Detect and Diagnosis (FDD); air-cooled gas turbine generator; PD;
Citations & Related Records
Times Cited By KSCI : 3  (Citation Analysis)
연도 인용수 순위
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