Browse > Article

An Experimental Study on the Stirrup Effectiveness in Reinforced Concrete Beams  

Lee, Young-Jae (국립 상주대학교 이공학부 토목공학과)
Lee, Yoon-Young (국립 상주대학교 이공학부 토목공학과)
Publication Information
Journal of the Korea institute for structural maintenance and inspection / v.9, no.1, 2005 , pp. 205-215 More about this Journal
Abstract
The main objective of this study is to investigate the behavior of NSC and HSC beams with stirrups. Main variables were the concrete compressive strength and amount of vertical stirrups. A total of 24 beams was tested; 4 beams without web reinforcement and 20 beams with web reinforcement in the form of vertical stirrups. Main variables were 2 different compressive strengths of concrete of 26.9MPa and 63.5MPa, 5 different spacing of stirrups of 200, 150, 120, 100 and 90mm. Therefore, the results were compared with the strengths predicted by the equations of ACI code 318-99 and other researchers. The shear reinforcement ratio, where the test beams were failed simultaneously under flexure and shear, were $0.63{\rho}_{vmax}$ for NSC beams and $0.53{\rho}_{vmax}$ for HSC beams, respectively. The ACI code equation was found to be very conservative for shear design.
Keywords
Shear behavior; stirrup effectiveness; NSC(normal strength concrete) beams; HSC(high strength concrete) beams;
Citations & Related Records
연도 인용수 순위
  • Reference