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Burst Behavior for Mechanically Machined Axial Flaws of Steam Generator Tubings  

Hwang, Seong Sik (Korea Atomic Energy Research Institute)
Kim, Hong Pyo (Korea Atomic Energy Research Institute)
Kim, Joung Soo (Korea Atomic Energy Research Institute)
Publication Information
Corrosion Science and Technology / v.3, no.1, 2004 , pp. 30-33 More about this Journal
Abstract
It has been reported that some events of a rupture of seam generator tube have occurred in nuclear power plants around the world. Main causes of the leakage are from various types of corrosion in the steam generator(SG) tubings. Primary water stress corrosion cracking(PWSCC) of steam generator tubings have occurred in many tubes in Korean plant, and they were repaired using sleeves or plugs, In order to develop proper repair criteria, it is necessary to ascertain the leak behavior of the tubings. A high pressure leak and burst testing system was manufactured. Various types of Electro Discharged Machined (EDM) notches were developed on the SG tubes. Leak rate and burst pressure were measured on the tubes at room temperature. Burst pressure of the part through wall defected tubes depends on the defect depth, Water flow rates after the burst were independent of the t1aw types; tubes having 20 to 60 mm long EDM notches showed similar flow rates regardless of the defect depth. A fast pressurization rate gave the tube a lower burst pressure than the case of a slow pressurization.
Keywords
SG tubes; stress corrosion cracking; leak test; burst test; burst pressure;
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