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http://dx.doi.org/10.6108/KSPE.2020.24.2.028

The Relationship between Grain Design and Non-uniform Ablation of Solid Rocket Insulation  

Kim, Jeongjin (The 4th R&D Institute, Agency for Defense Development)
Lee, Jungseob (The 4th R&D Institute, Agency for Defense Development)
Jin, Jungkun (The 4th R&D Institute, Agency for Defense Development)
Lee, Dohyung (The 4th R&D Institute, Agency for Defense Development)
Publication Information
Journal of the Korean Society of Propulsion Engineers / v.24, no.2, 2020 , pp. 28-34 More about this Journal
Abstract
In order to relieve the burden of the rear ablative material, the combustion test of the solid rocket motor with the forward deployed multi-pin grain design was successfully performed twice. However, after disassembling the solid rocket motor, a non-uniform ablation pattern was found in the rear ablative material. Periodic repetition of local and regional ablation was measured precisely. Two-dimensional flow and eddy flow, created by the uneven main-pin flow hitting the rear ablative material, were identified as the cause of non-uniform ablation. In addition. when the rear pins were removed, the possibility of securing the soundness of the rear ablative material was confirmed as the average flow velocity and the standard deviation were lowered.
Keywords
Solid Rocket Motor; Non-uniform Ablation; Grain Design;
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