한국지반공학회:학술대회논문집 (Proceedings of the Korean Geotechical Society Conference)
- 한국지반공학회 2006년도 춘계 학술발표회 논문집
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- Pages.208-218
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- 2006
OO 사찰 하부 터널통과 설계 사례
A Case Study on the Design of Railway Tunnel through section for under OO temple
- Kim, Shin (Teso Engineering Co.) ;
- Lee, Sung-Ki (Teso Engineering Co.) ;
- Seo, Hyoung-Chul (Teso Engineering Co.) ;
- Kwag, Jung-Yeol (Teso Engineering Co.) ;
- Cho, Bong-Sik (SK Engineering & Construction Co. Ltd.)
- 발행 : 2006.03.24
초록
It is very important to evaluate predictable problems diversely such as stability of a tunnel and structures when tunnel is inevitably constructed in the area where is adjacent to a structure and low overburden. Double electrified railway design on the third section of Donghae-Nambu line studied in this paper has some problems mentioned above. So more careful works are required before construction. In this study, ground surrounding is composed of faults, fault zone and set back about 13m from a Buddhist temple located on the upper part of the tunnel. From these conditions, this case study presents proper methods considering ground condition, effects of blasting and civil petitions. It is tried to make the tunnel and Buddhist temple stable by analytical technique and analysis of existing cases. And design considering stability of tunnel and adjacent structure during operation is carried out as well. Especially, environmentally friendly railway tunnel which is appropriate to the local condition and surroundings is designed by minimizing noise and vibration that is able to occur during construction and train service. From now on, this study is helpful to better design in the case of tunnel design which has to consider civil petition.
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