• Title/Summary/Keyword: z-axis vibration

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Analysis Study on Vibration Durability on Lens Manufacturing System of Camera (카메라의 렌즈 생산 시스템에 대한 진동 내구성에 관한 해석 연구)

  • Cho, Jae-Ung;Kim, Young-Choon;Joung, Woon-Se
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.15 no.5
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    • pp.2617-2622
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    • 2014
  • In this study, the critical frequency happened at system is analyzed when the motor of camera manufacturing system is working on the direction of Z axis. Configurations of modes at natural frequencies happened at two models are investigated by the study result through modal analysis. The range of natural frequency in this study system is from 100 Hz to 500 Hz. At this range, the maximum equivalent stress in case of 20 kg weight becomes 6.2335MPa and this stress is shown as 50 times more than in case of 10 kg weight. The working safety of system can be investigated through the analyses of natural frequency and harmonic response of this camera manufacturing system.

Effect of Flywheel Weight on the Vibration of Diesel Engine (플라이휠 중량(重量)이 디젤 기관(機關)의 진동(振動)에 미치는 영향(影響))

  • Myung, Byung Soo;Kim, Sung Rai
    • Korean Journal of Agricultural Science
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    • v.20 no.2
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    • pp.167-180
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    • 1993
  • Most of small size diesel engines are widely used with the same size and weight flywheel in the levels of 6.0kW and 7.5kW. This study was conducted to obtain basic data which affect the engine performance of the power tiller. The flywheel weight was considered as a major factor in this research. Basically, fuel consumption ratio, motoring loss, torque, vibration and mechanical efficiency of the engine were measured and analyzed on four levels of flywheel weight, 32.2, 29.4, 26.2 and $24.2kg_f$, respectively. Results were obtained as follows: 1. The weights of flywheel were $23.7kg_f$ from design program of JSME and $24.5kg_f$ from ASME and SAE design criteria. Therefore, the flywheel weight of $32.2kg_f$ might be reduced about $8kg_f$ in 7.5kW engine. 2. The rated outputs of 6.0kW and 7.5kW engine were actually 7.43kW and 7.85kW, respectively. When flywheel weight was reduced from $32.2kg_f$ to $24.2kg_f$, outputs were increased from 7.43kW to 7.70kW in 6.0kW engine and from 7.85kW to 8.25kW in 7.5kW engine. 3. When the flywheel weight was reduced from $32.2kg_f$ to $24.2kg_f$, fuel consumption ratio was decreased from 300.8 to 296.8g/kW-hr in 6.0kW engine and also from 313.6 to 312.8g/kW-hr in 7.5 kW engine, respectively. 4. When the flywheel weight was reduced from $32.2kg_f$ to $24.2kg_f$, mechanical efficiency of engine was increased from 76.1% to 76.8% in 6.0kW engine and also from 76.7% to 77.0% in 7.5kW engine, respectively. 5. When the flywheel weight was reduced from $32.2kg_f$ to $24.2kg_f$, vibration was decreased at X-axis and Z-axis in 6.0kW engine, however, slightly increased at Y-axis in 6.0kW engine and at all axes in 7.5kW engine. 6. When the flywheel weight was reduced from $32.2kg_f$ to $24.4kg_f$ motoring loss was decreased from 2.33kW to 1.75kW in 6.0kW engine and also from 2.46kW to 1.84kW in 7.5kW engine.

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Effect of Flywheel Weight on Engine Performance for the Small Diesel Engine (Flywheel의 중량(重量)이 소형(小型) 디젤기관(機關)의 성능(性能)에 미치는 영향(影響))

  • Jung, Hae Kook;Kim, Sung Rai;Myung, Byung Soo
    • Korean Journal of Agricultural Science
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    • v.15 no.2
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    • pp.143-152
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    • 1988
  • This study was conducted to obtain basic data which affected engine performance of the power tiller being widely used in the rural area. Among the various factors affected engine performance, only flywheel weight was considered as the major factor in this study. Fuel consumption ratio, motoring loss, torque, vibration and mechanical efficiency of the engine tested were measured and analyzed on the four levels of flywheel weight (32.2, 29.7, 26.4, 24.2 kg). The results obtained were as follows: 1. The maximum output of 6 and 7.5 kW engine was 7.43 kW and 7.85 kW respectively. When flywheel weight was reduced from 32.2 kg to 24.2 kg, output power of the engine was increased 0.27 kW in 6 kW engine and increased 0.39 kW in 7.5 kW engine. 2. The fuel consumption ratio was decreased from 300.8 to 296.8 g/kW-hr in 6 kW engine and decreased from 313.6 to 312.8 g/kW-hr in 7.5 kW engine when the flywheel weight was reduced from 32.2 kg to 24.2 kg. 3. The mechanical efficiencies of the engine was increased from 76.1 to 76.8% in 6 kW engine and increased from 76.7 to 77.0% in 7.5 kW engine when the flywheel weight was reduced from 32.2 kg to 24.2 kg. 4. When the flywheel weight was reduced from 32.2 kg to 24.2 kg, a tendency of a little decrease of vibration at X- and Z-axis in 6 kW engine and of a little increase of vibration at Y-axis in 6 kW engine and all directions in 7.5 kW engine was observed. 5. Motoring losses was decreased from 2.33 to l.76 kW in 6 kW engine and decreased from 2.46 to 1.84 kW in 7.5 kW engine when the flywheel weight was reduced from 32.2 kg to 24.2 kg. From the above results and the flywheel weight calculated theoretically, it was recommendable that the flywheel weight should be reduced about 7 kg in 6 kW engine and about 10 kg in 7.5 kW engine, respectively.

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