• Title/Summary/Keyword: torque ripple

검색결과 655건 처리시간 0.024초

영구자석 매입형 BLDC 모터의 전자기적 가진력 및 소음특성에 관한 연구 (A Study on the Electrical Magnetic Excitation Force and Noise Characteristics in Motor of Interior Permanent magnetic Type)

  • 고홍석;은희광;김광준;신현정
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2000년도 춘계학술대회논문집
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    • pp.1139-1146
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    • 2000
  • The frequencies of principal noise in interior permanent motor originate form two sources. One is torque ripple that is composed of cogging torque, magnetic torque ripple and reluctance torque ripple. The other is induced by natural frequencies. In this paper, the torque ripple and its influence on noise was examined by theoretical analysis. Understanding relation of dynamic characteristics and noise, natural frequencies and mode shapes were obtained by experimentation and operational deflection shape was observed. Finally, the method of predicting frequencies of principal noise was proposed.

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4스위치 3상 BLDC 전동기의 토크 리플 저감을 위한 전류제어 알고리즘 (A Current Control Algorithm for Torque Ripple Reduction of Four-Switch Three-Phase Brushless DC Motors)

  • 박상현;김태성;이병국;현동석
    • 전력전자학회논문지
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    • 제9권2호
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    • pp.126-133
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    • 2004
  • 본 연구에서는 저 비용 응용분야에 적합한 4스위치 3상 BLDC 전동기의 새로운 전류 제어 알고리즘을 제안하였다. 4스위치 시스템에서 빠른 속도 및 토크 응답 그리고 적은 토크 리플과 같은 좋은 동작 특성을 얻기 위한 기준 전류 발생 기법을 제안하였다. 특히, 제안한 기법은 전류 전환시 발생되는 토크 리플을 현저히 저감시켜 4스위치 시스템을 산업 응용 분야에 보다 널리 적용할 수 있을 것으로 기대한다.

인버터로 구동되는 동기전동기 시스템에서의 토크리플 저감 (Torque Ripple Reduction in Synchronous Motor Systems Driven by an Inverter)

  • 원의연;이동근;홍순찬
    • 대한전기학회:학술대회논문집
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    • 대한전기학회 1995년도 하계학술대회 논문집 A
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    • pp.247-250
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    • 1995
  • This paper proposes a new method to reduce the torque ripple in vector controlled inverter fed synchronous motor systems. In three phase voltage source inverter systems, all the three line currents are generally not measured and the currents of two lines are measured through two sensors and two A/D converters. The measured currents may contain some error due to the non-ideality of the current sensors and A/D converters, and the error coefficient of two line currents are not same. As a result, the developed torque contains the torque ripple. The proposed method can eliminate the torque ripple by setting the error coefficient to same value. To verify the proposed method, digital simulations are carried out.

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SRM의 상전환 구간 토크리플 저감을 위한 제어기법에 관한 연구 (A Study on the Control Method for Torque Ripple Reduction during Phase Commutation)

  • 김태형;안진우
    • 전기학회논문지
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    • 제59권2호
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    • pp.333-337
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    • 2010
  • In this paper, an advanced torque control scheme of Switched Reluctance Motor(SRM) using modified non-linear logical TSF (Torque Sharing Function) with PWM is presented. In the proposed control scheme, a simple calculation of PWM duty ratio and switching rules from DITC(Direct Instantaneous Torque Control) can reduce the torque ripple with fixed switching frequency. The proposed control scheme is verified by the computer simulations and experimental results.

퍼지 이론과 슬라이딩모드 제어를 이용한 스위치드 릴럭턴스 전동기의 토크리플 저감 (Torque Ripple Minimization for Switched Reluctance Motors Using a Fuzzy Logic and Sliding Mode Control)

  • 윤재승;김동희;신혜웅;이교범
    • 전기학회논문지
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    • 제63권10호
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    • pp.1384-1392
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    • 2014
  • This paper presents a torque ripple reduction algorithm for the switched reluctance motor drives using the fuzzy logic and the sliding mode control. A turn-on angle controller based on the fuzzy logic determines the optimal turn-on angle. In addition, a sliding mode torque control (SMTC) methods reduces torque ripples instantaneously in the commutation region. The proposed algorithm does not require complex system models considering nonlinear magnetizing or demagnetizing periods of the phase current. According to the rotor speed and torque, the proposed controller changes the turn-on angle and reference torque instantaneously until the torque ripples are minimized. The simulation and experimental results verify the validity of minimizing the torque ripple performance.

진상각 제어에 따른 AC 서보 모터의 토오크 특성에 관한 연구 (A study on the torque characteristic of AC servo system by phase advance control)

  • 임윤택;손명훈;허욱열
    • 제어로봇시스템학회:학술대회논문집
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    • 제어로봇시스템학회 1992년도 한국자동제어학술회의논문집(국내학술편); KOEX, Seoul; 19-21 Oct. 1992
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    • pp.393-400
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    • 1992
  • The DC(Direct-Current) servo motor has widely used for many application areas, FA(Factory Automation), OA(Office Automation) and home applications. But DC servo motor needs periodical inspection because it has brush and commutator. Recently, AC servo motor has expanded it's application areas due to for the development of the power semi-conductor and control technology. But it has large torque ripple for it's small number of commutation. And it also has cogging torque due to permanent magenet rotor. Therefore it can't run balence rotarion. Many torque ripple reduction methods are published. In this paper, phase advanced method adopted for torque ripple reduction of AC servo motor. In this research, AC servo motor torque characteristic variation surveied under the phase advance control through the computer simulation. Under the simulation, the load inertia varied from 0.0001[Kg.m$^{2}$] to 0.0314[Kg.m$^{2}$]. The result os nonlinear simulation, torque and speed ripple of AC servo motor under the phase advance control reduced approximately 50[%] and 10[%]. And maximum torque of AC servo motor under phase advance control condition increased about 5[%] as compare with fixed switching time.

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Torque Ripple Reduction of a PM Synchronous Motor for Electric Power Steering using a Low Resolution Position Sensor

  • Cho, Kwan-Yuhl;Lee, Yong-Kyun;Mok, Hyung-Soo;Kim, Hag-Wone;Jun, Byoung-Ho;Cho, Young-Hoon
    • Journal of Power Electronics
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    • 제10권6호
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    • pp.709-716
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    • 2010
  • MDPS (motor driven power steering) systems have been widely used in vehicles due to their improved fuel efficiency and steering performance when compared to conventional hydraulic steering. However, the reduction of torque ripples and material cost are important issues. A low resolution position sensor for MDPS is one of the candidates for reducing the material costs. However, it may increases the torque ripple due to the current harmonics caused by low resolution encoder signals. In this paper, the torque ripple caused by the quantized rotor position of the low resolution encoder is analyzed. To reduce the torque ripples caused by the quantization of the encoder signals, the rotor position and the speed are estimated by measuring the frequency of the encoder signals. In addition, the compensating q-axis current is added to the current command so that the 6th order torque harmonic is attenuated. The reduction of torque ripples by applying the estimated rotor position and the compensated q-axis current is verified through experimental results.

Electromagnetic Structure Design Study of Fault-Tolerant Interior Permanent Magnet Machines for Electric Vehicles Using Harmonic Order Shaping

  • Liu, Guohai;Zeng, Yu;Zhao, Wenxiang;Chen, Qian
    • Journal of Magnetics
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    • 제21권4호
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    • pp.561-569
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    • 2016
  • Although pretty methods have been proposed to reduce torque ripple, they generally suffer from the decreased torque density. This paper will investigate the spoke-type interior permanent magnet (IPM) machine with shaping methods, including the sinusoidal (SIN), the inverse cosine (ICS), the sinusoidal with third harmonic (SIN+3rd), and the inverse cosine with third harmonic (ICS+3rd). In order to obtain low torque ripple and high torque density, the shaping method applied in rotor and stator at the same time, termed as the dual-shaping method, is proposed. This method is analytically derived and further confirmed by finite element method (FEM). It turns out that the ICS and ICS+3rd shaping methods are more suitable for outer rotors, while the SIN and the SIN+3rd shaping method should be used in inner stators. The original machine, the singular shaped machines and the dual-shaped machines on electromagnetic performances are compared for evaluation. The results verify that the dual-shaping method can improve torque density, whilst reducing torque ripple.

최대 토크/효율 및 최소 토크맥동을 위한 스위칭각/전압에 의한 SRM 운전 (A SRM driving with voltage and switching angle for maximum torque/efficiency and minimum torque ripple)

  • 차현록;김현덕;김광현;임영철;장도현
    • 전력전자학회논문지
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    • 제5권4호
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    • pp.309-317
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    • 2000
  • 이 논문은 4상 6극 SRM의 최대토크/효율 및 최소토크맥동 운전을 위한 적정 전압과 스위칭각에 관한 연구이다. SRM은 비선형적인 특성이강하여 해석적인 방법으로 특성을 고찰하거나 속도/토크 제어가 어려운 단점이 있다. 이 논문에서는 최대토크/효율 및 최소토크맥동의 운전이 가능한 최적의 스위칭각과 전압을 SIMULINKK를 이용하여 구하였다. 시뮬레이션 결과 최대토크운전에서는 속도는 스위칭각에 의존되고, 토크는 전압에 의존됨을 알 수 있었다. 뿐 만 아니라 최대효율, 최소토크리플운전에서는 전압보디는 속도와 스위칭각에 의해서 최대효율과 최소토크 리플이 발생되는 것을 알 수 있었다. 시뮬레이션에 의해서 구해진 최적각들을 ROM 데이터형식으로 참조 테이블을 만들어 마이크로 프로세서를 이용하여 구동하여 최대토크/효율, 최소토크리플 운전의 타당성을 보였다.

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Dithering기법에 의한 직접 토크 제어 방식의 토크리플 개선에 관한 연구 (A study on the torque ripple reduction of PMSM in direct torque control by using dither signal)

  • 이홍희;김정현
    • 전력전자학회:학술대회논문집
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    • 전력전자학회 2003년도 춘계전력전자학술대회 논문집(1)
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    • pp.415-419
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    • 2003
  • This paper focuses on a simple technique to reduced torque ripple in the direct torque control inverter for PMSM drive. It is actually impossible to raise the inverter switching frequency in the conventional system, although the hysterisis bandwidths for the stator flux and torque control are sufficiently diminished, because of the sampling Interval and the delay in estimating the flux and the torque In order to overcome the problem, the proposed method introduces a dithering technique into the conventional system by superposing triangular waves with high frequency and minute amplitude on the torque error. And the programable 3- stage lowpass filter is added instead of pure Integrator. Simulation results prove the feasibility of proposed strategy compared with conventional method.

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