• Title/Summary/Keyword: steam header configuration

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The design method of overheat protection orifice for power plant boiler super heated tube (발전용 보일러 주증기 튜브 과열방지용 오리피스 설계기법)

  • Kim, Bum-Shin;Yoo, Seong-Yeon;Ha, Jung-Su;Kim, Eui-Hyun
    • Proceedings of the KSME Conference
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    • 2003.11a
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    • pp.373-378
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    • 2003
  • It is important that overheat protection of super heated tube in boiler operation and maintenance. The overheat of super heat tube can make damage and rupture of tube material, which causes accidental shutdown of boiler. The super heated tube overheat is almost due to the lack of uniformity of gas temperature distribution. There are two ways to protect overheat of super heated tube. The one is to control hot gas operation pattern which is temperature or flow distribution. the other is to control super heated steam flow distribution. The former is difficult than the later, because of control device design. In this paper steam flow control method which uses orifices is proposed to protect overheat of super heat tube.

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Influence Analysis on the Number of Ruptured SG u-tubes During mSGTR in CANDU-6 Plants (중수로 증기발생기 다중 전열관 파단사고시 파단 전열관 수에 대한 영향 분석)

  • Seon Oh Yu;Kyung Won Lee
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.18 no.2
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    • pp.37-42
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    • 2022
  • An influence analysis on multiple steam generator tube rupture (mSGTR) followed by an unmitigated station blackout is performed to compare the plant responses according to the number of ruptured u-tubes under the assumption of a total of 10 ruptured u-tubes. In all calculation cases, the transient behaviour of major thermal-hydraulic parameters, such as the discharge flow rate through the ruptured u-tubes, reactor header pressure, and void fraction in the fuel channels is found to be overall similar to that of the base case having a single SG with 10 u-tubes ruptured. Additionally, as the conditions of low-flow coolant with high void fraction in the broken loop continued, causing the degradation of decay heat removal, the peak cladding temperature (PCT) would be expected to exceed the limit criteria for ensuring nuclear fuel integrity. However, despite the same total number of ruptured u-tubes, because of the different connection configuration between the SG and pressurizer, a difference is foud in time between the pressurizer low-level signal and reactor header low-pressure signal, affecting the time to trip the reactor and to reach the PCT limit. The present study is expected to provide the technical basis for the accident management strategy for mSGTR transient conditions of CANDU-6 plants.