• Title/Summary/Keyword: static efficiency

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Studies on the Improvement of the Fishing Efficiency of Purse Seine in the Sea Area of Cheju Island -The Changes of Seine Volume and Tension in the Purseline During Pursing- (제주도 주변해역 선망의 어획성능 향상에 관한 연구 -짐줄 체결 중 선망의 용적과 짐줄의 장력 변화 -)

  • 김석종
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.35 no.2
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    • pp.93-101
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    • 1999
  • A simple experimental method was used in an attempt to realize the elevation of the fishing ability of purse seine in the sea area of Cheju Island, the changes of seine volume and tension in the purseline during pursing. Experiments carried out on the six types simplified reduced model seines which were made of knotless nettings. The nettings were woven in different leg length 4.3, 5.0, 5.5, 6.0, 6.6 and 7.7mm of polyester 28 tex two threads two-ply twine, and each of the seines were named I, II, III, IV, V and Ⅵ seine. Dimension of seine models were 450cm for corkline and 85cmfor seine depth, each seines rigged up 160g of float for a floatline and 50g (underwater weight) of lead for a leadline. These model purse seines were made of the scale of 1/200 of its full scale, a 120 ton in the near sea of Cheju Island. Designing and testing for the model purse seines were based on the Tauti's law. Experiments were measured in the observation channel of a flume tank at the static conditions set up shooting and pursing equipments. Motion of purse seine during purse line was recorded by the two sets video camera for VTR which were placed in top and front of the model seine. The reading coordinate of seine volume carried out by the video digitization system, disk data for the purseline tension. An analysis were performed on the changes seine volume and tension in the purseline during pursing. The results obtained were as follows: 1. The seine volume during pursing was largest for Ⅵ seine with smallest d/l followed by V, IV, III, II and I seines, and tension in the purseline was small. 2. Seine volume during pursing can be expressed by the following equation; CVt=l-EXP[{2.79 (d/l)+0.35}t-33.37 (d/l) + 0.57] Where CVt is volume ratio, d is twine diameter, l is leg length and t is pursing time (sec). 3. Tension in the purse line during pursing can be expressed by the following equation; T= 1- EXP {0.57t + 13.36 (d/l)+2.97} Where T is tension (kg) in the purseline during pursing.

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Studies on Creep Behavior for Rice Stalks (벼줄기의 크리이프 거동(擧動)에 관한 연구)

  • Huh, Yun Kun;Kim, Sung Rai;Lee, Sang Woo
    • Korean Journal of Agricultural Science
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    • v.22 no.1
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    • pp.1-10
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    • 1995
  • All agricultural crops and products should be cultured, harvested, handled and processed by the proper mechanical methods in the mechanized farming systems. Agricultural crops might be injured or deformed through various working stages due to static or dynamic forces of machines. Mechanical forces had to be applied with proper degrees to the agricultural crops in incoincidence with properties of crops without any damage of crops so as to increase the work efficiency qualitatively. Knowledges of mechanical properties of agricultural materials are essential to prevent of agricultural crops in relation with mechanical farming system. This study was carried out to examine and analyze the creep behavior of the rice stalk on growing and harvesting periods by mechanical model with computer measurement system in radial directional compressive force and bending force. The creep behavior of the rice stalk could be predicted precisely and its results approached closely to the measured values. The creep behaviors were increased greatly with increase of compressive force, namely, the steady state creep behavior occurred at the force less then 25N and the logarithmic creep behavior at the force bigger than 30N. The instantaneous elastic modulus $E_o$ and the retardation time ${\tau}_K$ were increased together with increase of applied forces, meanwhile the retarded elastic modulus $E_r$ and viscosity ${\eta}_v$ were decreased with increase of applied forces in mechanical model being expected the creep behavior in relation with the level of applied forces, which was well explained that the rice stalk might be visvo-elastic material. In the creep test along the stalk portion with compressive force and bending force, the intermediate portion showed greatest values and also the lower portion showed the least values, which implied that the intermediate portions of rice stalk were very weak. The steady state creep behavior occured at the intermediate portion and the upper portion in the rice stalk at the compressive force larger than 25.0N, which showed the possibility of injury due to external forces.

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Deodorization of H2S, CH3SH in Soil Filter Reactors Packed with Montmorillonites, Rice Hulls and Thickening-activated Sludge (Montmorillonites, 왕겨 및 농축활성슬러지를 충진한 토양상에서의 H2S, CH3SH의 제거)

  • Kim, Hwan-Gi;Park, Chan-Soo
    • Journal of Korean Society of Environmental Engineers
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    • v.22 no.1
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    • pp.43-52
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    • 2000
  • Deodorization characteristics and removal rate of sulfur-containing odor have been investigated in the soil filter reactors packed with montmorillonites (Mont.), rice hulls(Rh.), and thickening-activated sludge(Ts.). And variation of pH and $SO_4{^{2-}}$ with the removal of malodorous sulfur compounds have been investigated together. As compared removal rate of montmorillonites between wet and dry condition for sulfur compounds through batch test, it showed that wet condition was better than dry one; removal ratio, as wet/dry, was $H_2S$ of 1.2 and $CH_3SH$ of 1.9, and decrease of pH and increase of $SO_4{^{2-}}$ concentration in the wet condition also showed to be larger than in dry condition. In continuous test for biological deodorization experiment, removal rate of sulfur compounds in reactor packed with Mont., Rh. and Ts, was more than 98 %, and the variation of static pressure was maintained stably under condition of SV $150h^{-1}$, LV 4.2 mm/sec and SV $200h^{-1}$, LV 5.6 mm/sec, and in reactor packed with Mont. and Rh., $H_2S$ was 76.4 % to 87.2 % and $CH_3SH$ was 87.8 % to 93.3 % under the same condition. From above results, it ascertained that it can obtain the high deodorization efficiency by inoculating thickening-activated sludge in soil filter using montmorillonites.

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Analysis of Greenhouse Thermal Environment by Model Simulation (시뮬레이션 모형에 의한 온실의 열환경 분석)

  • 서원명;윤용철
    • Journal of Bio-Environment Control
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    • v.5 no.2
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    • pp.215-235
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    • 1996
  • The thermal analysis by mathematical model simulation makes it possible to reasonably predict heating and/or cooling requirements of certain greenhouses located under various geographical and climatic environment. It is another advantages of model simulation technique to be able to make it possible to select appropriate heating system, to set up energy utilization strategy, to schedule seasonal crop pattern, as well as to determine new greenhouse ranges. In this study, the control pattern for greenhouse microclimate is categorized as cooling and heating. Dynamic model was adopted to simulate heating requirements and/or energy conservation effectiveness such as energy saving by night-time thermal curtain, estimation of Heating Degree-Hours(HDH), long time prediction of greenhouse thermal behavior, etc. On the other hand, the cooling effects of ventilation, shading, and pad ||||&|||| fan system were partly analyzed by static model. By the experimental work with small size model greenhouse of 1.2m$\times$2.4m, it was found that cooling the greenhouse by spraying cold water directly on greenhouse cover surface or by recirculating cold water through heat exchangers would be effective in greenhouse summer cooling. The mathematical model developed for greenhouse model simulation is highly applicable because it can reflects various climatic factors like temperature, humidity, beam and diffuse solar radiation, wind velocity, etc. This model was closely verified by various weather data obtained through long period greenhouse experiment. Most of the materials relating with greenhouse heating or cooling components were obtained from model greenhouse simulated mathematically by using typical year(1987) data of Jinju Gyeongnam. But some of the materials relating with greenhouse cooling was obtained by performing model experiments which include analyzing cooling effect of water sprayed directly on greenhouse roof surface. The results are summarized as follows : 1. The heating requirements of model greenhouse were highly related with the minimum temperature set for given greenhouse. The setting temperature at night-time is much more influential on heating energy requirement than that at day-time. Therefore It is highly recommended that night- time setting temperature should be carefully determined and controlled. 2. The HDH data obtained by conventional method were estimated on the basis of considerably long term average weather temperature together with the standard base temperature(usually 18.3$^{\circ}C$). This kind of data can merely be used as a relative comparison criteria about heating load, but is not applicable in the calculation of greenhouse heating requirements because of the limited consideration of climatic factors and inappropriate base temperature. By comparing the HDM data with the results of simulation, it is found that the heating system design by HDH data will probably overshoot the actual heating requirement. 3. The energy saving effect of night-time thermal curtain as well as estimated heating requirement is found to be sensitively related with weather condition: Thermal curtain adopted for simulation showed high effectiveness in energy saving which amounts to more than 50% of annual heating requirement. 4. The ventilation performances doting warm seasons are mainly influenced by air exchange rate even though there are some variations depending on greenhouse structural difference, weather and cropping conditions. For air exchanges above 1 volume per minute, the reduction rate of temperature rise on both types of considered greenhouse becomes modest with the additional increase of ventilation capacity. Therefore the desirable ventilation capacity is assumed to be 1 air change per minute, which is the recommended ventilation rate in common greenhouse. 5. In glass covered greenhouse with full production, under clear weather of 50% RH, and continuous 1 air change per minute, the temperature drop in 50% shaded greenhouse and pad & fan systemed greenhouse is 2.6$^{\circ}C$ and.6.1$^{\circ}C$ respectively. The temperature in control greenhouse under continuous air change at this time was 36.6$^{\circ}C$ which was 5.3$^{\circ}C$ above ambient temperature. As a result the greenhouse temperature can be maintained 3$^{\circ}C$ below ambient temperature. But when RH is 80%, it was impossible to drop greenhouse temperature below ambient temperature because possible temperature reduction by pad ||||&|||| fan system at this time is not more than 2.4$^{\circ}C$. 6. During 3 months of hot summer season if the greenhouse is assumed to be cooled only when greenhouse temperature rise above 27$^{\circ}C$, the relationship between RH of ambient air and greenhouse temperature drop($\Delta$T) was formulated as follows : $\Delta$T= -0.077RH+7.7 7. Time dependent cooling effects performed by operation of each or combination of ventilation, 50% shading, pad & fan of 80% efficiency, were continuously predicted for one typical summer day long. When the greenhouse was cooled only by 1 air change per minute, greenhouse air temperature was 5$^{\circ}C$ above outdoor temperature. Either method alone can not drop greenhouse air temperature below outdoor temperature even under the fully cropped situations. But when both systems were operated together, greenhouse air temperature can be controlled to about 2.0-2.3$^{\circ}C$ below ambient temperature. 8. When the cool water of 6.5-8.5$^{\circ}C$ was sprayed on greenhouse roof surface with the water flow rate of 1.3 liter/min per unit greenhouse floor area, greenhouse air temperature could be dropped down to 16.5-18.$0^{\circ}C$, whlch is about 1$0^{\circ}C$ below the ambient temperature of 26.5-28.$0^{\circ}C$ at that time. The most important thing in cooling greenhouse air effectively with water spray may be obtaining plenty of cool water source like ground water itself or cold water produced by heat-pump. Future work is focused on not only analyzing the feasibility of heat pump operation but also finding the relationships between greenhouse air temperature(T$_{g}$ ), spraying water temperature(T$_{w}$ ), water flow rate(Q), and ambient temperature(T$_{o}$).

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