• Title/Summary/Keyword: settling basin effluent

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Case Study on Remodeling Outlet Structure within a Sedimentation Basin for Improving Performance (침전지 유출부 구조 Remodeling을 통한 개선사례 연구)

  • Kim, Seong-Su;Park, No-Suk;Moon, Yong-Taik;Lee, Sun-Ju
    • Journal of Korean Society of Water and Wastewater
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    • v.20 no.6
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    • pp.911-918
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    • 2006
  • This study was conducted to evaluate the effect of the launder type on settling performance and hydrodynamic behavior within the two certain full-scale sedimentation basins (each flow rate/one basin; $10,000m^3/d$); one is the transverse typed launder(existing basin) and the other is building the finger type launder in combination with the longitudinal baffle. Comparative experimental investigations have been carried out through residual turbidity and particle concentration measurements in each effluent from two basins with the transverse and the finger type launders, respectively. From the experimental results, we could observe that turbidity removal rate in the finger type launder basin (modified basin) is about 30% higher than that in the transverse type launder basin (existing basin). Also, from the measurement of total particle concentration in each effluent, the removal efficiency was improved about 27% within modified basin compared to the existing basin. In order to explain the comparative experimental results and investigate the hydridynamic behavior within each basin in more detail, we conducted computational fluid dynamics (CFD) simulation and verified simulation results with acoustic Doppler velocimetry (ADV) technique. From the CFD simulation, it was investigated that extreme upward flow occurs underneath of the transverse launder. On the other hand, in the case of modified basin, the upward flow, which occurred in the beneath of launder, was much less than that in the existing basins.

A Study on the Diatomaceous Earth Filtration of Settling Basin Effluent (정수장 침전지 유출수의 규조토 여과에 관한 연구)

  • Shin Dae-Yewn;Ji Sung-Nam;Moon Ok-Ran;Kim Ji-Yeong;Suh Dong-Woo;Cho Young-Kwan
    • Journal of Environmental Health Sciences
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    • v.30 no.5 s.81
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    • pp.410-416
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    • 2004
  • The objective of this investigation was to evaluate applicability of precoat filtration that can be substituted for rapid sand filter of conventional water treatment system(CWTS). Precoat filter used in this experiment are candle filter. Element disk of candle are pore size $10{\mu}m(R),\;20{\mu}m(B)$ And diatomaceous earth are cake pore size $3.5{\mu}m$(Standard Super- Cel; A), $7{\mu}m$(Hyflo Super-Cel; B) and $17{\mu}m$(Celite 545RV; C). $2kg/m^2$ diatomaceous earth is used for precoating, it coated candle in $5{\sim}6mm$ thickness. 1. Al adsorption dosages by diatomaceous earth used in experimental we Hyflo Super-Cel 0.843mg/g, Standard Super-Cel 0.782 mg/g and Celite 545RV 0.766 mg/g. 2. Filtrate of precoat filter during 60min are R-C combination 20.7($m^3/m^2$)>B-C 18.3($m^3/m^2$)>B-B 15.0($m^3/m^2$)> R-B 12.9($m^3/m^2$)> R-A 11,093($l/m^2$). 3. Water quality of precoat filter effluent are thus. $KMnO_4$ consumption are $1.10{\sim}2.20mg/l$, removal rate are $30.9{\sim}65.6\%$. They are R-A 1.10(mg/l)(removal rate $65.6\%$). R-C(2.20 mg/l)(removal rate $30.9\%$). 4. $Al^{3+}$ are not detected with all combination, removal rate $100\%$. 5. Considering water quality and flux, continued running time of R-A combination is 7 hr. Accumulated filtrate are $74.4 m^3/m^2$, average flux is $177.2 l/m^2{\cdot}min$. And filtrate per diatomaceous earth 1g are 37.2 l. 6. R-A effluent's water quality are $KMnO_4$ Consumption 1.10(mg/l), DOC 1.161 mg/1, Al 0.0 mg/1, $UV_{254}$ 0.016/cm, Turbidity 0.1(NTU). R-A combination is suitable to precoat filtration for the settling basin effluent treatment.

Removal of Fine Suspended Solids and Soluble Heavy Metals in H Mine Drainage using Settling and Filtering : Field Application (침전 및 여과를 통한 H 광산배수 내 미세부유물질 및 용해성 중금속의 제거 : 현장실험을 중심으로)

  • Oh, Minah;Kim, WonKi;Oh, Seungjin;Kim, DukMin;Lee, SangHoon;Lee, Jai-Young
    • Journal of Soil and Groundwater Environment
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    • v.18 no.7
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    • pp.54-62
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    • 2013
  • Fine suspended solids and soluble heavy metals generated from mine drainage could destroy environment as the aesthetic landscapes, and depreciate water quality. Therefore, this research is focused on process development applied the actual field for controlling fine suspended solids and heavy metals, and so that bench-scale tests were performed for field application based on advanced researches. The field of mine drainage in this research was in H mine located Taebaek-si, Gangwon-do. The inclination plates were mounted 2 kinds of arrangement (octagon and radial types) in circle type settling basin. The inclination plates could be helped to settle of suspended solids; decreased 34% of suspended solids and 50% of turbidity in effluent. Radial type of inclination plates showed the results that is more efficient to settle of suspended solids (average to 3.45 mg/L) compared to octagon type. In the experiments to decrease retention time of mine drainage in settling basin from 6 hrs to 1.5 hrs, suspended solid concentration was exceeded to 30 mg/L as the standard for suspended solid at 10 days after the operation under tha retention time of 3hrs and 1.5hrs. In the tests for filtration, granular activated carbons were indicated the better effective to filtering and absorption of fine suspended solid and soluble heavy metals than anthracite.

A study on sedimentation characteristic according to concentration change of top soil lost by flood (유실토양의 농도변화에 따른 침강특성에 대한 연구)

  • Jeon, Young-Bong;Kang, Seon-Hong
    • Journal of Korean Society of Water and Wastewater
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    • v.28 no.5
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    • pp.581-587
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    • 2014
  • Sediment basin that is typical facility installed for development business to prevent soil erosion has low removal efficiency and therefore, it causes complaints from the residents and has a bad effect on ecosystem. Thus there is a limit to control soil erosion using the existing design methods of sediment basin, so the purposes of this study is providing suitable design factors for sediment basin with regarding soil characteristic of development areas and analysing sedimentation characteristic by inflow concentration changes. The results, for analyzing the sedimentation characteristic by soil concentrations within approximately 2,000 ~ 20,000 mg/L of initial SS concentration, indicated similar sedimentation trends for same soil in the supernatant regardless of initial concentrations. However, for different soil characteristic (percent finer), there are different results in sedimentation rate and concentrations of the supernatant. Thus it is recommended that sediment basin to prevent soil erosion during construction should be designed based on retention time derived from soil sedimentation experiments regardless of inlet concentration. In addition, installing the soil erosion prevention facility at the back to satisfy effluent water quality should be considered to minimize soil erosion effectively.

Distribution and Migration Characteristics of Explosive Compounds in Soil at Military Shooting Ranges in Gyeonggi Province (경기도 북부지역 군용 사격장 토양에 존재하는 화약물질 분포 및 이동 특성 조사)

  • Bae, Bumhan;Park, Jieun
    • Journal of the Korean GEO-environmental Society
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    • v.15 no.6
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    • pp.17-29
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    • 2014
  • A remedial investigation was conducted at five military training ranges in northern Gyeonggi province to collect information necessary for the design of on-site treatment facilities for the abatement of explosive compounds release to the environment. These information includes (i) identification of dominant explosive compounds in each range, (ii) discharge/migration routes, and (iii) contaminant distribution in particle size fraction and settling velocity of the soils. The results of investigation showed that TNT and RDX are the major contaminants but the extent of contamination varied depending on the types of military training practices and topography of the site. RDX was also detected in the subsurface soil and in the nearby stream within the training ranges, suggesting release of contaminants to streams. The median concentrations of explosives in the surface soil were less than 20 mg/kg despite several 'hot spots' in which explosives concentrations often exceeds several hundred mg/kg. The average clay contents in the soil of target area was less than 5 % compared to 12 % in the control, indicating loss of smaller particles by surface runoff during rainfall due to lack of vegetative land cover. Analysis of explosive compounds and particle size distribution showed that the amount of explosive compounds in soil particles smaller than 0.075 mm was less than 10 % of the total. Settling column tests also revealed that the quantity of explosive compounds in the liquid phase of the effluent was greater than that in the solid phase. Therefore, pre-treatment of particulate matter in surface runoff of shooting range with a simple settling basin and subsequent effluent treatment with planted constructed wetlands as polishing stage for explosives in the aqueous phase would provide the shooting ranges with a self-standing, sustainable, green solution.

Reuse and Concentration of Sewage by Forward Osmosis Using Fertilizer as Draw Solution (비료 유도용액의 정삼투를 이용한 하수의 재이용 및 농축)

  • Kim, Seung-Geon;Lee, Ho-Won
    • Applied Chemistry for Engineering
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    • v.30 no.1
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    • pp.122-131
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    • 2019
  • In order to reuse and concentrate the sewage, a forward osmosis using fertilizer as draw solution was applied. Sewage-1, which is the supernatant after settling for 30 minutes for the primary settling basin influent, and Sewage-2, which is the supernatant after settling for 30 minutes for the effluent, and Sewage-3, which is the filtrate filtered through a $1{\mu}m$ cartridge filter for the effluent were tested. Eight draw solutions of $NH_4H_2PO_4$, KCl, $KNO_3$, $NH_4Cl$, $(NH_4)_2HPO_4$, $NH_4NO_3$, $NH_4HCO_3$, and $KHCO_3$ were used in consideration of osmotic pressure, solubility and pH. In the case of Sewage-3, the permeate flux was almost similar to that of the discharge water of the sewage treatment plant, and was larger than that of Sewage-1 and Sewage-2. $NH_4H_2PO_4$ was the smallest, and $NH_4NO_3$ was the largest in the specific reverse solute flux. $NH_4H_2PO_4$ was found to be most useful for the reuse and concentration of sewage because it contains nitrogen and phosphorus, which are the major components of fertilizer, as well as low specific reverse solute flux. When $NH_4H_2PO_4$ was used as the draw solution, the concentration factor after 24 hours for Sewage-3 was 1.72.

Application of Ultra Rapid Coagulation for Securing Water Resource II: Study of organic, metals, and nutrients removal (수자원 확보를 위한 URC공법의 적용 I: 유기물, 중금속, 영양염의 제거특성에 관한 연구)

  • Park, Se Jin;Yoon, Tai Il;Kim, Jae Hyung;Cho, Kyung Chul
    • Clean Technology
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    • v.6 no.1
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    • pp.27-38
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    • 2000
  • A physicochemical process called Ultra Rapid Coagulation(URC) can dramatically remove organics, metals, and phosphates in wastewater by adding weighted coagulation additive(WCA) and recycling sludge into the coagulation basin to increase the growth rate and adsorption ability of floc. Also this process can improve floc settling rate than conventional coagulation process and reduce the pollutants loaded into the receiving water for securing water source. It was evaluated that WCA and sludge added have effects on the removal efficiency and estimated the possibilities of reusing the effluent from this process.

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Development and Lab-scale Plant Study of Coagulation Sedimentation Module using Cyclone (선회류를 이용한 응집침전모듈의 개발 및 실증 연구)

  • Moon, Jinyoung;Cho, Young-Gun;Song, Seung-Jun;Kim, Jin-Han
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.15 no.5
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    • pp.3336-3344
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    • 2014
  • The purpose of this study is small scale coagulation module is developed and demonstrated through a lab-scale test. Recent as a sewage treatment rate increases, have heightened the interest in the necessity on the nonpoint source and developing a small processing unit has been increased. Coagulation sedimentation module in this study is additional growth of floc through swirling in the outside zone, reduction of microstructure floc number and the internal settling zone through vertical/level flow complex sedimentation method after the coagulation process precipitation method as an effective high separation efficiency can be divided was also assessed. Coagulation sedimentation module can increase the load factor was 4.4 times compared to conventional clarifier base on the same volume and surface area through vertical/level flow. In this study, this process was selected formation and maintenance of swirling and uniform flow distribution in the internal settling zone as an important design factor, to derive its FLUENT was used to characteristics of the flow model. Through the simulation of swirling, influent velocity, dimensions of external basin, hopper depth of bottom cone was determined and through analysis of velocity distribution, flow distribution detailed specifications are derived like as diameter and number of effluent hole. Lab-scale($120{\ell}/hr$) test results, influent of 300~800 NTU to less than 10 NTU without polymer feeding was able to operate in the 20minutes retention time(surface loading rate $37.3m^3/m^2$-day), and through analysis FLUENT the possibility of using design parameters were derived.