• 제목/요약/키워드: rotor loss

검색결과 299건 처리시간 0.022초

Analysis of Slot Leakage Reactance of Submersible Motor with Closed Slots during Starting Transient Operation

  • Bao, Xiaohua;Di, Chong;Fang, Yong
    • Journal of Electrical Engineering and Technology
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    • 제11권1호
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    • pp.135-142
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    • 2016
  • Generally, closed slots are adopted to reduce the water friction loss in both the stator and the rotor of water filling submersible motor due to the special environment of operation. One of the obvious differences between the traditional induction motors and water filling submersible motors is that the submersible motors only need relatively smaller starting torque. This paper aims to analyze the slot leakage reactance of water filling submersible motor during starting transient operation. An improved analytical method which considered the magnetic saturation of the slot bridge and the skin effect of rotor bars is proposed. The slot permeance factor which has a direct impact on the slot leakage reactance is calculated. Then finite element models with different stator slot types are constructed and search coils are introduced to measure the slot flux linkage. Moreover, the starting performances of the models with two typical stator slots are compared and the flux leakage characteristics are obtained. Finally, the results obtained by finite element method are very close to the results obtained by analytical method.

CFD prediction and simulation of a pumpjet propulsor

  • Lu, Lin;Pan, Guang;Sahoo, Prasanta K.
    • International Journal of Naval Architecture and Ocean Engineering
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    • 제8권1호
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    • pp.110-116
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    • 2016
  • In this study an attempt has been made to study the hydrodynamic performance of pumpjet propulsor. Numerical investigation based on the Reynolds Averaged NaviereStokes (RANS) computational fluid dynamics (CFD) method has been carried out. The structured grid and SST ${\kappa}-{\omega}$ turbulence model have been applied. The numerical simulations of open water performance of marine propeller E779A are carried out with different advance ratios to verify the numerical simulation method. Results show that the thrust and the torque are in good agreements with experimental data. The grid independent inspection is applied to verify accuracy of numerical simulation grid. The numerical predictions of hydrodynamic performance of pumpjet propulsor are carried out with different advance ratios. Results indicate that the rotor provides the main thrust of propulsor and the balance performance of propulsor is generally satisfactory. Additionally, the curve of propulsor efficiency is in good agreement with experimental data. Furthermore, the pressure distributions around rotor and stator blades are reasonable. Beyond that, the existence of tip clearance accounts for the appearance of tip vortex that leads to a further loss in efficiency and a probability of cavitation phenomenon.

100,000 RPM급으로 회전하는 에어공구의 성능측정에 관한 연구 (Study on Measuring the Performance of an Air Tool Operating at 100,000 RPM Class)

  • 조수용;김은종
    • 한국유체기계학회 논문집
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    • 제6권3호
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    • pp.44-50
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    • 2003
  • An experiment is conducted for measuring the performance of an air tool, which is operated at 100,000 RPM in an unloaded state with very low torque. A 551 kPa in gauge pressure is supply to the inlet of an air tool. An experimental apparatus is developed as a friction type dynamometer. Inlet total pressure, air flow rate, rotational speed and operating force are measured simultaneously. Torque, output power and specific output power are obtained with different rotational speeds. Those are compared with the experimental results which were obtained by a commercial dynamometer. However, no commercial dynamometers are available for measuring the torque above 30,000 RPM. In order to reduce the rotational speed, a reduction gear is applied between the air tool and the commercial dynamometer. Torque and power obtained by the commercial dynamometer show $55\%$ lower than those obtained by the developed friction type dynamometer, because the mass is added to the rotor of air tool for the braking system of the commercial dynamometer and power loss is generated by the reduction gear. From the compared results, the friction type dynamometer should be applied for measuring the performance of the air tool operating at low torque and high RPM.

터보펌프 터빈의 토크 및 시동특성 연구 (Research on the Torque and Starting Characteristics of a Turbopump Turbine)

  • 정은환;이항기;박편구;홍문근;김진한
    • 한국추진공학회지
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    • 제17권1호
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    • pp.35-41
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    • 2013
  • 75톤 추력급 터보펌프 터빈의 토크 특성을 성능시험 데이터를 바탕으로 분석하였다. 터빈의 토크는 해석적으로 고정된 압력비에서 보정 선속도의 일차함수로 표현되며 이를 시험적으로 확인하였다. 일정 압력비 이상의 영역에서는 보정선속도-무차원 토크 변화가 일정하게 나타나는 현상도 아울러 발견하였다. 분석된 토크 특성과 파이로 시동기의 시험 측정 데이터를 이용하여 터보펌프의 시동특성을 예측한 결과 터보펌프 설계회전수의 약 50%의 수준에 이르는 시간은 0.7초 이내인 것으로 나타났다. 파이로 시동기에서 터빈입구까지의 열손실은 최대회전수를 90 rpm 정도 줄어들게 하는 것으로 예측되었다.

Development and Performance Investigation on a 60kW Induction Motor for EV Propulsion

  • Chun, Yon-Do;Park, Byoung-Gun;Kim, Dong-Jun;Choi, Jae-Hak;Han, Pil-Wan;Um, Sukkee
    • Journal of Electrical Engineering and Technology
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    • 제11권3호
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    • pp.639-643
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    • 2016
  • This paper introduces the development process and investigation of a 60kW induction motor for electric vehicles. We present performance improvement in the induction motor of electric vehicle using copper die-casting based on a multi-gate process. Copper die-casting motors can reduce the size of the motor, the loss of the rotor, and material costs. We also introduce electromagnetic, thermal, mechanical design and analysis results that satisfy the design and the performance requirements. In order to analyze losses accurately of induction motor, commercial finite element analysis is done considering PWM voltage and thermal characteristics by using lumped-circuit parameters. Experimental tests are also carried out to validate the traction motor design.

신개념 로터리 엔진의 개발 (I) - 개념과 이론적 성능 분석 - (Development of A New Concept Rotary Engine (I) - Concept and theoretical performance analysis -)

  • 오문근;이규승;박원엽
    • Journal of Biosystems Engineering
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    • 제28권1호
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    • pp.27-34
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    • 2003
  • Present combustion engines have reached almost at the limit of development due to the fundamental structural problems. This study was carried out to propose a new concept internal combustion engine which has great potential advantages to the conventional engines. Proposed new concept engine is a kind of rotary engine. A rotor is rotating concentrically in a cylinder which is divided into two partitioning valves. and it makes four compartments in the cylinder. The volumes of each of four compartments are changing continuously with the rotor movement, and performs the functions of intake, compression. expansion and exhaust simultaneously. The results of this study can be summarized as follows. 1. Expected theoretical thermal efficiency is 44.9 percent at the condition of 1000rpm and compression ratio of 8.0. which is almost the same as that of the conventional engines. i.e., piston and Wankel rotary engine. 2. The new concept engine has 2. working strokes in every revolution. Therefore. the new concept engine can reduce the specific weight and volume than four-stroke piston engine. 3. The torque variation is very small. therefore minimal noise and vibration are expectable. 4. The new concept engine can reduce mechanical energy loss than piston engine because neither crank mechanism nor eccentrical motion exists.

Research on Forces and Dynamics of Maglev Wind Turbine Generator

  • Wang, Nianxian;Hu, Yefa;Wu, Huachun;Zhang, Jinguang;Song, Chunsheng
    • Journal of Magnetics
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    • 제18권4호
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    • pp.443-453
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    • 2013
  • Maglev wind turbine generator (MWTG) technology has been widely studied due to its low loss, low maintenance cost, and high reliability. However, the dynamics of the magnetic bearing system differ fromthe those of the traditional mechanical bearing system. A horizontal axial MWTG supported with a permanent magnetic bearing is designed in this research and the radial forces and the natural frequencies of the rotor system are studied. The results show that the generatorhas a cyclical magnetic forceand an unreasonable bearing stiffness may mean that the rotor system needs to work in the resonance region; the bearing stiffness is the key factor to avoid this problem. This is the main rule of the bearing stiffness design in the MWTG, and this rule can also be used in other maglev permanent magnet motors.

화력발전소에 사용되는 개선된 오일 디플렉터 개발 (Development of an Advanced Oil Deflector Used in Thermoelectric Power Plant)

  • 최용훈;곽효서;이창렬;김철
    • 한국정밀공학회지
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    • 제33권8호
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    • pp.661-668
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    • 2016
  • Oil deflector prevents oil leakage that occurs in thermoelectric power plant at operating lubricant facilities. Vibration of rotating rotor-induced wear of aluminum tooth in existing oil deflector leads to oil leakage as well as life shortening of the tooth. In this study, an advanced oil deflector was developed for shock absorption and prevention of wear by decreasing clearance (from 0.5 mm to 0.2 mm) between rotor and tooth to minimize oil leakage, and by replacing 2 aluminum teeth in outmost of the oil deflector with hi-performance seal made of engineering plastic. The CFD results were compared between advanced vs. existing oil deflector to determine the amount of oil loss. Structural safety was verified through impact analyses according to the three kinds of engineering plastics, considering cost efficiency, and optimal material of hi-performance seal was chosen.

터보펌프 터빈의 토크 및 시동특성 연구 (Research on the Torque and Starting Characteristics of a Turbopump Turbine)

  • 정은환;이항기;박편구;홍문근;김진한
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2012년도 제38회 춘계학술대회논문집
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    • pp.4-10
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    • 2012
  • 75톤 추력급 터보펌프 터빈의 토크 특성을 성능시험 데이터를 바탕으로 분석하였다. 터빈의 비토크는 해석적으로 고정된 압력비에서 보정 선속도의 일차함수로 표현되며 이를 시험적으로 확인하였다. 일정 압력비 이상의 영역에서는 보정선속도-비토크 변화가 일정하게 나타나는 현상도 아울러 발견하였다. 분석된 토크 특성과 파이로 시동기의 시험 측정 데이터를 이용하여 터보펌프의 시동특성을 예측한 결과 터보펌프 설계회전수의 약 50%의 수준에 이르는 시간은 0.7초 이내인 것으로 나타났다. 파이로 시동기에서 터빈입구까지의 열손실은 최대회전수를 약 90 rpm 줄어들게 하는 것으로 예측되었다.

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허브 측 선단 수정에 따른 터빈 로터의 공력 특성에 대한 수치적 연구 (Numerical Study of Aerodynamics of Turbine Rotor with Leading Edge Modification Near Hub)

  • 김대현;이원석;정진택
    • 대한기계학회논문집A
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    • 제37권8호
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    • pp.1007-1013
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    • 2013
  • 이 논문은 터빈 로터의 형상변화에 따른 공력 특성에 대하여 분석하였다. 본 논문의 터빈은 헬리콥터의 보조동력 장치로 사용되는 소형엔진이다. 소형엔진은 팁 형상의 구조적 취약성 때문에 성능을 향상시키기 어렵다. 그러므로, 터빈의 허브를 개선하는 것이 여러 가지 측면에서 유리하다. 터빈의 작동유체는 고온 고압의 가스이다. 터빈표면의 열전달률이 고려되었을 때, 열부하에 의한 블레이드의 손상을 줄이기 위해서는 블레이드 표면의 열전달률 분포를 고찰하여야 한다. 수치모사 결과를 검증용 실험값과 비교하였을 때, SST난류모델은 공력 특성을 잘 반영하고 열전달 예측성능도 우수하였다. 결론적으로, 허브측 선단에서 구륜설계(bulbous design)를 적용하였을 때 공력효율이 향상되었고, 전체 공력 손실 중 끝벽 손실은 15% 감소되었다.