• Title/Summary/Keyword: pilot plant scale

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Design and Operation of 3MW Pilot Plant of $Mg(OH)_2$ Flue Gas Desulfurization Process

  • Kim, In-Won;Jin, Sang-Hwa;Choi, Byung-Moon;Lee, Hyung-Keun
    • 제어로봇시스템학회:학술대회논문집
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    • 2001.10a
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    • pp.116.2-116
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    • 2001
  • Korea Institute of Energy Research(KIER) has designed the 3MW pilot scale wet FGD process based on the experimental results of the bench scale FGD system which can treat 150 m3/hr of flue gases. The effects of process chemistry, packing material, and operating variables including L/G ratio, pH, scrubber pressure drop were investigated. In cooperation with Kyunggi Chemicals, the 3MW pilot scale plant was established on the industrial site at Onsan, Korea. This system has been operating since October 1999. This paper introduces an outline of the design features of the pilot plant and discusses its operational results.

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Optimization of Supercritical Water Oxidation(SCWO) Process for Decomposing Nitromethane (Nitromethane 분해를 위한 초임계수 산화(SCWO) 공정 최적화)

  • Han, Joo Hee;Jeong, Chang Mo;Do, Seung Hoe;Han, Kee Do;Sin, Yeong Ho
    • Korean Chemical Engineering Research
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    • v.44 no.6
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    • pp.659-668
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    • 2006
  • The optimization of supercritical water oxidation (SCWO) process for decomposing nitromethane was studied by means of a design of experiments. The optimum operating region for the SCWO process to minimize COD and T-N of treated water was obtained in a lab scale unit. The authors had compared the results from a SCWO pilot plant with those from a lab scale system to explore the problems of scale-up of SCWO process. The COD and T-N in treated waters were selected as key process output variables (KPOV) for optimization, and the reaction temperature (Temp) and the mole ratio of nitromethane to ammonium hydroxide (NAR) were selected as key process input variables (KPIV) through the preliminary tests. The central composite design as a statistical design of experiments was applied to the optimization, and the experimental results were analyzed by means of the response surface method. From the main effects analysis, it was declared that COD of treated water steeply decreased with increasing Temp but slightly decreased with an increase in NAR, and T-N decreased with increasing both Temp and NAR. At lower Temp as $420{\sim}430^{\circ}C$, the T-N steeply decreased with an increase in NAR, however its variation was negligible at higher Temp above $450^{\circ}C$. The regression equations for COD and T-N were obtained as quadratic models with coded Temp and NAR, and they were confirmed with coefficient of determination ($r^2$) and normality of standardized residuals. The optimum operating region was defined as Temp $450-460^{\circ}C$ and NAR 1.03-1.08 by the intersection area of COD < 2 mg/L and T-N < 40 mg/L with regression equations and considering corrosion prevention. To confirm the optimization results and investigate the scale-up problems of SCWO process, the nitromethane was decomposed in a pilot plant. The experimental results from a SCWO pilot plant were compared with regression equations of COD and T-N, respectively. The results of COD and T-N from a pilot plant could be predicted well with regression equations which were derived in a lab scale SCWO system, although the errors of pilot plant data were larger than lab ones. The predictabilities were confirmed by the parity plots and the normality analyses of standardized residuals.

Removal of Toxicity from Kraft Pulp Mill Effluents by Activated Sludge Process (활성슬러지 공정에 의한 Kraft 펄프 폐수의 독성 제거)

  • Kim, Yeong-Kwan
    • Journal of Korean Society of Water and Wastewater
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    • v.8 no.3
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    • pp.9-18
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    • 1994
  • Activated sludge pilot plant testing was conducted to determine the ability of a well-designed activated sludge treatment system to remove chromic toxicity from the bleached kraft pulp mill effluent. Removals of conventional(BOD and SS) and nonconventional(resin and fatty acids, color, AOX) pollutants were estimated. The pilot plant was operated at steady state for about 10 weeks at an F/M of 0.28 and a sludge age of 8.4 days. The average MLSS concentration was 4,309mg/l, of which volatile fraction was 57%. During the operation period, the BOD removal reaction rate(k) was determined to be 8.2/day at $30^{\circ}C$. The BOD removal was 84 percent, which was 3 to 6 percent lower than expected for full-scale treatment. The chronic toxicity of the activated sludge effluent was tested by employing both Dinnel and the BML protocols. It was found that the pilot plant could achieve in excess of 90 percent reduction in chronic echinoderm toxicity. The data show slight reduction of color and AOX across the activated sludge system. The pilot system, however, demonstrated on excellent removal of resin and fatty acids.

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Removal of VOC compounds in the vent of a pharmaceutical plant using a pilot-scale biofilter (Pilot-scale 바이오필터를 이용한 제약공정 배출가스의 처리)

  • Ryu, Hee-Wook;Lee, Tae-Ho;Park, Chang-Ho
    • KSBB Journal
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    • v.23 no.6
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    • pp.470-473
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    • 2008
  • A pilot-plant biofilter ($1750\;m\;W{\times}2750\;mm\;L{\times}2000\;mm\;H$) packed with polyurethane foam ($20\;m\;W{\times}20\;mm\;L{\times}20\;mm\;H$) was installed in an pharmaceutical plant emitting gas streams containing n-hexane and alcohols. The biofilter was successfully operated for 74 days under highly fluctuating incoming concentrations at a residence time of 12.8-24.8 sec. Alcohols and n-hexane were removed by more than 90% from 5 and 20 days after start up, respectively. Malodor was also removed more than 95% from 20 days after start up.

The Remodelling of Hydraulic Structure in a Distribution Channel for Improving the Equality of the Flow Distribution (II): Optimization through Wet Tests (수리구조 개선을 통한 분배수로 균등분배 성능 향상에 관한 연구(II): Pilot plant 실험을 통한 최적화)

  • Park, No-Suk;Kim, Seong-Su;Hwang, Jun-Sick;Im, Jae-Rim;Kim, Chung-Hwan
    • Journal of Korean Society of Water and Wastewater
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    • v.21 no.5
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    • pp.581-587
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    • 2007
  • In order to suggest the methodology for improving the equality of flow distribution in a distribution channel, wet tests were carried out for pilot plant which was scaled down to 1/8 of full scale distribution channel being operated in domestic K_water treatment plant. The correlation between various hydraulic variables and their effects on the equality of flow distribution was evaluated through wet tests using pilot plant. From the results of wet tests, the longitudinal baffle with orifices was installed in the distribution channel, the equality of flow distribution was improved on the condition that the Froude number in pilot plant was similar with that in the full scale channel. Also, the opening ratio of the orifices on the longitudinal baffled did not have influence on the performance of the equality of flow distribution when the average flow velocity and Froud number were relatively low (Froude number ${\fallingdotseq} 0.01$). In the other hand, the performance of the equality of flow distribution was improved with increasing the opening ration of on the longitudinal baffle under conditions of relatively high average flow velocity and high Froud number(${\gtrsim}0.1$)

A Study on Removal of Organics, Nitrogen and Phoschorus of Domestic Wastewater in Pilot-Scale Upflow Packed Bed Column Reactor (Pilot 규모의 상향류식 충전탑 반응기를 이용한 생활오수의 유기물 및 질소, 인 처리에 관한 연구)

  • Seon, Yong-Ho
    • KSBB Journal
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    • v.22 no.4
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    • pp.191-196
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    • 2007
  • This study used biofilm process, which needs simple operation, maintenance and smaller facility area than conventional activated sludge process with the small plant operation, in the treatment of increasing sewage with the rapid industrial growth. The reactor used in this study consists of one anaerobic and one aerobic chamber filled with waste ceramic and waste vinyl as media and the treated sewage was from restaurant source. The experiment was scaled up from lab. to pilot scale and lasted for about 100 days. We focused on the removal efficiency of organics, nitrogen and phosphorus with constant HRT and continuous aeration. The removal efficiency of $BOD_5$ and SS were 94.33% and 87.77% respectively, which was a satisfaction level. However the removal efficiency of $COD_{Cr}$ was 81.46% somewhat below the desired level of 90%, and that of T-N and T-P showed 71.92% and 21.10% respectively, that was below the expected value. The removal efficiency of $COD_{Cr}$ and T-N in the pilot scale was about 10% low compared with the lab.-scale.

Treatment of gas from the vent of a fine chemical plant using a pilot-scale biofilter (파일럿 규모 바이오필터를 이용한 정밀화학공장 배출가스의 처리)

  • Ryu, Hee-Wook;Lee, Tae-Ho;Park, Chang-Ho
    • KSBB Journal
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    • v.24 no.1
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    • pp.47-52
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    • 2009
  • A pilot-plant biofilter (1750 mm W ${\times}$ 2750 mm L ${\times}$ 2000 mm H) packed with polyurethane foam (20 mm W ${\times}$ 20 mm L ${\times}$ 20 mm H) was installed in an fine chemical plant emitting gas streams containing ethyl alcohol, ethyl acetate, and dichloromethane. The biofilter was successfully operated for 30 days under highly fluctuating incoming concentrations (maximum 3500 ppm) at a residence time of 36 and 60 sec. Both ethyl alcohol and ethyl acetate were removed more than 95%, but dichloromethane removal was less than 50%. Malodor was also removed more than 90% from 17 days after start up.

Development of High-rate Nitrogen Removal Process Using Submerged MBR Packed with Granular Sulfur of Pilot Scale Plant (Pilot Scale Plant의 황 충진 MBR을 이용한 고효율의 질소제거 공법 개발)

  • Mun, Jin-Yeong;Hwang, Yong-U;Jo, Hyeon-Jeong
    • Journal of Korean Society of Water and Wastewater
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    • v.25 no.3
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    • pp.383-390
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    • 2011
  • In this study, a process combined biofiltration with sulfur-utilizing autotrophic denitrification and membrane separation was proposed to examine the efficiency of nitrogen removal. As an experimental device, hollow-fiber module was installed in the center of reactor to generate the flux forward sulfur layer in the cylinder packed with granular sulfur. In addition, a simple module was installed in activated sludge aeration tank which inside and outside of sulfur-using denitrification module was covered with microfilter and the module was considered as an alternative of clarifier. The experiment for developing new MBR process was carried out for three years totally. As the results of first two-year experiment, successful nitrogen removal performance was revealed with lab-scale test and pliot scale plant using artificial wastewater and actual plating wastewater. In this year, pilot scale test using actual domestic wastewater was performed to prove field applicability. As the results, high-rate nitrogen removal performance was confirmed with about 0.19 kg ${NO_3}^--N/m^3$ day of rate. Also significant fouling and pressure increase were not found during the experiment. And, the production ratio of sulfate and the consumption ratio of alkalinity showed a slightly higher value about 311 mg ${SO_4}^{2-}/L$ and 369 mg $CaCO_3$/L, respectively. In conclusion, the developed MBR process can be utilized as an alternative for retrofiting existing wastewater plants as well as new construction of advanced sewage wastewater treatment plants, with cost-effective merit.

Complex odor removal in pilot-scale biofilter with microorganisms immobilized on polymer gel media (미생물 포괄고정화 담체를 적용한 파일럿 스케일 바이오필터에서의 복합악취 제거)

  • Kim, Sun-Jin;Kim, Tae-Hyeong;Lee, Yun-Hee;Jang, Hyun-Sup;Song, Ji-Hyeon;Hwang, Sun-Jin
    • Journal of Korean Society of Water and Wastewater
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    • v.25 no.5
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    • pp.741-750
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    • 2011
  • A pilot-scale biofilter was constructed to discover degradation characteristics of the complex odor discharged from Ansan wastewater treatment plant. Candida tropicalis for volatile organic compounds, sulfur oxidizing bacteria(SOB) for hydrogen sulfide, and bacteria extracted from feces soil were immobilized on a polymer gel media. According to this study, the EBCT was varied from 36 sec to 18 sec. Toluene was removed as 80% along the variations, but it was recovered as 100% within 1 week. All benzene and xylene were removed during the operation while the efficiency of hydrogen sulfur was temporary decreased at 18 sec of EBCT, thereafter it was recovered to 100% within a week. The maximum elimination capacities of the benzene, toluene, xylene, and hydrogen sulfur were 6.6 g/$m^{3}$/hr, 31.7 g/$m^{3}$/hr, 7.8 g/$m^{3}$/hr, and 133.6 g/$m^{3}$/hr, respectively. There were merits on removal both organic and inorganic complex odor using the pilot-scale biofilter embedded with microorganisms immobilized on polymer gel media.