• Title/Summary/Keyword: in-reactor performance

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Performance of Upflow Anaerobic Sludge Blanket (UASB) Reactor Depending on Reactor Configuration and Sludge Bed Fluidization (반응조 형태 및 슬러지층 유동화 특성에 따른 Upflow Anaerobic Sludge Blanket (UASB) 반응조의 운전효율)

  • Jeong Byung-Gon
    • Journal of Environmental Health Sciences
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    • v.32 no.2 s.89
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    • pp.179-185
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    • 2006
  • Effect of organic loading rate on UASB performance was evaluated under the renditions of some surface area/reactor volume ratio and different reactor diameter. At the low leading rate of 0.4 kg $COD/m^3{\cdot}d$, reactor performance was not affected by reactor diameter. At the organic loading rate of 6 kg $COD/m^3{\cdot}d$, however, volatile acid accumulation and low COD removal efficiency is observed in reactor having 6.4 cm diameter, while volatile acid is not accumulated at all and high COD removal efficiency is observed in reactor having 3 cm diameter. Such a difference of reactor performance depending on reactor diameter can be explained that sludge bed can be fluidized by evolved gas bubble in narrow reactor, while sludge bed ran not be fluidized by evolved gas bubble only in wide reactor. At a high organic loading rate of 20 kg $COD/m^3{\cdot}d$, it can be judged that there is no relation between reactor configuration and reactor performance because all reactors showed very low COD removal efficiencies regardless of reactor diameter. Narrow and tall type reactor is favorable condition for making sludge bed fluidization at a constant surface area/reactor volume ratio. Thus, it can be judged that reactor configuration and sludge bed fluidization have great influence to reactor performance.

Hydraulic performance and flow resistance tests of various hydraulic parts for optimal design of a reactor coolant pump for a small modular reactor

  • Byeonggeon Bae;Jaeho Jung;Je Yong Yu
    • Nuclear Engineering and Technology
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    • v.55 no.3
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    • pp.1181-1190
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    • 2023
  • Hydraulic performance and flow resistance tests were performed to confirm the main parameters of the hydraulic instrumentation that can affect the pump performance of the reactor coolant pump. The flow resistance test offers important experimental data, which are necessary to predict the behavior of the primary coolant when the circulation of the reactor coolant pump is stopped. Moreover, the shape of the hydraulic section of the pump, which was considered in the test, was prepared to compare the mixed-flow- and axial-flow-type models, the difference in the number of blades of the impeller and diffuser, the difference in the shape of the impeller blade and its thickness, and the effect of coating at the suction bell. Additionally, five models of the hydraulic part were manufactured for the experiments. In this study, the differences in performance owing to the design factors were confirmed through the experimental results.

Simultaneous Removal of Carbon and Ammonia Nitrogen from Recirculation Water in High Density Seawater Aquaculture Farm (고밀도 해산어 양식장 순환수로부터 유기물 및 암모니아질소 동시 제거)

  • 정병곤;김문태;이헌모
    • Journal of environmental and Sanitary engineering
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    • v.18 no.1
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    • pp.15-22
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    • 2003
  • Treatability tests were conducted using EMC process to study the feasibility of applying this process as recycling-water treatment system in high density seawater aquaculture farm. To study the effect of organic and ammonia nitrogen loading on system performance, hydraulic retention time of reactor was reduced gradually from 12hr to 10min. The conclusions are can be summarized as follows. When the system HRT was reduced from 12hr to 10 min gradually, there was little noticeable change(reduction) in ammonia nitrogen removal efficiencies until 2hr of HRT, however, removal efficiencies were decreased dramatically when the system was operated under the HRT of less than 2hr. In case of organics(COD), there was no dramatic deterioration in removal efficiencies depending on HRT reduction. More than 90% of removal efficiencies were maintained successfully when the system was operated at the HRT of 10 min. In case of system performance depending on media packing ratio in reactor, there was little difference in each reactor performance depending on media packing ratio in reactor when the reactors were operated under the HRT of longer than 1hr, however, differences in reactor performances were considerably evident when the reactors were operated under the HRT of shorter than 1hr. That is, the more reactor was packed, the better reactor performed. When comparing reactor performance among 25%, 50%, 75% packed reactor, it can be judged that media packing ratio more than 50% plays no significant role in increasing reactor performance. For this reason, packing the media less than 50% is more reasonable way in view of economic. Such a tendency well agreed with the variation of ammonia-nitrogen removal efficiencies according to the media packing ratio in reactors at each HRT. Difference in effluent ammonia-nitrogen concentration between 50% media packing reactor and 75% media packing reactor was negligible. When comparing with the results of 25% packing reactor, difference was not so great.

Influence of design modification of control rod assembly for Prototype Generation IV Sodium-cooled Fast Reactor on drop performance

  • Son, Jin Gwan;Lee, Jae Han;Kim, Hoe Woong;Kim, Sung Kyun;Kim, Jong Bum
    • Nuclear Engineering and Technology
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    • v.51 no.3
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    • pp.922-929
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    • 2019
  • This paper presents the drop performance test of the control rod assembly which is one of the main components strongly related to the safety of the prototype generation IV sodium-cooled fast reactor. To investigate the drop performance, a real-sized control rod assembly that was recently modified based on the drop analysis results was newly fabricated, and several free drop tests under different flow rate conditions were carried out. Then the results were compared with those obtained from the previous tests conducted on the conceptually designed control rod assembly to demonstrate the improvement in performance. Moreover, the drop performance tests under several types and magnitudes of seismic loadings were also conducted to investigate the effect of the seismic loading on the drop performance of the modified control rod assembly. The results showed that the effects of the type and magnitude of the seismic loading on the drop performance of the modified control rod assembly were not significant. Also, the drop time requirement was successfully satisfied, even under the seismic loading conditions.

Anaerobic Digestion Fish Offal(I): Effect of Reactor Configuration and Sludge Bed Fluidization on Start-up of Digester (어류 폐기물의 혐기성소화 처리(I): 반응조 형상 및 슬러지층 유동화가 소화조 Start-up에 미치는 영향)

  • Jeong Byung-Gon;Kim Byung-Hyo
    • Journal of the Korean Society for Marine Environment & Energy
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    • v.9 no.2
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    • pp.72-78
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    • 2006
  • Effect of organic loading rate on digester performance was evaluated under the conditions of same surface area/reactor volume ratio and different reactor diameter. At the low loading rate of $0.4\;kg\;COD/m^3{\cdot}d$, high rate of organic removal could be obtained regardless of reactor diameter. It can be estimated that reactor configuration can not affect reactor performance at the low loading rate. However, different performance depending on reactor diameter was observed at the organic loading rate of $6\;kg\;COD/m^3{\cdot}d$. That is, volatile acid accumulation and low COD removal efficiency was observed in reactor having 6.4 cm diameter, while volatile acid was not accumulated at all and high COD removal efficiency was observed in reactor having 3 cm diameter. Such a difference of reactor performance depending on reactor diameter can be explained that sludge bed can be fluidized by evolved gas bubble in narrow reactor while sludge bed can not be fluidized by evolved gas bubble only in wide reactor. At a high organic loading rate of $20\;kg\;COD/m^3{\cdot}d$, it can be judged that there is no relation between reactor configuration and reactor performance because all reactors showed very low COD removal efficiencies regardless of reactor diameter. Sludge bed fluidization is one of the most important factors in achieving efficient start-up of anaerobic digester. Narrow and tall type reactor is favorable condition for making sludge bed fluidization at a constant surface area/reactor volume ratio. Thus, it can be judged that reactor configuration and sludge bed fluidization have great influence to reactor performance.

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Development of Reactor Vessel Head Penetration Performance Demonstration System in Korea (국내 원자로 상부헤드관통관 기량검증 기술개발)

  • Kim, Yongsik;Yoon, Byungsik;Yang, Seunghan
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.10 no.1
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    • pp.44-50
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    • 2014
  • There were many flaw issues of reactor vessel head penetration in USA fleets. USNRC issued 10CFR50.55a to implement reactor vessel head penetration ultrasonic examination performance demonstration(PD) in US for enhancement of inspection reliability. After September 2009, all US utilities inspected their RVHP with PD qualified system. Korea Hydro and Nuclear Power Company(KHNP) have developed reactor vessel head penetration performance demonstration system for ultrasonic test to apply for pressurized light-water reactor power plants in accordance with 10CFR50.55a since September 2011. RVHP configuration surveying and analysis, code requirement analysis, and performance demonstration specimen design were performed up to this day. Fingerprinting of manufactured specimen, development of test data management program, development of operation procedure, input of flawed data, and development of final report will be performed for the next step. This paper describes the development status of the performance demonstration system for reactor vessel head penetration ultrasonic examination in Korea.

Effect of Bioaugmentation on Performance of Intermittently Aerated Sewage Treatment Plant (Bioaugmentation이 간헐폭기 오수처리장치의 운전효율에 미치는 영향)

  • Jeong, Byung-Gon
    • Journal of Environmental Health Sciences
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    • v.34 no.3
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    • pp.233-239
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    • 2008
  • In order to improve reactor performance of existing sewage treatment plants, the feasibility of enhancing reactor performance by bioaugmentation using EM as bioaugmentation agent and the effects of anoxic: oxic time ratio on reactor performance were investigated. Continuous and intermittent aeration modes were compared under the 6 hr of HRT. Three different types of intermittent aeration modes, that is, 15 min, of anoxic:45 min of oxic, 30 min of anoxic: 30 min of oxic, and 45 min of anoxic: 15 min oxic respectively were chosen as test modes to study the effects of anoxic : oxic time ratios on reactor performance. The optimum anoxic: oxic time ratio was 30 min:30 min when considering simultaneous removal of organic, nitrogen and phosphorus. When applying EM into a continuously aerated reactor under the varying dosing rates of 50-200 ppm, reactor performance in terms of organic and nitrogen removal efficiencies was not improved at all. Nitrogen removal efficiency was increase when the EM dosing rate was increased. However the degree of improvement was slight when the EM was injected above 100 ppm. However optimum phosphorus removal was found at the EM dosing of 200 ppm. Thus it was found that optimum injection concentration of EM is 200 ppm. It is apparent that putting EM into a sewage treatment plant significantly affects the T-N removal efficiency of the reactor by enhancing denitrification efficiency especially in operational conditions of relatively long anoxic periods. To achieve reciprocal condition in a reactor with intermittent aeration it is necessary to enhance the reactor performance by EM injection. In the case of modifying existing continuously aerated reactors into intermittent aerated reactors, it is obvious that operating costs of aeration would be reduced by reducing aeration time when compared with existing conventional sewage treatment plants.

Drop Performance Test of Conceptually Designed Control Rod Assembly for Prototype Generation IV Sodium-Cooled Fast Reactor

  • Lee, Young-Kyu;Lee, Jae-Han;Kim, Hoe-Woong;Kim, Sung-Kyun;Kim, Jong-Bum
    • Nuclear Engineering and Technology
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    • v.49 no.4
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    • pp.855-864
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    • 2017
  • The control rod assembly controls reactor power by adjusting its position during normal operation and shuts down chain reactions by its free drop under scram conditions. Therefore, the drop performance of the control rod assembly is important for the safety of a nuclear reactor. In this study, the drop performance of the conceptually designed control rod assembly for the prototype generation IV sodium-cooled fast reactor that is being developed at the Korea Atomic Energy Research Institute as a next-generation nuclear reactor was experimentally investigated. For the performance test, the test facility and test procedure were established first, and several free drop performance tests of the control rod assembly under different flow rate conditions were then carried out. Moreover, performance tests under several types and magnitudes of seismic loading conditions were also conducted to investigate the effects of seismic loading on the drop performance of the control rod assembly. The drop time of the conceptually designed control rod assembly for 0% of the tentatively designed flow rate was measured to be 1.527 seconds, and this agrees well with the analytically calculated drop time. It was also observed that the effect of seismic loading on the drop time was not significant.

Evaluation for the Cooling Capability of Secondary Cooling Tower in HANARO (하나로 2차 냉각탑의 냉각능력 평가)

  • Park, Yong-Chul;Wu, Jong-Sup;Cho, Yeong-Gurb;Ryu, Jeong-Soo
    • 유체기계공업학회:학술대회논문집
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    • 2000.12a
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    • pp.345-350
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    • 2000
  • The heat produced by the fission in the fuel of HANARO, 30 MW research reactor, is transferred from the primary cooling water to the secondary cooling water through heat exchangers, and the heat absorbed by the secondary cooling water is released into the atmosphere by the 33 MW cooling tower which is a mechanical induced draft and counter flow type. If the outlet temperature of cooling tower exceeds 33 of due to the loss of the cooling tower performance under reactor operation above $50\%$ of the full power, the reactor power should be reduced to half of the full power for safe operation. Therefore, the cooling capability of cooling tower should be maintained for the reactor to be normally operated. To predict the capability of cooling tower for full power reactor operation of 30 MW, the performance test of cooling tower was done at the reactor present power of 24 MW and the capability was respectively evaluated by characteristics and performance curves methods in accordance with the Code of Cooling Tower Institute of U.S.A. to confirm the reliability of evaluation. As a result, it was confirmed, through the results of each evaluation, that the cooling capability of cooling tower meets the design required heat load. Also, the equations of the performance and the characteristics curves of the cooling tower, based on the collected data during this performance test, was obtained for developing the calculation program to predict the cooling capability during reactor operation.

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IRRADIATION TEST OF MOX FUEL IN THE HALDEN REACTOR AND THE ANALYSIS OF MEASURED DATA WITH THE FUEL PERFORMANCE CODE COSMOS

  • WIESENACK WOLFGANG;LEE BYUNG-HO;SOHN DONG-SEONG
    • Nuclear Engineering and Technology
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    • v.37 no.4
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    • pp.317-326
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    • 2005
  • The burning-out of excess plutonium from the reprocessing of spent nuclear fuel and from the dismantlement of nuclear weapons is recently emphasized due to the difficulties in securing the final repository for the spent fuel and the necessity to consume the ex-weapons plutonium. An irradiation test in the Halden reactor was launched by the OECD Halden Reactor Project (HRP) to investigate the in-pile behavior of plutonium-embedded fuel as a form of mixed oxide (MOX) and of inert matrix fuel (IMF). The first cycle of irradiation was successfully accomplished with good integrity of test fuel rods and without any undesirable fault of instrumentations. The test results revealed that the MOX fuel is more stable under irradiation environments than IMF. In addition, MOX fuel shows lower thermal resistance due to its better thermal conductivity than IMF. The on-line measured in-pile performance data of attrition milled MOX fuel are used in the analysis of the in-pile performance of the fuel with the fuel performance code, COSMOS. The COSMOS code has been developed for the analysis of MOX fuel as well as $UO_2$ fuel up to high burnup and showed good capability to analyze the in-reactor behavior of MOX fuel even with different instrumentation.