• Title/Summary/Keyword: casting defect

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Effect of Shrinkage Defect on Fracture Impact Energy of A356 Cast Aluminum Alloy (A356 알루미늄 합금의 파단 충격에너지에 대한 수축공결함의 영향)

  • Chul, Hwang-Seong;Kwak, Si-Young
    • Journal of Korea Foundry Society
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    • v.34 no.1
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    • pp.22-26
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    • 2014
  • Internal defects, such as shrinkage during casting, cause stress concentrations and initiate cracking. Therefore, it is important to understand the effects of internal defects on the mechanical properties including the impact behavior. This study evaluates the effects of internal casting defects on the impact performance of A356 Al-alloy castings. The internal shrinkage defects in the casting impact specimen are scanned using an industrial Computed Tomography (CT) scanner, and drop impact tests are performed with varing impact velocities on the A356 casting aluminium specimen ($10mm{\times}10mm$ section area) in order to locate the fracture energy under an impact load. The specimens with defects with a diameter less than 0.35 mm exhibit equivalent fracture impact energies of approximately 32 J and those with a 1.7 mm diameter defect reduced the fracture impact energy by 35%.

Effect of Critical Cooling Rate for Minimization of Porosity in the Thick Aluminum Casting (후육 Al 주조재의 기포결함 최소화를 위한 임계냉각속도의 영향)

  • Kwak, Si-Young;Cho, In-Sung;Kim, Yong-Hyun;Lee, Hee-Kwon
    • Journal of Korea Foundry Society
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    • v.37 no.6
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    • pp.181-185
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    • 2017
  • In the present study, the effect of cooling rate on the formation of the porosity in the thick aluminum sand casting was investigated. Nowadays, due to considerations of weight and cost reduction, large scale thick aluminum casting has replaces steel frames for vacuum chambers for semiconductor production. Several thick aluminum castings were manufactured using chill with temperature measurements. The castings were inspected using 3D computed tomography in order to quantify the porosity defect density in the castings. Effects of the thickness of the chill on the porosity defect density were discussed.

Utilization of 3D CAD and 3D Printer and UV Curavle resin Casting Defect (3D CAD, 3D 프린터 활용과 광경화수지 주물 결함)

  • Ryu, Ki-Hyu;Seo, Jin-Hwan
    • Journal of the Korea Convergence Society
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    • v.8 no.3
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    • pp.169-176
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    • 2017
  • Casting process includes wax pattern, investment, dewaxing, curing, casting, etc., and each single process is important to achieve a good result. Since 2000, 3D printers have been developed and widely used; as more prefer UV Curavle resin method over wax method, resultant casting defects have become worse. To resolve such problem, preceding research revealed casting defects of existing wax method. In particular, defects of UV Curavle resin method showed difference in investment, dewaxing, deresinating and curing compared to the existing one. Accordingly, results were presented through casting tests; especially, a temperature rising curve only for UV Curavle resin was shown rather than one for the existing method. Lastly, this research classified those not available with direct casting and suggested mold manufacturing. This research is expected to be useful for 3D printer users or those who would conduct direct casting with UV Curavle resin.

A study on the Horizontal Continuous Casting by Horizontal Continuous Casting Machine of Al-xSi(x=10-15%) Aluminum Alloy (수평식 연속주조 시스템을 이용한 Al-xSi(x=10-15%)합금 수평연주에 관한 연구)

  • Seo, Heesik;Ha, Sangbaek
    • Journal of the Korean Society of Industry Convergence
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    • v.17 no.3
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    • pp.122-135
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    • 2014
  • This paper was studied on the horizontal continuous casting of Al-xSi(x=10~15%) aluminum alloy. The experiments of the horizontal continuous casting was carried out by the horizontal continuous casting machine for various casting conditions and investigated on fracture types and mechanisms. Surface defect types for the horizontal continuous casting is also investigated. And the study was carried out that the horizontal continuous casting conditions such as casting temperature, cooling rate, and drawing speed affect the hardness and primary silicon size of Al-xSi(x=10~15%) aluminum rod bar. Casting temperature within this experiment conditions don't affect on the hardness of rod bar but the higher casting temperature is the smaller primary silicon size. The higher cooling rate and drawing speed have the higher hardness and the smaller primary silicon size.

Internal Defect Minimization of Die Cast Impeller Blade Using Taguchi's Design of Experiment (다구치 실험계획법을 이용한 임펠러 블레이드 다이캐스팅의 내부 결함 최소화)

  • Kim, D.;Choo, I.H.;Lee, Y.S.;Kim, S.W.
    • Transactions of Materials Processing
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    • v.19 no.3
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    • pp.173-178
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    • 2010
  • A die cast impeller blade has been developed in the effort on cost reduction in marine equipment industry. The purpose of this work is to optimize the die casting process using Taguchi's design of experiment for minimizing the internal defect of the die cast impeller blade. The experiments were preformed using the numerical simulation based on the L18 orthogonal array. As a results, the internal defect size of the die cast impeller blade for optimal design was controlled less than 1mm.

Effect of Casting Temperature and Speed on Formation of Surface Defect in Al-8Zn-2Mg-2Cu Billets Fabricated by Direct-Chill Casting Process (수직 연속주조 공정으로 제조된 Al-8Zn-2Mg-2Cu 빌렛의 표면 결함 형성에 미치는 주조 온도와 주조 속도의 영향)

  • Lee, Yoon-Ho;Kim, Yong-You;Lee, Sang-Hwa;Kim, Min-Seok;Euh, Kwangjun;Lee, Dong-Geun
    • Journal of Korea Foundry Society
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    • v.41 no.3
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    • pp.241-251
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    • 2021
  • 7000-series aluminum alloys are noted for their superior strength compared with other Al alloys, and their billets are generally fabricated by direct-chill (DC) casting. Surface defects in a DC-cast aluminum billet are mainly related to exudation and the meniscus freezing phenomenon, which are influenced by alloy compositions, casting speed, and casting temperature. 7000-series aluminum alloys have a wide freezing range during solidification, which makes it easy for casting defects to occur. In this study, we investigated surface defect evolution in casting billets of Al-8Zn-2Mg-2Cu alloy fabricated by a DC casting process. The billets showed "wavy" or "dotted" surfaces. The wavy surface was formed by meniscus freezing at a lower casting speed (200 mm/min) and temperature (655 ℃). In the wavy surface, refined dendritic cells were observed in a concave region due to the constitutional supercooling caused by meniscus freezing. Meanwhile, at a higher casting temperature (675 ℃), the dotted surface was formed by pore formation. In the dotted surfaces in the billet formed at a high casting speed (230 mm/min), an exudation layer was formed by the high metallostatic head pressure. The dotted region and the smooth region had a refined dendritic morphology and a columnar morphology at the exudation layer, respectively. This is attributed to the formation of gas pores in the dotted region.

Development of High Quality Die Casting Technology with Function to Purify Molten Metal (용탕청정기능을 부여한 고품질 다이캐스팅 기술의 개발)

  • Hatano, Tomoyuki;Takagi, Hiromi;Inagaki, Mitsugi
    • Journal of Korea Foundry Society
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    • v.24 no.1
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    • pp.3-9
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    • 2004
  • Die casting is "a process in which molten metal is injected at high velocity and pressure into a mold(die) cavity". Casting with smooth surfaces, high dimensional precision, complicated shapes, and reduced weight can be obtained using this process. But this process is susceptible to casting defects such as porosities, scattered chilled layers, hard spots, etc. For preventing casting defects, we developed "low-velocity high pressure die casting technology", "squeeze die casting technology", "heat insulating sleeve lubricant technology", and "direct pouring technology". The "direct pouring technology" is useful for producing molten metal without oxide contamination. It consists of a pumping system which supplies pure molten metal to the die casting machine. By using this technology, we have successfully reduced oxide contamination in castings to 1/20 of that of our previous castings.

Flow Characteristic of Hybrid-Lower Arm on Casting Parameters in Rheocasting Process (하이브리드 로워암 반응고 사출시 주조변수에 따른 레오캐스팅 충진거동에 대한 연구)

  • Moon, Jun-Young;Kim, Hae-Soo;Lee, Jong-Hyun;Sim, Jae-Gi;Kim, Jae-Min;Jung, Myung-Hwa;Roh, Seung-Kang;Kim, Kang-Wuk;Hong, Chun-Pyo
    • Journal of Korea Foundry Society
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    • v.28 no.5
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    • pp.231-236
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    • 2008
  • H-NCM(Hong-Nanocast Method)has several benefits such as a lower porosity defect and high quality casting comparing to conventional die casting. Influence of casting parameters of hybrid-lower arm in rheocasting process on the slurry flow and the amount of porosity defect was investigated using experimental and simulation methods. In the present study, the Carreau model was adopted to simulate the pattern of rheological flow. Optimal casting paremeters such as injection speed and stroke variations were established. Sound products with integral microstructure and sound shape of joinning different materials of Al and steel pipe without deforming the steel pipe were obtained by the H-NCM slurry and X-ray analysis also showed integral condition throughout the entire parts.

A study on structure of feed sprue considering turbulence and mold temperature in the investment casting process (Investment casting 공정에서 수축률을 고려한 소형탕도의 이상적인 구조와 주형 온도에 관한 연구)

  • Lee, Jong-Rae
    • Journal of the Korean Crystal Growth and Crystal Technology
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    • v.32 no.1
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    • pp.25-32
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    • 2022
  • Investment casting is a production method commonly used to manufacture precision equipment, medical fields, and accessories, and has continued to develop through the modernization of equipment and high quality of materials, and its scope of use has been expanded. The purpose of this study is to minimize the defect rate by deriving structural improvement and standardization of mold temperature, which are key elements of the investment casting process, to minimize the defect rate. The scope of the study is limited to jewelry manufacturing casting processes suitable for understanding the structure and principles of small gate, and an experimental research is to be conducted by using soft Wax, gypsum powder, and 14 K gold as research materials. According to the results, the most appropriate casting standard temperature for the casting pattern of Alloy 14 k was the lowest turbulence at 980℃ flask temperature of 550℃, so good products could be produced. As a future task of this study, detailed studies are needed to data the structure and system temperature of small gate, reduce production defects in the field, and provide data for excellent investment casting competitiveness.

Optimization of the Thin-walled Aluminum Die Casting Die Design by Solidification Simulation (응고 시뮬레이션에 의한 박육 알루미늄 다이캐스팅 금형 방안의 최적화)

  • Kim, Young-Chan;Cho, Se-Weon;Cho, Jae-Ik;Jeong, Chang-Yeol;Kang, Chang-Seog
    • Journal of Korea Foundry Society
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    • v.28 no.4
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    • pp.190-194
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    • 2008
  • Thin-walled die casting of aluminum notebook computer housing with less than 1mm thickness was investigated by using computational solidification simulation and actual casting experiment. Three different types of gate design, finger, tangential and split type, were used and the results showed that sound thin-walled die casting was possible with tangential and split type gating design because those gates allowed aluminum melt flowed into the thin-wall cavity uniformly and split type gating system was preferable gating design than tangential type at the point of view of soundness of casting and distortion generated after solidification. Also, solidification simulation agreed well with the actual die-casting and the casting showed no casting defect and distortion.