• Title/Summary/Keyword: Zr Propellant

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Storability and Material Compatibility Test of Blended Hydrogen Peroxide Propellant (블렌딩 기법을 적용한 과산화수소 추진제의 저장성 및 재료 적합성 평가)

  • Lee, Jeong-Sub;Jang, Dong-Wuk;Kwon, Se-Jin
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.11a
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    • pp.150-158
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    • 2011
  • Blending method was applied to increase the performance of hydrogen peroxide which is called green propellant. 90 wt.% hydrogen peroxide was blended with ethanol which is less toxic fuel, and there was no storability decrease due to fuel addition. Inconel X750 and Tophet A showed good compatibility and high heat resistance, and SUS 316L was compatible. Al2O3, Y2O3, and ZrO2, were coated on the material to improve heat resistance, and it was proved from endurance test that Y2O3 coating is not suitable and adhesive strength between coating and material is related with allowable temperature of material. Thruster test was performed to confirm the performance increase by blending method, and chamber temperature was $870^{\circ}C$ which is higher than $760^{\circ}C$ that is adiabatic chamber temperature of 90 wt.% hydrogen peroxide.

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Development of the Drive-away Motor for Cold Launch System (저온 사출장치용 이탈모타 개발)

  • Baek, Gook-Hyun;Oh, Jong-Yun;Lee, Young-Won;Lee, Ji-Hyung;Jung, Jin-Suk
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.11a
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    • pp.369-374
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    • 2011
  • To solve the combustion instability, especially chuffing phenomena, happened during development process of the drive-away motor that was required for cold launch system of missile, we tried various technical approaches and performed ground firing tests. The supplying content or method of ignition energy, generally that is deeply related with the chuffing phenomena, does not affect suppression of the chuffing, but the addition of 2% ZrC as a damping material is effective to suppress the chuffing. Therefore we could newly experience a special solution of the combustion instability in double base propellant.

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Development of the Drive-away Motor for Cold Launch System (저온 사출장치용 이탈모타 개발)

  • Baek, Gook-Hyun;Oh, Jong-Yun;Lee, Young-Won;Lee, Ji-Hyung;Jung, Jin-Suk
    • Journal of the Korean Society of Propulsion Engineers
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    • v.16 no.4
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    • pp.93-98
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    • 2012
  • To solve the combustion instability, especially chuffing phenomena, happened during development process of a drive-away motor that was required for cold launch system of missile, various technical approaches have been performed through ground firing tests. The ignition energy or its supply system, generally closely related with the chuffing phenomena, does not affect suppression of the chuffing, but the increase of characteristic length($L^*$) as well as the addition of 2% ZrC as a damping material is effective to suppress the chuffing. Therefore we could have a typical experience on the combustion instability in double base propellant.