• Title/Summary/Keyword: Venturi Injector

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Study of Flow Characteristics of Gel Propellant through Various Injector Geometries (인젝터 형상 변화에 따른 Gel 추진제의 유동 특성 연구)

  • Oh, Jeong-Su;Jeon, Doo-Sung;Choi, Sang-Tae;Kim, Deok-Yoon;Choi, Yang-Ho;Lee, Jeong-Hyuk;Moon, Hee-Jang
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.300-303
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    • 2010
  • The present study investigates the flow characteristics of simulant gel propellant(carbopol 0.5%wt) in a variety of injectors. Rheological data for gel propellant has been measured and injector flow characteristics for plain-orifice, chamfered-orifice and venturi type injector have been numerically analyzed. The apparent viscosity of plain-orifice and chamfered-orifice have tendency to increase along axial direction, whereas for venturi type injector, low viscosity has been achieved in the injector flow. This phenomenon was clearly pronounced as Reynolds number is increased.

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Design of Venturi Dump Surface for Pre-filming Airblast Injector (예막 공기충돌형 분사기의 벤추리 덤프면 설계)

  • Shin, Dongsoo;Choi, Myunghwan;Radhakrishnan, Kanmaniraja;Koo, Jaye;Jung, Seungchai
    • Journal of the Korean Society of Propulsion Engineers
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    • v.22 no.4
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    • pp.44-54
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    • 2018
  • In a spray experiment using a venturi mounted on a lean premixed LPP injector, droplets appear to have non-uniform distributions. To solve this problem, the exit angle of the venturi was changed to form a dump surface on the nozzle neck. The dump surface improved the atomization performance and minimized droplet loss while forming recirculation zone in the venturi exit. In order to solve the non-uniform spray of the injector, the flow characteristics inside the venturi and SMD of the spray are compared. Finally, an optimum venturi shape is selected to minimize the spray loss and improve the spray performance.

A Study on the Flow Control for Stable Combustion of Liquid Rocket (액체로켓의 연소안정을 위한 유량공급에 관한 실험적 연구)

  • Park, Hee-Ho;Kim, Yoo;Cho, Nam-Choon;Keum, Young-Tag
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.26 no.6
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    • pp.788-794
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    • 2002
  • In liquid rocket engine, propellant feed rate is proportional to approximately square root of the pressure difference between injector head and combustion chamber. This ΔP depends on the engine design, but in general on the order of 50psi. However, during ignition period, especially for the pressurized feed system, combustion chamber pressure is almost atmospheric and large ΔP causes over flow of propellants which may lead to catastrophic accident due to hard start. Hard start may be prevented by applying cavitating venturi or/and two step ignition. In cavitating venturi, evaporated propellants near the venturi throat become chocked and flow rate depends on only upstream condition. In two step ignition propellants are supplied to the liquid engine in two different flow rate. First step, to avoid hard start, small amount of propellants are supplied to build up chamber pressure in safe zone, then full propellants to ensure design pressure. In this study, both cavitating venturi and two step ignition method were used for the hot test and hard start problem was completely solved.

Development of Intelligent IoT Exhaustion System for Bag Filter Collector (백필터 집진기의 지능형 IoT 탈진 시스템 개발)

  • Jang, Sung-Cheol;Lee, Jung-Won
    • Journal of Internet of Things and Convergence
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    • v.5 no.1
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    • pp.29-34
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    • 2019
  • A bag filter collector is a kind of air purifier that organizes several or dozens of filters to purify fine dust and release clean air into the atmosphere. If the bag filter length is less than 5m, the dust and fume attached to the bag filter could be effectively removed by passing the compressed air generated by the diaphragm valve through the venturi. Injectors that are more efficient and economical are urgently needed to achieve satisfactory results for long-bag exhaustion of more than 7 meters. In the case of existing domestic and foreign injectors, a number of blow tubes were dismantled during maintenance, and the injector and blow tube were combined to pose a number of problems, including inconvenience of work due to weight increase. In this study, injector flow for the development of the best use of interpretation of the coanda effect and the fourth round of industrial technology Intelligent automation of exhaustion, have been engineered energy than standard equipment. lowering costs and filter life to radically improve the commercial studies.

CFD simulation of a prefilming air blast fuel nozzle (Prefilming air blast 연료 노즐의 다상유동 및 반응 유동장 수치해석)

  • Jung, Seungchai;Kim, Shaun;Park, Heeho;Ryu, Shiyang
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2017.05a
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    • pp.251-253
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    • 2017
  • Numerical study of air-blast type injector for low emission aircraft engines was conducted. Volume-of-fluids approach was used to track interface of fuel and air. Primary atomization of fuel stream was visualized, and thickness and mean velocity at the injector exit was calculated. Liquid fuel injected from fuel slots joined together as a thin film on preflimer surface, and interacted with swirling air. As instability on the fuel surface increased, separation of fuel as ligaments and droplets occured. The film thickness and velocity were used to as fuel injection boundary condition for reactive flow simulation. Primary reaction zone was formed in vicinity of the fuel nozzle, creating a stable flame inside the combustor.

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A Study on the Design of High-Frequency Jet Ventilator Using PLL system (위상동기루프 방식을 이용한 고빈도 JET환기장치의 설계에 관한 연구)

  • Lee, Joon-Ha;Chung, Jae-Chun
    • Journal of Yeungnam Medical Science
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    • v.6 no.2
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    • pp.63-70
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    • 1989
  • This paper describes to design and to examine the mechanical characteristics of high frequency jet ventilator. The device consists of Phase lock loop(PLL) system, solenoid valve driving control part and Air regulating system. This study is carried out by changing several factors such as endotracheal tube(E.T. tube)diameter, injector cannula diameter, 1%, and frequency(breaths/mim.) having direct effects on the gas exchange as well as parameters of the entrained gas by venturi effects, so as to measure the tidal volume and minute volume. This system characteristics were as follows : 1) Frequency : 6-594bpm 2) Inspiration time : 1-99% 3) Variance of input air pressure : 1-30PSI.

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Investigation about the Decrease Efficiency of Thermal Discharge Temperature at Mixing Basin of Power Plant using 3-D CFD (3차원 수치모의에 의한 발전소 배수로 혼합지에서의 온배수 수온저감 효과에 대한 고찰)

  • Park, Byong-Jun;Lee, Sang-Hwa;Park, Ji-Sung
    • Proceedings of the Korea Water Resources Association Conference
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    • 2012.05a
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    • pp.593-593
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    • 2012
  • 본 연구는 화력 및 원자력 발전소로 취입된 냉각수(circulating and essential service water)가 복수기로부터 온배수 형태의 개수로 흐름으로 표층배수 될 경우 수온을 저감시키기 위해 주입하는 희석수(by-pass cooling water)와의 혼합효과의 효율성을 증대시키고, 불리한 수리현상을 야기하지 않으며, 경제적인 배수로 구조물을 고찰하기 위한 목적으로 시도되었다. 배수로 구조물 내 온배수와 희석수가 혼합되는 구간을 혼합지(mixing basin)라 하는데, 본 과업에서는 ${\bigcirc}{\bigcirc}$발전소의 배수로 구간 중 혼합지를 대상으로 FLOW-3D$^{(R)}$를 이용한 3차원 수치모형을 구축하고, 총 9개에 해당하는 각 대안별 현상을 분석하고 비교하였다. 각 대안들의 차이점은 배수로에 설치되는 보조구조물들의 형상과 배열 등이며, 복수기로부터 나오는 배출수의 수온은 $42^{\circ}C$, 희석수는 $35^{\circ}C$이고, 본 과업의 주요 관심대상 물리량은 유속과 온도이다. 배수로에 아무런 보조 구조물이 없는 형태인 기본 계획안을 검토한 결과, 평균 $3.31^{\circ}C$의 수온강하가 이루어졌으나, 우안 쪽으로 강한 흐름이 발생하여 수온의 좌우편차가 $4.61^{\circ}C$ 가량 발생하는 것으로 나타났다. 기본 계획안의 검토결과를 보완하기 위한 대안으로 연직 흐름의 소산을 위해 고안된 잠형 소파블록(baffle block) 설치안은 평균 $3.06^{\circ}C$의 수온강하가 이루어지고 $4.44^{\circ}C$의 수온 좌우편차가 발생했다. 지그재그(zigzag) 형태의 흐름을 만들어 혼합효과를 올리기 위한 미로형 수제(labyrinth groin) 설치안은 평균 $5.33^{\circ}C$의 수온강하가 이루어지고, $1.43^{\circ}C$의 수온 좌우편차를 보여줘 검토했던 대안들 중 가장 좋은 결과를 보여주었다. V자 배열 소파블럭(deformed block) 설치안은 연직 및 수평방향의 소산을 기대했으나 평균 $3.00^{\circ}C$의 수온 강하와 $4.41^{\circ}C$의 수온 좌우편차를 나타냈다. 벤츄리(Venturi) 형태의 흐름을 발생시키기 위한 병목형(bottleneck) 수로안은 평균 $3.18^{\circ}C$의 수온강하와 $3.94^{\circ}C$의 수온 좌우편차, 흐름의 소산과 흐름방향을 변화시키기 위한 와형 수제(swirl groin) 설치안은 평균 $2.24^{\circ}C$의 수온강하와 $1.48^{\circ}C$의 수온좌우편차, 우안 흐름을 지연시키기 위한 물방석(water cushion) 수로안은 평균 $3.03^{\circ}C$의 수온강하와 $4.50^{\circ}C$의 수온 좌우편차, 우안의 흐름을 좌안으로 보내기 위한 분사형(injector) 수로안은 평균 $3.13^{\circ}C$의 수온강하와 $4.45^{\circ}C$의 수온 좌우편차, 우안의 흐름을 막기 위한 외팔형 수제(cantilever groin) 설치안은 평균 $3.11^{\circ}C$의 수온강하와 $3.02^{\circ}C$의 수온 좌우편차가 발생하는 것으로 나타났다.

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