• Title/Summary/Keyword: Turbo-Ring

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A Study on the Development of Marine Turbocharger Nozzle Ring using Investment Casting (인베스트먼트법을 이용한 선박용 대형 터보차져 노즐링 개발을 위한 연구)

  • Hwang, Seong Ju;Lee, Man Gil;Jung, Jin Wook;Kwon, Soon Kook;Lee, Choon Man
    • Journal of the Korean Society for Precision Engineering
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    • v.31 no.8
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    • pp.671-675
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    • 2014
  • Nozzle ring is an important part of turbocharger which is applied to today's most diesel engines. Turbo charger nozzle ring is difficult to process and takes a high cost and a long time relatively. For this reason, it is largely produced by using a precision casting. Investment method, the representative technology of precision casting, has excellent dimensional accuracy and can produce complex shapes relatively easily. However, it is difficult to avoid the casting defects such as shrinkage cavity and short shot. This study is to predict the casting defects which could be occurred during the investment method by use of finite element analysis software and to design the process and mold of the marine turbocharger nozzle ring.

Combustion Performance Tests of Fuel-Rich Gas Generator for Liquid Rocket Engine Using an Impinging Injector (충돌형 분사기 형태의 액체로켓엔진용 가스발생기 연소성능시험)

  • 한영민;김승한;문일윤;김홍집;김종규;설우석;이수용;권순탁;이창진
    • Journal of the Korean Society of Propulsion Engineers
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    • v.8 no.2
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    • pp.10-17
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    • 2004
  • The results of the combustion performance tests of gas generator which supplies hot gas into the turbine of turbo-pump for liquid rocket engine and uses LOx and kerosene as propellant are described. The gas generator consists of a injector head with F-O-F impinging injector, a water cooled combustion chamber, a gas torch igniter, a turbulence ring and an instrument ring. The effect of turbulence ring and combustion chamber length on performance of gas generator are investigated. The ignition and combustion at design point are stable and the pressure and gas temperature at gas generator exit meets the target. The turbulence ring installed at middle of chamber effectively mixes hot gas with cold gas and the effect of residence time of hot gas in gas generator on combustion efficiency is small. Test results show that the main parameter controlling the gas temperature at gas generator exit is overall O/F ratio.

A Study on Performance of a Variable-Speed Turboblower (가변속 고속블로워의 성능특성에 관한 연구)

  • Choi, Bum-Seog;Park, Moo-Ryong;Hwang, Soon-Chan;Park, Joon-Young
    • The KSFM Journal of Fluid Machinery
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    • v.7 no.5 s.26
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    • pp.43-49
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    • 2004
  • A turbo blower, driven by a high-speed blushless DC motor, was designed as a efficient substitute of a ring blower or a roots blower. Computational analysis and performance tests have been performed to investigate performance characteristics of the blower. Experimental measurements showed that the blower has a good stability margin. This paper gives an outline of design, computational flow analysis and performance test for aerodynamic evaluation of the variable speed turboblower.

An Experimental Analysis for System Optimization to Reduce Smoke at WOT with Low Volatile Fuel on Turbo GDI Engine (저 기화성 연료를 사용한 직접분사식 과급 가솔린엔진에서 전 부하 스모크 저감을 위한 시스템 최적화에 관한 연구)

  • Kim, Dowan;Lee, Sunghwan;Lim, Jongsuk;Lee, Seangwock
    • Transactions of the Korean Society of Automotive Engineers
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    • v.23 no.1
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    • pp.97-104
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    • 2015
  • This study is a part of the high pressure injection system development on the Turbo GDI engine in order to reduce smoke emission in case of using the low volatile(high DI) fuel which is used as normal gasoline fuel in the US market. Firstly, theoretical approach was done regarding gasoline fuel property, performance, definition of particle matters and its creation as well as problems of the high DI fuel. In this experimental study, 2L Turbo GDI engine was selected and optimized system parameter was inspected by changing fuel, fuel injection mode (single/multiple), fuel pressure, distance between injector tip and combustion chamber, start of injection, intake valve timing in engine dyno at all engine speed range with full load. In case of normal gasoline fuel, opacity was contained within 2% in all conditions. On the other hands, in case of low volatile fuel (high DI fuel), it was confirmed that the opacity was rapidly increased above 5,000 rpm at 14.5 ~ 20 MPa of fuel pressure and there were almost no differences on the opacity(smoke) between 17 MPa and 20 MPa fuel pressure. According to the SOI retard, smoke decrease tendency was observed but intake valve close timing change has almost no impact on the smoke level in this area. Consequently, smoke decrease was observed and 16% at 6000rpm respectively with injector washer ring installed. By removing injector washer to make injector tip closer to the combustion chamber, smoke decrease was observed by 46% at 5,500 rpm, 42% at 6,000 rpm. It is assumed that the fuel injection interaction with cylinder head, piston head, intake and exhaust valve is reduced so that impingement is reduced in local area.

A Development of Stem Analysis Program and its Comparison with other Method for Increment Calculation (수간석해(樹幹析解) 전산(電算)프로그램 개발(開發) 및 생장량(生長量) 계산방법(計算方法)의 비교(比較)에 관(關)한 연구(硏究))

  • Byun, Woo Hyuk;Lee, Woo Kyun;Yun, Kwang Bae
    • Journal of Korean Society of Forest Science
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    • v.79 no.1
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    • pp.1-15
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    • 1990
  • In this study the stem analysis program, which can be operated with personal computer was developed to reduce time and cost of calculation, and to increase accuracy of analysis. The stem analysis method used in this program was compared with other methods. The results obtained were as follows : The value, 1/100mm measured from the latest annual ring measurement machine (Jahrringme${\beta}$geraete Johan Type II) was automatically inputed to the computer and saved into given file name. Turbo Pascal program was written to do this. The measured data was analyzed by stem analysis calculation program written by Fortran-77. Volume and height increments were approximated by spline function, and diameter of the stem disk was calculated by quadratic mean method. The increment values calculated by the programs were printed annually and in every five-year. Stem analysis diagram and several increment graphs were also easily printed. The result compared between those analysis methods showed that quadratic mean could reduce the error caused from eccentric pith. When the stem taper curve method, approximated by spline function, was used in the calculation of tree height and volume, increments would be more exactly calculated.

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A Numerical Method & Experiments for the Aerodynamic Design of High Performance 2-Stage Axial Flow Fans (고성능 2단 축류송풍기의 공력설계를 위한 수치해석 및 실험에 관한 연구)

  • Cho, Jinsoo;Han, Cheolhui;Cho, Leesang
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.23 no.8
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    • pp.1048-1062
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    • 1999
  • A numerical method and experiments for the aerodynamic design of high performance two-stage axial flow fans was carried out. A vortex ring element method used for the aerodynamic analysis of the propellers was extended to the fan-duct system. Fan Performance and velocity profiles at the fan inlet and outlet are compared with experimental data for the validations of numerical method. Performance test was done based on KS B 6311(testing methods for turbo-fans and blowers). The velocity profile was obtained using a 5-hole pitot tube by the non-nulling method. The two stage axial flow fan configurations for the optimal operation conditions were set by using the experimental results for the single rotating axial flow fan and the single stage axial flow fan. The single rotating axial flow fan showed relatively low efficiency due to the swirl velocities behind rotor exit which produced pressure losses. In contrast, the single stage and the two-stage axial flow fans showed performance improvements due to the swirl velocity reduction by the stator. The peak efficiency of the two stage axial flow fan was improved by 21% and 6%, compared to the single rotating axial flow fan and the single stage axial flow fan, respectively.