• Title/Summary/Keyword: Running Bucket Test

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Running Bucket Vibration Test of Steam Turbines (증기 터빈 버킷의 회전 진동 시험)

  • 박종포;신언탁;김호종
    • Journal of KSNVE
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    • v.8 no.2
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    • pp.331-335
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    • 1998
  • A design modification was made on the 9-th stage wheel dovetail of a high-intermediate pressure (HIP) turbine rotor for a fossil power plant that necessitates the use of new long-shank buckets for the row. A bucket vibration test is necessary to verify that the new 9-th stage buckets have adequate frequency margin from a nozzle passing frequency when running at speed. A finite element analysis (FEA) has been performed using a commercial S/W to approximately estimate bucket natural frequencies, and thus to help the vibration test. A row of the new buckets has assembled on the HIP rotor for the vibration tests using dynamic balancing facilities. The tests have been done during deceleration run with air excitation. The test results are compared with the calculation using our empirical formula, and show that the modified design meets the frequency-margin requirements.

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Running Bucket Vibration Test of Steam Turbines (증기 터빈 버켓의 회전 진동 시험)

  • 박종포;신언탁;김호종
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 1997.10a
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    • pp.96-100
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    • 1997
  • A design modification was made on the 9-th stage wheel dovetail of a high-intermodiate pressure (HIP) turbine rotor for a fossil power plant that necessitates the use of new long-shank buckets for the row. A bucket vibration test is necessary to verify that the new 9-th stage buckets have adequate frequency margin from a nozzle passing frequency when running at speed. A finite element analysis (FEA) has been performed using a commercial S/W to approximately estimate bucket natural frequencies, and thus to help the vibration test. A row of the new buckets has been assembled on the HIP rotor for the vibration tests using dynamic balancing facilities. The tests have been done during deceleration run with air excitation. The test results are compared with the calculation using our empirical formula, and show that the modified design meets the frequency-margin requirements.

  • PDF