• Title/Summary/Keyword: Rotary Pump

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Volatility of Herbicides Sprayed in Zoysia japonica Turf and Bare Soil (잔디밭과 나지에 산포된 주요 잔디밭용 제초제의 휘산)

  • 김석정;박진희;죽내안지;김길웅;신동현;허영조
    • Asian Journal of Turfgrass Science
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    • v.10 no.3
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    • pp.263-270
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    • 1996
  • This experiment was conducted to investigate the loss of various herbicides by means of vola-tility from the turfgrass field and the hare ground with the different soil moisture contents and temperatures. Different herbicides were applied at the rates of 375 g a.i. /l0a of pendimethalin,250 g a.i. /l0a of napropamide, and 96.4 g a.i. /l0a of dicamba with 200 \ulcorner/10a of spray volume in the turfgrass(Zoysia japonica cut off 5cm) grown in pots(265.8 $cm^2$) and bared soil. The pots were placed in the growth chamber with 10,000 lux of light intensity(12h per day) at 25 and 35˚C for 7days. Amberlite XAD polymeric resin(20/50 mesh) was used as sampling media for herbicide airborne residues. Air flow was maintained at 10 \ulcorner /min by vacuum pump regulated with a factory calibrated flow meter. Herbicide airborne residues were extracted from the XAD resin with 300 ml of 1:1 acetone and hexane. The extracts were concentrated by rotary evaporation at 35˚C and dissolved in 1 ml MeCN for HPLC analysis. The airborne losses of the herbicide applied in the turfgrass and bare soil increased as the temperature and soil moisture contents were increased, regardless of the kinds of herbicide. Higher airborne residues was observed in the turfgrass pots than the bare soil pots. Pendimethalin and dicamba with higher vapor pressure gave rise to the increased loss of airborne herbicides, showing that 6.26 and 6.4% of average airborne loss in pendimethalin and dicamba, respectively, compared to 0.56% in napropamide. The amount of airborne losses in turfgrass was highest at one day after application and then a declined trend was observed as the time was prolonged. Key words. Herbicides, Turfgrass field, Bare ground, Volatility.

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Vacuum Safety

  • Ju, Jang-Heon
    • Vacuum Magazine
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    • v.2 no.2
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    • pp.49-58
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    • 2015
  • 진공 배기 시스템에 위험한 환경을 초래할 수 있는 모든 가능성을 찾아 낼 수는 없지만 누적된 현장 경험과 연구 결과에 맞추어 최대한 필요한 안전 조치들을 취해야 한다. 진공 배기 시스템이나 그 구성품들에 대한 심각한 파손을 유발하는 공통적인 요인들은 발화성 물질의 점화나 진공 배기 시스템의 배기구 막힘에 의해 발생한다. 따라서, 진공 펌프와 진공 시스템의 안전한 가동과 사용을 위해서는 다음과 같은 것들을 반드시 준수하여야 한다. ${\blacksquare}$ 발화성, 폭발성 공정 물질을 사용하는 진공 배기 시스템은 정규 유지 보수 작업(PM) 후 첫 번째 배기 과정은 매우 천천히 진행하여 진공 배기 시스템 내부에 급격한 난류가 형성되지 않도록 해 주어야 한다. ${\blacksquare}$ 진공 배기 시스템 내에서 발화성 물질들의 농도가 발화 영역(flammable zone, potentially explosive atmosphere)에 들어가지 않도록 하여야 한다. 이를 위해서는 불활성 가스를 이용하여 진공 펌프와 진공 배기 시스템의 가동 예상 조건이나 고장 환경하에서 안전한 농도 이하로 희석시켜야 한다. ${\blacksquare}$ 진공 펌프와 진공 배기 시스템에 장착되어 사용되는 밸브 등의 기계적 부품들이나 공정에 사용되는 물질과 공정 부산물들(by-products)로 인하여 배관, 필터 배기구 등이 막히지 않도록 하여야 한다. ${\blacksquare}$ 공정에 사용되는 물질들, 특히 산소($O_2$), 오존 ($O_3$) 등의 산화제 농도가 높을 때는 오일 회전 배인 진공 펌프(Oil rotary vane vacuum pump)에 미네랄(mineral) 오일을 사용하지 말아야 하며, PFPE(Perfluoropolyether) 오일을 사용하여야 한다. 시판되는 진공 펌프 오일 중 비발화성(non-flammable)으로 표기된 오일이라고 하더라도 산화제(oxidant)의 농도가 체적비로 30 % 넘는 공정 환경에는 사용하지 말아야 한다. ${\blacksquare}$ 진공 펌프와 진공 배기 시스템에 의해 배기되는 물질들이 물($H_2O$)과 격렬하게 반응하는 경우는 물이 아닌 다른 냉각제를 사용하여야 한다. ${\blacksquare}$ 안전하지 않다고 판단되는 상황에서는 해당 전문가의 조언이나 해당 전문가의 직접적인 현장 도움을 통해 문제를 해결하여야 한다.

Performance of R290 and R1270 as Alternative Refrigerants of R22 According to Temperature Variations of Evaporator and Condenser (증발기와 응축기 온도변화에 따른 R22 대체냉매 R290 및 R1270의 성능평가)

  • Baek In-Cheol;Park Ki-Jung;Shim Yun-Bo;Jung Dong-Soo
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.18 no.10
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    • pp.761-767
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    • 2006
  • In this study, performance of 2 pure hydrocarbons R290 and R1270 was measured in an attempt to substitute R22 under 3 different temperature conditions. They were tested in a refrigerating bench tester with a hermetic rotary compressor. The test bench provided about 3.5 kW capacity and water and water/glycol mixture were employed as the secondary heat transfer fluids. All tests were conducted under the same external conditions resulting in the average saturation temperatures of $7/45^{\circ}C$ and $-7/41^{\circ}C$ and $-21/28^{\circ}C$ in the evaporator and condenser, respectively. Test results show that the coefficient of performance (COP) of these refrigerants is up to 11.54% higher than that of R22 in all temperature conditions. Compressor discharge temperatures were reduced by $14{\sim}31^{\circ}C$ with these fluids. There was no problem with mineral oil since the mixtures were mainly composed of hydrocarbons. The amount of charge was reduced up to 58% as compared to R22. Overall, these fluids provide good performance with reasonable energy savings without any environmental problem and thus can be used as long term alternatives for residential air-conditioning and heat pumping application.

Performance Evaluation of R22 Alternative Refrigerants According to Temperature Variations of Evaporator and Condenser (증발기와 응축기 온도변화에 따른 R22 대체냉매의 성능평가)

  • Baek, In-Cheol;Shim, Yun-Bo;Jung, Dong-Soo
    • Proceedings of the SAREK Conference
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    • 2006.06a
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    • pp.58-63
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    • 2006
  • In this study, performance of 2 pure hydrocarbons and 3 mixtures was measured in an attempt to substitute R22 under 3 different temperature conditions. The mixtures were composed of R1270(propylene), R290(propane) and R152a. They were tested in a refrigerating bench tester with a hermetic rotary compressor The test bench provided about 3.5 kW capacity and water and water/glycol mixture were employed as the secondary heat transfer fluids. All tests were conducted under the same external conditions resulting in the average saturation temperatures of $7^{\circ}C/45^{\circ}C$ and $-7^{\circ}C/41^{\circ}C$ and $-21^{\circ}C/28^{\circ}C$ in the evaporator and condenser, respectively. Test results show that the coefficient of performance (COP) of these refrigerants is up to 11.54% higher than that of R22 in all temperature conditions. Compressor discharge temperatures were reduced by $14{\sim}31^{\circ}C$ with these fluids. There was no problem with mineral oil since the mixtures were mainly composed of hydrocarbons. The amount of charge was reduced up to 58% as compared to R22. Overall, these fluids provide good performance with reasonable energy savings without any environmental problem and thus can be used as long term alternatives for residential air-conditioning and heat pumping application.

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Research to Predict the Thermal Characteristics of Electro Hydrostatic Actuator for Aircraft (항공기용 전기-정유압식 작동기(Dual Redundant Asymmetric Tandem EHA)의 열특성 예측을 위한 연구)

  • Kim, Sang Seok;Park, Hyung Jun;Kim, Daeyeon;Kim, Dae Hyun;Kim, Sang Beom;Lee, Junwon;Choi, Jong Yoon
    • Journal of Aerospace System Engineering
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    • v.16 no.3
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    • pp.84-92
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    • 2022
  • The electro-hydrostatic actuator (EHA) recently has been used in flight control fields for aircraft because of its benefits of minimizing oil leakage and weight, improving safety, and etc. while independently operating the hydraulic power source and eliminating complex hydraulic piping. The aircraft of which EHA is installed inside, has the thermal management issue of EHA, because of its limited cooling source as compared with the aircraft which installs the traditional central hydraulic system. So, the thermal analysis model which predicts the thermal characteristics of EHA, is required to resolve this thermal management issue. In this study, an oil circulation circuit inside the hydraulic power module comprised of hydraulic pump and electrical motor for EHA was applied. This is for the purpose of developing the internal rotary group of hydraulic power module, which operates under the conditions of high rotation speed and hydraulic pressure. After formulating an appropriate thermal analysis model, the thermal analysis results with oil cooled or no oil cooled hydraulic control module were compared and reviewed, for the purpose of predicting the thermal characteristics of EHA.

Development of control system for complex microbial incubator (복합 미생물 배양기의 제어시스템 개발)

  • Hong-Jik Kim;Won-Bog Lee;Seung-Ho Lee
    • Journal of IKEEE
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    • v.27 no.1
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    • pp.122-126
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    • 2023
  • In this paper, a control system for a complex microbial incubator was proposed. The proposed control system consists of a control unit, a communication unit, a power supply unit, and a control system of the complex microbial incubator. The controller of the complex microbial incubator is designed and manufactured to convert analog signals and digital signals, and control signals of sensors such as displays using LCD panels, water level sensors, temperature sensors, and pH concentration sensors. The water level sensor used is designed and manufactured to enable accurate water level measurement by using the IR laser method with excellent linearity in order to solve the problem that existing water level sensors are difficult to measure due to foreign substances such as bubbles. The temperature sensor is designed and used so that it has high accuracy and no cumulative resistance error by measuring using the thermal resistance principle. The communication unit consists of two LAN ports and one RS-232 port, and is designed and manufactured to transmit signals such as LCD panel, PCT panel, and load cell controller used in the complex microbial incubator to the control unit. The power supply unit is designed and manufactured to supply power by configuring it with three voltage supply terminals such as 24V, 12V and 5V so that the control unit and communication unit can operate smoothly. The control system of the complex microbial incubator uses PLC to control sensor values such as pH concentration sensor, temperature sensor, and water level sensor, and the operation of circulation pump, circulation valve, rotary pump, and inverter load cell used for cultivation. In order to evaluate the performance of the control system of the proposed complex microbial incubator, the result of the experiment conducted by the accredited certification body showed that the range of water level measurement sensitivity was -0.41mm~1.59mm, and the range of change in water temperature was ±0.41℃, which is currently commercially available. It was confirmed that the product operates with better performance than the performance of the products. Therefore, the effectiveness of the control system of the complex microbial incubator proposed in this paper was demonstrated.