• 제목/요약/키워드: Power Plant Valve

검색결과 225건 처리시간 0.023초

원자력 발전소 배관계 글로브 밸브의 고주파 진동 원인 분석 및 해결 사례 (A Case Study of Root Cause Analyses and Remedies for High frequency Vibration of Globe Valve in Nuclear Power Plant Piping System)

  • 최병화;박수일;전창빈
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2005년도 추계학술대회논문집
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    • pp.394-399
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    • 2005
  • A case history is presented pertaining to high frequency piping vibration and noise caused by globe valve in the spent fuel pool cooling system of nuclear power plant. Frequency analyses were performed on the system to diagnose the problem and develop a solution to reduce the piping vibration and noise. The source of the high frequency and noise energy was traced to the globe valve located immediately downstream of the centrifugal pump by performing valve throttling test. Measurements of vibration and noise are presented to show that the high frequency vibration and noise amplitude was dependent upon the valve disc position and flow rate. Strouhal vortex shedding frequencies were generated at the exit of the globe valve which exited structural resonance of valve disc and amplified the high frequency vibration and noise. The problem was identified as an interaction between the flow inside globe valve and the valve disc structure. Attempts to reduce the vibration and noise amplitudes of the piping system were successfully achieved by the modification of guide-disc diameter and disc-edge figure The valve disc was replaced by an alternative to eliminate the source of the harmful high frequency vibration and noise.

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발전소내 긴 밸브 stem을 갖는 옥외 소화전의 파손 현상 규명 (Diagnosis for damage of fire hydrant with long valve stem in power plant.)

  • 손석만;이상국;이욱륜;이준신;김기태
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2007년도 춘계학술대회B
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    • pp.3512-3517
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    • 2007
  • Nuclear power plant has many external fire hydrants that have to operate in the state of emergency such as facility fire, forest fire. The valve stem of one among them was broken 3 times for 4 years. It had long valve stem and operated under high water pressure. The elongation and the tensile strength for the broken valve stem was measured to examine the defect of material property. And the vibration level and the natural frequencies was detected to check the resonance. As the result of a diagnosis, the cause of this fault is proven buckling of long valve stem.

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원자력 발전소 고압터빈의 교축여유(Throttle Margin) 최적화 연구 (Study on Optimization of Throttle Margin in High Pressure Turbine of Nuclear Power Plant)

  • 고우식
    • 동력기계공학회지
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    • 제14권4호
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    • pp.43-49
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    • 2010
  • In the present study, optimization of throttle margin for high pressure turbine to be retrofitted or partially modified for power uprating or life extension in nuclear power plant, has been performed to increase the electrical output. Throttle margin for high pressure turbine is required to maintain all the time the rated power by opening more of governor valves whenever inlet pressure is decreased due to the tube plugging of steam generator. If throttle margin of high pressure turbine is too much compared to remaining lifetime, loss of electrical output due to pressure drop of governor valves is inevitable. On the contrary, if it is too little, the rated power operation can not be accomplished when inlet pressure of high pressure turbine is dropped after many years operation. So, throttle margin for high pressure turbine in nuclear power plant is compromised considering for the degradation of steam generator, governor valve capacity, manufacturing tolerance of high pressure turbine, future plan of power uprating, and remaining lifetime of power plant.

원자력/화력발전소의 터빈제어밸브시스템의 신뢰성 향상에 관한 연구 (A Study on the Reliability Improvement of the Turbine Control Valve System in Nuclear and Thermal Power Plants)

  • 양종대;양석조;이용범
    • 드라이브 ㆍ 컨트롤
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    • 제16권4호
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    • pp.93-100
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    • 2019
  • Nuclear and thermal power plants must provide the turbines with an appropriate degree of high temperature and high pressure steam, to produce the optimum electricity. Additionally, in the event of system and power system failure during electrical production, the steam is immediately disabled, to protect the turbines and generators rotating at high speed. The plant thus uses a special steam control valve system for turbine control, which is opened by force of the hydraulic servo actuator and closed by a large steel spring force. In this study, the causes of failure of the turbine control valve system, a key device of the power plants, were analyzed, and the causes of failure were improved relative to reliability of the equipment.

화력발전소에서 과열저감기의 증기온도제어 (Steam Temperature Control of Attemperator in Thermal Power Plant)

  • 신휘범
    • 조명전기설비학회논문지
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    • 제25권7호
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    • pp.40-48
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    • 2011
  • An attemperator is a part of the 4-stage superheater in the boiler system of the thermal power plant. The attemperator receives the over-heated steam and makes the steam with proper temperature by adjusting the control valve of the cold steam. In this paper, the attemperator is modeled considering physical point of view and the linearized model is derived for the control purpose. To overcome the integral windup phenomenon due to the opening limitation of the control valve, an anti-windup PI controller is proposed to the attemperator and compared with the PI controller operated in the thermal power plant in view of control performance.

원자력 발전소 AOV 구동기 설계 정립화 (A Thesis of Design Air Operated Valve Actuator in Nuclear Power Plant)

  • 최종귀;황지혁;김영범;손기철
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2008년도 추계학술대회B
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    • pp.2616-2620
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    • 2008
  • AOV used fluid capacity and fluid pressure control in nuclear power plant with heating power plant. AOV structures safely must be secured the reliability and a safety of the atomic power plant. but, AOV where is used from domestic is using the product of the overseas enterprise. The AOV design and maintenance technique is insufficient. Therefore According to ASME designed AOV, The performance test resultant fluid leakage did not occur and AOV design was satisfactory.

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화력발전소용 1인치 볼 밸브 유량계수 Cv에 관한 유동해석 및 실험에 관한 연구 (Experiment and Flow Analysis of the Flow Coefficient Cv of a 1 inch Ball Valve for a Thermal Power Plant)

  • 강창원;이중섭;이치우
    • 한국기계가공학회지
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    • 제18권3호
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    • pp.109-115
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    • 2019
  • The purpose of this study was to analyze and test the flow rate of a 1-inch ball valve used in a thermal power plant. To identify the flow-rate characteristics, numerical analysis was conducted and an experimental apparatus of the valve flow rate coefficient was used to compare the flow coefficient Cv values. To determine the internal pressure distribution, the sites of opening ball valves and flow fields were investigated. In particular, a smaller the valve opening resulted in a more complicated the flow field of the ball. The valve flow characteristic test showed that the Cv value and flow rate increased with increasing valve-opening rate and the secondary function was performed. The pressure drop increased as the valve opening rate decreased. In addition, the experimental results for the flow analysis are similar to the numerical analysis results.

원전 단종 밸브의 DED 방식 금속 3D프린팅 제작 및 성능시험 (Manufacturing and Performance Test of Obsolete Valve in NPP using DED Metal 3D Printing Technology )

  • 장경남
    • 한국압력기기공학회 논문집
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    • 제17권2호
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    • pp.75-82
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    • 2021
  • The 3D printing technology is one of the fourth industrial revolution technology that drives innovation in the manufacturing process, and should be applied to nuclear industry for various purposes according to the manufacturing trend change. In nuclear industry, it can be applied to manufacture obsolete items and new designed parts in advanced reactors or small modular reactors (SMRs), replacing the traditional manufacturing technologies. A gate valve body was manufactured, which was obsolete in nuclear power plant, using DED(Directed Energy Deposition) metal 3D printing technology after restoring design characteristics including 3D design drawing by reverse engineering. The 3D printed valve body was assembled with commercial parts such as seat-ring, disk, stem, and actuator for performance test. For the valve assembly, including 3D printed valve body, several tests were performed, including pressure test, end-loading test, and seismic test according to KEPIC MGG and KEPIC MFC. In the pressure test, hydraulic pressure of 391kgf/cm2 was applied to 3D printed valve body, and no leak was detected. Also the 3D printed valve assembly was performed well in end-loading and seismic tests.

원자력발전소 터빈밸브 시험주기 연장시 신뢰도평가 (The Reliability Evaluation of TBN Valve Testing Extension in NPP)

  • 임혁순;이은찬;이근성;황석원;성기열
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2007년도 춘계학술대회B
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    • pp.3221-3223
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    • 2007
  • Recently, nuclear power plant companies have been extending the turbine valve test interval to reduce the potential of the reactor trip accompanied with a turbine valve test and to improve the NPP's economy through the reduction of unexpected plant trip or decreased operation. In these regards, the extension of the test interval for turbine valves was reviewed in detail. The effect on the destructive overspeed probability due to the test interval change of turbine valves is evaluated by Fault Tree Analysis(FTA) method. Even though the test interval of turbine valves is changed from 1 month to 3 months, the analysis result shows that the reliability of turbine over speed protection system meets acceptance criteria of 1.0E-4/yr. This result will be used as the technical basis on the extension of the test interval for turbine valves. In this paper, the propriety of the turbine valve test interval extension is explained through the review on the turbine valve test interval status of turbine overspeed protection system, the analysis on the annual turbine missile frequency and the probability evaluation of the destructive overspeed due to the test interval extension.

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시스템분배기 소음방지 및 성능개선방안 연구 (A Study on the Noise Reduction and Performance Improvement of the Hot Water Distributing System)

  • 김용기;이태원;한태수;유선학
    • 대한설비공학회:학술대회논문집
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    • 대한설비공학회 2009년도 하계학술발표대회 논문집
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    • pp.1055-1060
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    • 2009
  • Noise is one of the major environmental problems in human life. But hot water distributers with the flow rate control valve bring about often noise according to the heating control condition in residential buildings. The sound power level increased as the flow rate and pressure difference increased. And thus, experimental analyses for the flow rate control and the pressure difference control were carried out in this study to reduce the noise emitted from the flow rate control valve. As the results, the flow rate control method using a SMA(Shape Memory Alloy)-valve and the flow rate control system using a pressure difference sensor can be expected to control noise in the region of below 50 dB of sound power level.

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