• Title/Summary/Keyword: Lost-wax casting

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Evaluation of trueness and precision of removable partial denture metal frameworks manufactured with digital technology and different materials

  • Leonardo Ciocca;Mattia Maltauro;Elena Pierantozzi;Lorenzo Breschi;Angela Montanari;Laura Anderlucci;Roberto Meneghello
    • The Journal of Advanced Prosthodontics
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    • v.15 no.2
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    • pp.55-62
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    • 2023
  • PURPOSE. The aim of this study is to evaluate the accuracy of removable partial denture (RPD) frameworks produced using different digital protocols. MATERIALS AND METHODS. 80 frameworks for RPDs were produced using CAD-CAM technology and divided into four groups of twenty (n = 20): Group 1, Titanium frameworks manufactured by digital metal laser sintering (DMLS); Group 2, Co-Cr frameworks manufactured by DMLS; Group 3, Polyamide PA12 castable resin manufactured by multi-jet fusion (MJF); and Group 4, Metal (Co-Cr) casting by using lost-wax technique. After the digital acquisition, eight specific areas were selected in order to measure the Δ-error value at the intaglio surface of RPD. The minimum value required for point sampling density (0.4 mm) was derived from the sensitivity analysis. The obtained Δ-error mean value was used for comparisons: 1. between different manufacturing processes; 2. between different manufacturing techniques in the same area of interest (AOI); and 3. between different AOI of the same group. RESULTS. The Δ-error mean value of each group ranged between -0.002 (Ti) and 0.041 (Co-Cr) mm. The Pearson's Chi-squared test revealed significant differences considering all groups paired two by two, except for group 3 and 4. The multiple comparison test documented a significant difference for each AOI among group 1, 3, and 4. The multiple comparison test showed significant differences among almost all different AOIs of each group. CONCLUSION. All Δ-mean error values of all digital protocols for manufacturing RPD frameworks optimally fit within the clinical tolerance limit of trueness and precision.

Evaluation of marginal and internal gaps of Ni-Cr and Co-Cr alloy copings manufactured by microstereolithography

  • Kim, Dong-Yeon;Kim, Chong-Myeong;Kim, Ji-Hwan;Kim, Hae-Young;Kim, Woong-Chul
    • The Journal of Advanced Prosthodontics
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    • v.9 no.3
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    • pp.176-181
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    • 2017
  • PURPOSE. The purpose of this study was to evaluate the marginal and internal gaps of Ni-Cr and Co-Cr copings, fabricated using the dental ${\mu}-SLA$ system. MATERIALS AND METHODS. Ten study dies were made using a two-step silicone impression with a dental stone (type IV) from the master die of a tooth. Ni-Cr (NC group) and Co-Cr (CC group) alloy copings were designed using a dental scanner, CAD software, resin coping, and casting process. In addition, 10 Ni-Cr alloy copings were manufactured using the lost-wax technique (LW group). The marginal and internal gaps in the 3 groups were measured using a digital microscope ($160{\times}$) with the silicone replica technique, and the obtained data were analyzed using the non-parametric Kruskal-Wallis H test. Post-hoc comparisons were performed using Bonferroni-corrected Mann-Whitney U tests (${\alpha}=.05$). RESULTS. The mean (${\pm}$ standard deviation) values of the marginal, chamfer, axial wall, and occlusal gaps in the 3 groups were as follows: $81.5{\pm}73.8$, $98.1{\pm}76.1$, $87.1{\pm}44.8$, and $146.8{\pm}78.7{\mu}m$ in the LW group; $76.8{\pm}48.0$, $141.7{\pm}57.1$, $80.7{\pm}47.5$, and $194.69{\pm}63.8{\mu}m$ in the NC group; and $124.2{\pm}52.0$, $199.5{\pm}71.0$, $67.1{\pm}37.6$, and $244.5{\pm}58.9{\mu}m$ in the CC group. CONCLUSION. The marginal gap in the LW and NC groups were clinically acceptable. Further improvement is needed for CC group to be used clinical practice.

Influence of the accuracy of abutment tooth preparation on the marginal adaptation of Co-Cr alloy copings fabricated with a selective laser sintering technology (지대치삭제의정확도가레이져신터링기술로제작된Co-Cr 코핑의변연적합도에미치는영향)

  • Kim, Seo-Rahng;Koak, Jai-Young;Heo, Seong-Joo;Kim, Seong-Kyun;Kim, Myung-Joo
    • The Journal of Korean Academy of Prosthodontics
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    • v.53 no.4
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    • pp.337-344
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    • 2015
  • Purpose: The purpose of present study is to examine the correlation between the accuracy of abutment preparation and the marginal adaptation of metal coping. With this view, this study compared the correlations regard to the three different manufacturing methods of selective laser sintering technique, milling and casting. Materials and methods: Two master models were made in a different way. First model with deep chamfer margin was prepared directly by a general clinician and the second model was designed by 3-D designing software program with the same abutment preparation principle and produced by computer aided manufacturing. 12 Co-Cr alloy copings were produced respectively with three different method; SLS system, CAD/CAM milling and conventional lost wax technique from each master model. The total 72 copings fully sit on the master model were stereoscopically evaluated at 40 points along the entire circumferential margin. Results: Significant differences in the absolute marginal discrepancies of Co- Cr copings from SLS system (P=.0231) and casting method (P<.0001) were shown between hand preparation model and computer designed model. However, no significant difference was found between the two model groups from milling method (P=.9962). Conclusion: Within the limitation of this study, the effect of the accuracy of abutment preparation on the marginal adaptation of Co-Cr coping is statistically significant in SLS system and casting group. The copings produced by SLS system exhibited the lowest marginal discrepancies among all groups, and the marginal gap of this method group was influenced by the accuracy of the abutment preparation.

A Study of the Golden Royal Seals Made by the Directorate for the Restoration of the Golden Royal Seals(金寶改造都監) in 1705 (1705년 금보개조도감(金寶改造都監) 제작 금보 연구)

  • Je, Ji-Hyeon
    • Korean Journal of Heritage: History & Science
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    • v.50 no.1
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    • pp.42-57
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    • 2017
  • The Joseon Dynasty (1392~1910) had a long tradition of making official seals to commemorate the granting of official royal titles, including posthumous honorary titles, to its kings, queens, crown princes and queen dowagers. These royal seals were typically gold-plated or made of jade. After the death of its holder, each seal would be stored in the royal seal depository in the Royal Ancestral Shrine. Extensive efforts were made to restore the traditions and culture of the royal family of Joseon during the reign of King Sukjong (r. 1674~1720). In 1705, discussions were held about the royal ceremonial objects, including the royal seals, stored in the Royal Ancestral Shrine, resulting in the reproduction of a set of accessories related with the storage of royal seals and ten golden royal seals which had been lost during wars or had yet to be made. With these reproductions, each shrine chamber of the Royal Ancestral Shrine would have had at least one seal. The details of the reproduction project were meticulously recorded in The Royal Protocol by the Directorate for the Restoration of Golden Royal Seals("金寶改造都監儀軌"). Given that the restoration project was the single event that led to the reproduction of all the golden royal seals, it is reasonable to conclude that the directorate had fulfilled a historically significant function. In this study, the main discussion is focused on the establishment of the directorate and the storage and management of the damaged royal seals. The discussion includes the manufacturing process of the golden seals, for which The Royal Protocol is compared with other similar documents in order to gain more detailed knowledge of the measurements of the turtle knob, the lost-wax casting technique, the gold plating with mercury amalgamation technique, and other ornamentation techniques. The discussion also covers the activities of the artisans who made the royal seals, based on a study of the royal protocols; the styles of the artifacts, based on an examination of the remaining examples; and the techniques used by the Directorate for the Restoration of Golden Royal Seals to produce the royal seals in 1705.