• Title/Summary/Keyword: High-Speed Rotating Machinery

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Rotordynamic Analysis and Experimental Investigation of the Turbine-Generator System Connected with Magnetic Coupling (마그네틱 커플링으로 연결된 터빈-발전기 시스템의 로터다이나믹 해석 및 실험적 고찰)

  • Kim, Byung Ok;Park, Moo Ryong;Choi, Bum Seok
    • The KSFM Journal of Fluid Machinery
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    • v.16 no.3
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    • pp.32-38
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    • 2013
  • This paper deals with the study on the rotordynamic and experimental analysis of turbine-generator system connected with a magnetic coupling. Although magnetic coupling has been used to torque transmission of chemical processing pump rotating at under 3,600rpm, magnetic coupling in this study is applied to high-speed turbine-generator system using a working fluid that is refrigerant such as ammonia or R-124a. Results of rotordynamic design analysis are as follows. The first, shaft diameter nearest to outer hub of magnetic coupling has a big effect on the $1^{st}$ critical speed of generator rotor. The second, if the $1^{st}$ critical speeds of turbine rotor and generator rotor have enough to separation margin in comparison to rated speed, the $1^{st}$ critical speed of turbine-magnetic coupling-generator rotor train has enough to separation margin regardless of connection stiffness of magnetic coupling. The analytical FE model is guaranteed by impact test on the prototype and condition monitoring such as measurements of vibration and bearing temperature is also performed.

Prediction of Power and Efficiency Requirement of Motor/generator for 500W Class Micro Gas Turbine Generator Considering Losses (손실을 고려한 500W급 마이크로 가스터빈 발전기용 전동발전기의 요구동력 및 요구효율 선정)

  • Park, Cheol-Hoon;Choi, Sang-Kyu;Ham, Sang-Yong
    • The KSFM Journal of Fluid Machinery
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    • v.14 no.5
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    • pp.24-30
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    • 2011
  • 500W class MTG(Micro turbine generator) operating at 400,000 rpm is under development. From the cycle analysis, it is decided that the self-sustaining speed of MTG is 200,000rpm and the generating speed is 400,000 rpm. Therefore, motor should be designed so that it is able to rotate the rotor up to 200,000rpm and generator should designed so that it is able to generate 500W output at 400,000rpm. First step to design motor/generator is to determine the power and efficiency requirement. Not only the power into the compressor and from the turbine at the operating speed but also the mechanical and electrical losses should be considered in determining the power and efficiency requirement. This study presents the procedure and the results of determining the power and efficiency requirement considering the mechanical and electrical losses depending on the rotating speed which is measured from the experiment.

A Study on the Accelerated Life Test of BLDC Motor in Ceiling Mounted Digital Signage Rotating System (천정 거치형 디지털 사이니지 회전 시스템의 BLDC모터 가속수명시험에 관한 연구)

  • Kim, Ki-Hong;Kwon, Soon-Hong;Kwon, Soon-Gu;Park, Jong-Min;Kim, Jong-Soon;Jung, Sung-Won;Choi, Won-Sik
    • Journal of the Korean Society of Industry Convergence
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    • v.21 no.3
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    • pp.141-147
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    • 2018
  • In a time when product development cycles are getting shorter and shorter, many companies are making efforts to develop products with high reliability in a short period of time, accelerated life test is widely used as a method to quickly evaluate reliability. Accelerated life test reduces the test life or the life of the product from the observed data by shortening the lifetime of the product or abruptly lowering the performance under the worse condition than the actual condition in order to shorten the test cost or the test time. In this paper, BL3640A-06P+RB35, DC12V model, which is used in the support device of an automatic rotation type digital signage, which display various information such as textures and images on a display screen in a public place or a commercial space, BLDC motors were subjected to a constant stress test and at the rotational speed of 1rpm, $180^{\circ}$ rotation and reverse rotation under actual use conditions, the stress was imposed on the rotating speed of 2rpm and the weight of the actual installed product from 22.2kgf to 10kgf were installed. The lifetime of the actual use environment condition is 23,545 hours and the rotation speed is accelerated. The life time of the acceleration condition with the additional weight is 1,380 hours. The acceleration factor is calculated as 17.06, the one year guarantee test day is 235 days to 14 days, of the period from 470 days to 28 days, and the third year from 704 days to 42 days. The test date of the BLDC motor was tested on the shortened test date, and the rotational speed and the current value were measured. It is found that there is no defect even if it operates as the test date corresponding to the specified one year warranty period and the 3 year accelerated life test which is experimented. Using the statistical technique of the regression analysis the expected time for the motor to defect to #4 samples was 20 years.

A Study on the Reliability of an Air Foil Journal Bearing for High Speed Turbomachinery (고속 터보기계용 공기 포일 저널 베어링의 신뢰성에 관한 연구)

  • Lee, Yong-Bok;Kim, Tae-Ho;Kim, Chang-Ho;Lee, Nam-Soo
    • 유체기계공업학회:학술대회논문집
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    • 2002.12a
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    • pp.199-206
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    • 2002
  • This paper describes a reliability characteristics of an air foil journal bearing for high speed turbomachinery at room temperature. To verify the reliability of air foil journal bearing, lift-off characteristics, load carrying capacity, and 10,000 cycle start-stop test were performed with motor driven test rig. Lift-off test shows the relationship between the rotating speed of the shaft and the frictional torque with bearing surface. About load carrying capacity, the tested air foil journal bearing produced a load capacity of 500N at an operating speed of 15,000rpm, which is compared with results of numerical analysis and empirical coefficients. Finally, The trends in change of start torque, stop torque, and bearing temperature were shown during 10,000 cycle start-stop test of an air foil journal bearing. from the results of this work, an air foil bearing will be done well, as a supported bearing for high speed turbo-compressor.

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Seismic analysis of turbo machinery foundation: Shaking table test and computational modeling

  • Tripathy, Sungyani;Desai, Atul K
    • Earthquakes and Structures
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    • v.12 no.6
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    • pp.629-641
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    • 2017
  • Foundation plays a significant role in safe and efficient turbo machinery operation. Turbo machineries generate harmonic load on the foundation due to their high speed rotating motion which causes vibration in the machinery, foundation and soil beneath the foundation. The problems caused by vibration get multiplied if the soil is poor. An improperly designed machine foundation increases the vibration and reduces machinery health leading to frequent maintenance. Hence it is very important to study the soil structure interaction and effect of machine vibration on the foundation during turbo machinery operation in the design stage itself. The present work studies the effect of harmonic load due to machine operation along with earthquake loading on the frame foundation for poor soil conditions. Various alternative foundations like rafts, barrette, batter pile and combinations of barrettes with batter pile are analyzed to study the improvements in the vibration patterns. Detailed computational analysis was carried out in SAP 2000 software; the numerical model was analyzed and compared with the shaking table experiment results. The numerical results are found to be closely matching with the experimental data which confirms the accuracy of the numerical model predictions. Both shake table and SAP 2000 results reveal that combination of barrette and batter piles with raft are best suitable for poor soil conditions because it reduces the displacement at top deck, bending moment and horizontal displacement of pile and thereby making the foundation more stable under seismic loading.

Development of Rotating Cone Type Garlic Clove Separator (II) - Effect by Clearance between Inner and Outer Frustum - (회전 원추형 마늘 쪽분리기 개발에 관한 연구 (II) - 원추 간극의 영향 -)

  • Lee, J.S.;Kim, K.B.
    • Journal of Biosystems Engineering
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    • v.32 no.2 s.121
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    • pp.77-83
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    • 2007
  • The purpose of this study is to find optimal conditions for various outlet clearances of prototype garlic clove separator with a rotating cone in the constant inlet clearance and cone height. Optimal outlet clearance from medium to small size garlics was 25 mm at the $200{\sim}400rpm$. For large garlic, optimal outlet clearances of Namdo and Uiseong garlic were 34 mm and 37 mm, respectively, in the range of $300{\sim}400rpm$. The proportion of garlic separation was over 95% for all quality of garlics. The proportions of damaged garlics at 25 mm and 28 mm outlet clearances were below 5% and below 10%, respectively. Therefore, in order to maintain high performance of garlic separation for the various varieties and qualities, the rotating cone type separator should be designed with cone speed ranges of $200{\sim}400rpm$ and the outlet clearance ranges of $25{\sim}37 mm$. The outlet clearance of the separator should be easily controlled within those ranges.

Flow Analysis of a Low-Noise Turbo Fan for a Vacuum Cleaner (진공청소기용 저소음 터보팬 내부 유동 해석)

  • Lee, Ki-Choon;Kim, Chang-Jun;Hur, Nahmkeon;Jeon, Wan-Ho
    • The KSFM Journal of Fluid Machinery
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    • v.6 no.4 s.21
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    • pp.14-20
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    • 2003
  • In this study an analysis of the flow characteristics in three types of turbo-fans for a vacuum cleaner was performed by using CFD. The characteristics of three models calculated for various rotating speed for flow rates are obtained and compared with measured data. The mixing plane approach is applied to compute the flow between impeller and diffuser. The results show that the model that is modified to reduce fan noise gives stable flow characteristics in operating range than the original model, with both models show similar performance characteristics at the range of high flow rate. Since in the modified model it takes much longer for an impeller blade to pass a diffuser blade than in the original model, and the peak pressure at BPF can be relieved, it is anticipated that the modified model give much lower noise level with similar performance than the original one, which remains to be verified by unsteady computation and measurements. The good agreement between the predictions and measurement results confirms the validity of this study.

Comparison of Theoretical Analysis with Test Results of Floating Ring Seals for the LRE Turbo Pump (액체 추진 로켓 터보 펌프용 플로팅 링 실에 대한 해석 및 실험 결과의 비교 연구)

  • Lee, Yong-Bok;An, Kyoung-Min;Kim, Chang-Ho;Ha, Tae-Woong
    • The KSFM Journal of Fluid Machinery
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    • v.7 no.6 s.27
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    • pp.21-27
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    • 2004
  • The floating ring seal has an advantage to find the optimum position by itself, which is used in the turbo pump of a liquid rocket. The main purpose of seals is to reduce the leakage. Especially, seals of the turbo pump for the liquid rocket engine are operated under the serious conditions such as high pressure above 10 MPa, very low temperature about $-180^{\circ}C$ and high rotating speed above 25,000 rpm. So, rotordynamic stability is very important for the system stability. In this paper, the leakage and dynamic characteristics of floating ring seals were investigated by a experimental and analytical method. The theoretical results of the leakage performance for the floating ring seal showed much higher than that of experimental results. On the other hand, the results of stiffness and damping characteristics showed similarity each other. As the shaft speed was increasing, the whirl frequency ratio was increased in the experimental results.

DEVELOPMENT OF MUSHROOM SPAWN BOTTLE CUTTER-SPAWM CAKE SHREDDER

  • Choe, Kwang-Jae;Chang, Yu-Seob;Yun, Jin-Ha
    • Proceedings of the Korean Society for Agricultural Machinery Conference
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    • 1996.06c
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    • pp.1031-1040
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    • 1996
  • Spawn bottle cutting and spawn cake shredding machine has been developed to save the farm labor and operating cost for mushroom growing farmers. The prototype can cut the bottom and side of the bottle while shredding the spawn cake by one farmer. The cutting plastic shell is done by two couples of high speed disc saws that can cut cross section and lengthwise two side of the bottle, while spawn cake shredding is done by spike teethed rotating drum and wiremesh concave. The optimum speed of cutting disc saw was observed 1.700rpm both the cross cutting saw and lengthwise cutting saw in consideration of the cutting accuracy. And the location for the instalation of cross cutting disc saw was considered as around 4 mm above the table bottom , while the optimum clearance between two edges of lengthwise cutting disc saw was showed 86mm. For the sawdust spawn cake shredder , proper size of spawn sawdust granule was observed in the 15 x 15mm size withmesh concave with the shredding rum speed of 500rpm. The prototype can be reduce 73 per cent of working hours with the working cost reduction of 49 per cent compare with those of conventional operation.

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Characteristics of the Shaft Vibration in a High Head Pump-Turbine (고낙차 펌프-터빈에서의 축계 진동 특성)

  • Ha, Hyun Cheon;Choi, Seong Pil
    • 유체기계공업학회:학술대회논문집
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    • 1998.12a
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    • pp.166-172
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    • 1998
  • This paper describes the shaft vibration phenomena measured on a pump-turbine ofa pumped storage power plant. The pump-turbine runs at a rotational speed of 450 rpm (7.5 Hz). The power output (load) of the pump-turbine was varied from 100 to 300 MW in the generating mode. It was found that the magnitude of the shaft vibration was highly dependent upon the power load. The vibration magnitude of the shaft vibration is very high in the middle load zone from 170 to 210 MW, elsewhere the vibration low. From vibration spectra, it was found that the frequency of major vibration in that load zone was 2.5 Hz which is approximately $34\%$ of the shaft rotating speed in Hz. This frequency component disappeared below and above that load zone. This subsynchronous vibration is caused by the flow induced disturbance due to spiral vortex flow downstream of the pump-turbine runner. Furthermore, it was found that shaft vibration was highly decreased due to the increase of bearing preload.

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