• Title/Summary/Keyword: Heat Exchange Heater

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Design of Large Capacity Clean Air Heater (대용량 청정 공기 가열 장치 설계)

  • Kim, Jeong-Woo;Jung, Kwang-Soo;Jeon, Min-Joon;Lee, Kyu-Joon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.115-118
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    • 2010
  • 2 Types of heater (Vitiated Type, Clean Air Type) in order to increase the temperature for a test are used for industry. In this report, large capacity clean air type heater was designed. Heater capacity and LNG consumption rate can be calculated by the air mass flow and heater inlet/outlet temperature. The heater is composed by Burner, Furnace, Heat Exchanger, and Stack. The hot air from the burner and cold air from the tube inlet exchange their heat indirectly in the heat exchanger, so the desired temperature can be achieved at the exit of the tube.

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A Study on the Characteristics of Heating Performance of High-Performance Heat Pump with VI cycle using Re-Heater (재열기를 사용한 고성능 VI 사이클 열펌프의 난방 성능 특성에 관한 연구)

  • Lee, Jin-Kook;Choi, Kwang-Hwan
    • Journal of Power System Engineering
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    • v.19 no.4
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    • pp.69-75
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    • 2015
  • In this study, the characteristics of heating performance of a high-performance air-cooled heat pump with vapor-injection(VI) cycle using re-heater was investigated experimentally. Devices used in the experiment is consist of a VI compressor, condenser, oil separator, refrigerant (economizer outlet refrigerant) re-heater, economizer, evaporator. And R410A was used as a working fluid. The experiment was conducted with two cycles(cycles A and B) for investigating heating performance. In case of cycle B, heat exchange was conducted by re-heater between outlet refrigerant of compressor and suction refrigerant of the VI system(Fig.1, re-heater). But the re-heater was not used in case of cycle A. As a result of this experiment, discharge temperature of refrigerator in compressor was shown higher value, when the cycle B was conducted, because of the heat exchange between suction refrigerant of VI cycle and outlet refrigerant of compressor in the re-heater than cycle A that was not use re-heater. it means that liquid hammer and the decrement of heating performance can be decreased by using re-heater. Also, Heating coefficient of performance(COPh) was shown about 2.98 in Cycle B which was 4% higher than Cycle A and from these results, It was confirmed that the improvement of the heating performance of heat pump with VI cycle can be achieved by applying re-heater.

The Review and Investigation of High Temperature Heater Development (고온 공기 가열기 개발 현황 조사 및 고찰)

  • Kim, Jeongwoo;Lee, Jungmin
    • Journal of the Korean Society of Propulsion Engineers
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    • v.20 no.5
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    • pp.90-98
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    • 2016
  • A high temperature heater is required to supply high temperature air to the hypersonic propulsion system in order to simulate high velocity flying condition during the ground test. Various high temperature heaters were reviewed, categorized, and analyzed in this paper. Heaters were categorized in 4 groups; in-stream combustion heater, electric arc heater, storage heater, and heat exchange heater. Each group has its own advantages and disadvantages, so the heater should be selected considering its purpose.

EXHAUST GAS HEAT RECOVERY SYSTEM FOR PLANT BED HEATING IN GREENHOUSE PRODUCTION

  • Kim, Y.J.;Ryou, Y.S.;Rhee, K.J.;Kang, G.C.
    • Proceedings of the Korean Society for Agricultural Machinery Conference
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    • 2000.11c
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    • pp.639-646
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    • 2000
  • Hot air heater with light oil combustion is the most common heater for greenhouse heating in the winter season in Korea. However, since the heat efficiency of the heater is about 80%, considerable unused heat in the form of exhaust gas heat discharges to atmosphere. In order to capture this exhaust gas heat a heat recovery system for plant bed heating in the greenhouse was built and tested in the hot air heating system of greenhouse. The system consists of a heat exchanger made of copper pipes, ${\phi}\;12.7{\times}0.7t$ located inside the rectangular column of $330{\times}330{\times}900mm$, a water circulation pump, circulation plastic pipe and a water tame The total heat exchanger area is $1.5m^2$, calculated considering the heat exchange amount between flue gas and water circulated in the copper pipes. The system was attached to the exhaust gas path. The heat recovery system was designed as to even recapture the latent heat of flue gas when exposing to low temperature water in the heat exchanger. According to performance test it can recover 45,200 to 51,000kJ/hr depending on the water circulation rates of 330 to $690{\ell}$/hr from the waste heat discharged. The exhaust gas temperature left from the heat exchanger dropped to $100^{circ}C$ from $270^{circ}C$ by the heat exchange between the water and the flue gas, while water gained the difference and temperature increased to $38^{circ}C$ from $21^{circ}C$ at the water flow rate of $690{\ell}$/hr. And, the condensed water amount varies from 16 to $43m{\ell}$ at the same water circulation rates. This condensing heat recovery system can reduce boiler fuel consumption amount in a day by 34% according to the feasibility study of the actual mimitomato greenhouse. No combustion load was observed in the hot air heater.

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Heat Recovery Characteristics of the Exhaust Heat Recovery System with Heat Pipe Unit Attached to the Hot Air Heater in the Greenhouse (히트파이프를 이용한 온풍난방기 배기열회수 시스템의 열회수 특성)

  • Kang, K. C.;Kim, Y. J.;Ryou, Y. S.;Baek, Y.;Rhee, K. J.
    • Journal of Biosystems Engineering
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    • v.26 no.5
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    • pp.441-448
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    • 2001
  • Hot air heater with light oil combustion is used as the most common heater for greenhouse heating in the winter season. However, exhaust gas heat discharged to atmosphere through chimney reaches up to 10~20% of total heat capacity of the oil burred. In order to recover the heat of this exhaust gas and to use for greenhouse heating, the heat pipe type exhaust heat recovery system was manufactured and tested in this experiment. The system consisted of a heat exchanger made of heat pipes, ø15.88${\times}$600mm located in the rectangular box of 675(L)${\times}$425(W)${\times}$370(H)mm, an air suction fan and air ducts. The number of heat pipe was 60, calculated considering the heat exchange amount between exhaust gas and air and heat transfer capacity of a heat pipe. The working fluid of heat pipe was acetone because acetone is known for its excellent heat transfer capacity. The system was attached to the exhaust gas path. According to the performance test it could recover 53,809 to 74,613kJ/h depending on the inlet air temperature of 12 to -12˚at air flow rate of 1.100㎥/h. The temperature of the exhaust gas left the heat exchanger dropped to 100$^{\circ}C$ from 270$^{\circ}C$ after the heat exchange between the suction air and the exhaust gas.

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Heating Performance Characteristics of Heat Pump with VI cycle using Re-Heater and Solar-Assisted (태양열과 재열기를 사용한 VI heat pump의 성능 특성에 관한 연구)

  • Lee, Jin-Kook;Choi, Kwang-Hwan
    • Journal of the Korean Solar Energy Society
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    • v.35 no.6
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    • pp.25-33
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    • 2015
  • In this study, heating performance of the air-cooled heat pump with vapor-injection (VI) cycles, re-heater and solar heat storage tank was investigated experimentally. Devices used in the experiment were comprised of a VI compressor, re-heater, economizer, variable evaporator, flat-plate solar collector for hot water, thermal storage tank, etc. As working fluid, refrigerant R410A for heat pump and propylene glycol (PG) for solar collector were used. In this experiment, heating performance was compared by three cycles, A, B and C. In case of Cycle B, heat exchange was conducted between VI suction refrigerant and inlet refrigerant of condenser by re-heater (Re-heater in Fig. 3, No. 3) (Cycle B), and Cycle A was not use re-heater on the same operating conditions. In case of Cycle C, outlet refrigerant from evaporator go to thermal storage tank for getting a thermal energy from solar thermal storage tank while re-heater also used. As a result, Cycle C reached the target temperature of water in a shorter time than Cycle B and Cycle A. In addition, it was founded that, as for the coefficient of heating performance($COP_h$), the performance in Cycle C was improved by 13.6% higher than the performance of Cycle B shown the average $COP_h$ of 3.0 and by 18.9% higher than the performance of Cycle A shown the average $COP_h$ of 2.86. From this results, It was confirmed that the performance of heat pump system with refrigerant re-heater and VI cycle can be improved by applying solar thermal energy as an auxiliary heat source.

Basic Study on 250KW-class IoT Electric Heater for Ship Fuel Heating (선박연료 가열용 250KW급 판형 IoT 전기히터의 기초연구)

  • Jang, Sung-Cheol
    • Journal of Internet of Things and Convergence
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    • v.7 no.3
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    • pp.63-68
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    • 2021
  • Domestic electric heater manufacturers are focusing on technology development to improve the efficiency of existing products. The electric heater for ship fuel is large in size and has high difficulty in miniaturization/high efficiency, so there are not many companies that try to develop technology yet. The existing electric heater has a structure of low heating efficiency because the contact time with the heat exchange tube of the heating medium is very short because the flow path of the ship engine fuel is monotonous. Since it is manufactured in a tubular shape, the volume is very large regardless of the heating efficiency. As a result, the tubular electric heater device applied by overseas advanced companies has difficulty in maintaining and repairing because it is necessary to decompose all tubular heaters when a specific part of the inside is damaged and if the heat exchange tube is damaged, all the heat exchange tubes must be decomposed. In this study, a basic study on plate type electric heaters capable of heating 10 tons of ship engine fuel per hour and setting a maximum temperature of up to 150℃ was conducted through a 250kW capacity plate type electric heater.

Heat Transfer Performance of Plate Type Absorber with Surfactant

  • Yoon, Jung-In;M. M. A. Sarker;Moon, Choon-Geun
    • Journal of Advanced Marine Engineering and Technology
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    • v.28 no.2
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    • pp.243-251
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    • 2004
  • Absorption chiller/heater can utilize the unused energy of the daily life waste heat, the industry waste heat. the solar energy and the earth energy. These can contribute to energy savings. But the absorption chiller/heater has a demerit that the size of absorption chiller/heater is larger than that of the vapor compression type based on same capacity. In this study. the experimental apparatus of an absorber is manufactured as a plate. which is newly applied in an absorber. The experimental apparatus is composed of a plate type absorber. which can increase the heat exchange area per unit volume and thus facilitating to deeply investigate more detail features instead of that done by the existing type. i.e.. horizontal tube bundle type. The characteristics of heat transfer and refrigeration capacity are studied experimentally. The absorption enhancement by using surfactant is closely examined through the experiment and comparative figures are presented in quantitative and qualitative analysis.

Study on the Performance of Total Heat Exchanger with Rotating Porous Plates (다공형 전열판의 회전에 의한 열교환시스템의 성능에 관한 연구(Ⅰ) - 환기측과 외기측의 풍량 변화에 대하여 -)

  • Cho, D.H.;Lim, T.W.
    • Journal of Power System Engineering
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    • v.9 no.4
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    • pp.11-17
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    • 2005
  • This paper reports an experimental study on the performance evaluation of air-to-air heat exchanger with rotary type newly developed in this study. Air flow rate is varied from 10 to 120 m3/h. The range of RPM of the porous rotating discs mounted inside the heat exchanger unit is 0 to 50. The temperature of the return air side is set by adjusting heat supply at heater. The material of the porous rotating discs is cooper and its thickness is 1.0 mm. The heat transfer rate increased with the increase in air flow rate. It was found that the heat transfer rate, as the temperature of the return air side was increased, was improved due to higher temperature difference. The heat exchange performance increased with the increase in the temperature of the return air side at the conditions of the same RPM. The sensible heat exchange efficiency was maximum 68 to 76 percent, and enthalpy exchange efficiency 64 to 74 percent.

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Heat Recovery Characteristics of the Hot Water Supply System with Exhaust Heat Recovery Unit Attached to the Hot Air Heater for Plant Bed Heating in the Greenhouse (온풍난방기의 배기열을 이용한 지중 난방용 온수공급시스템의 열회수특성)

  • 김영중;유영선;장진택;강금춘;이건중;신정웅
    • Journal of Biosystems Engineering
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    • v.25 no.3
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    • pp.221-226
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    • 2000
  • Hot air heater with light oil burner is the most common heater for greenhouse heating in the winter season in Korea. However, since the thermal efficiency of the heater is about 80∼85%, considerable unused heat amount in the form of exhaust gas heat discharges to atmosphere. In order to capture this exhaust heat a heat recovery system for plant bed heating in the greenhouse was built and tested in the hot air heating system of greenhouse. The heat recovery system is made for plant bed or soil heating in the greenhouse. The system consisted of a heat exchanger made of copper pipes, ${\Phi}12.7{\times}0.7t$ located in the rectangular column of $330{\times}330{\times}900mm$, a water circulation pump, circulation plastic pipe and a water tank. The total heat exchanger area is 1.5$m^2$, calculated considering the heat exchange amount between flue gas and water circulated in the copper pipes. The system was attached to the exhaust gas path. The heat recovery system was designed as to even recapture the latent heat of flue gas when exposing to low temperature water in the heat exchanger. According to the performance test it could recover 45,200 to 51,000kJ/hr depending on the water circulation rates of 330 to $690\ell$/hr from the waste heat discharged. The exhaust gas temperature left the heat exchanger dropped to $100^{\circ}C$ from $270^{\circ}C$ by the heat exchange between the water and the flue gas, while water gained the difference and temperature increased to $38^{\circ}C$ from $21^{\circ}C$ at the water flow rate of $690\ell$/hr. By the feasibility test conducted in the greenhouse, the system did not encounter any difficulty in operations. And, the system could recover 220,235kJ of exhaust gas heat in a day, which is equivalent of 34% of the fuel consumption by the water boiler for plant bed heating of 0.2ha in the greenhouse.

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