• Title/Summary/Keyword: Head loss & discharge

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A Study on a Calculation Method of Economical Intake Water Depth in the Design of Head Works (취입모의 경제적 계획취입수심 산정방법에 대한 연구)

  • 김철기
    • Magazine of the Korean Society of Agricultural Engineers
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    • v.20 no.1
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    • pp.4592-4598
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    • 1978
  • The purpose of this research is to find out mathemetically an economical intake water depth in the design of head works through the derivation of some formulas. For the performance of the purpose the following formulas were found out for the design intake water depth in each flow type of intake sluice, such as overflow type and orifice type. (1) The conditional equations of !he economical intake water depth in .case that weir body is placed on permeable soil layer ; (a) in the overflow type of intake sluice, {{{{ { zp}_{1 } { Lh}_{1 }+ { 1} over {2 } { Cp}_{3 }L(0.67 SQRT { q} -0.61) { ( { d}_{0 }+ { h}_{1 }+ { h}_{0 } )}^{- { 1} over {2 } }- { { { 3Q}_{1 } { p}_{5 } { h}_{1 } }^{- { 5} over {2 } } } over { { 2m}_{1 }(1-s) SQRT { 2gs} }+[ LEFT { b+ { 4C TIMES { 0.61}^{2 } } over {3(r-1) }+z( { d}_{0 }+ { h}_{0 } ) RIGHT } { p}_{1 }L+(1+ SQRT { 1+ { z}^{2 } } ) { p}_{2 }L+ { dcp}_{3 }L+ { nkp}_{5 }+( { 2z}_{0 }+m )(1-s) { L}_{d } { p}_{7 } ] =0}}}} (b) in the orifice type of intake sluice, {{{{ { zp}_{1 } { Lh}_{1 }+ { 1} over {2 } C { p}_{3 }L(0.67 SQRT { q} -0.61)}}}} {{{{ { ({d }_{0 }+ { h}_{1 }+ { h}_{0 } )}^{ - { 1} over {2 } }- { { 3Q}_{1 } { p}_{ 6} { { h}_{1 } }^{- { 5} over {2 } } } over { { 2m}_{ 2}m' SQRT { 2gs} }+[ LEFT { b+ { 4C TIMES { 0.61}^{2 } } over {3(r-1) }+z( { d}_{0 }+ { h}_{0 } ) RIGHT } { p}_{1 }L }}}} {{{{+(1+ SQRT { 1+ { z}^{2 } } ) { p}_{2 } L+dC { p}_{4 }L+(2 { z}_{0 }+m )(1-s) { L}_{d } { p}_{7 }]=0 }}}} where, z=outer slope of weir body (value of cotangent), h1=intake water depth (m), L=total length of weir (m), C=Bligh's creep ratio, q=flood discharge overflowing weir crest per unit length of weir (m3/sec/m), d0=average height to intake sill elevation in weir (m), h0=freeboard of weir (m), Q1=design irrigation requirements (m3/sec), m1=coefficient of head loss (0.9∼0.95) s=(h1-h2)/h1, h2=flow water depth outside intake sluice gate (m), b=width of weir crest (m), r=specific weight of weir materials, d=depth of cutting along seepage length under the weir (m), n=number of side contraction, k=coefficient of side contraction loss (0.02∼0.04), m2=coefficient of discharge (0.7∼0.9) m'=h0/h1, h0=open height of gate (m), p1 and p4=unit price of weir body and of excavation of weir site, respectively (won/㎥), p2 and p3=unit price of construction form and of revetment for protection of downstream riverbed, respectively (won/㎡), p5 and p6=average cost per unit width of intake sluice including cost of intake canal having the same one as width of the sluice in case of overflow type and orifice type respectively (won/m), zo : inner slope of section area in intake canal from its beginning point to its changing point to ordinary flow section, m: coefficient concerning the mean width of intak canal site,a : freeboard of intake canal. (2) The conditional equations of the economical intake water depth in case that weir body is built on the foundation of rock bed ; (a) in the overflow type of intake sluice, {{{{ { zp}_{1 } { Lh}_{1 }- { { { 3Q}_{1 } { p}_{5 } { h}_{1 } }^{- {5 } over {2 } } } over { { 2m}_{1 }(1-s) SQRT { 2gs} }+[ LEFT { b+z( { d}_{0 }+ { h}_{0 } )RIGHT } { p}_{1 }L+(1+ SQRT { 1+ { z}^{2 } } ) { p}_{2 }L+ { nkp}_{5 }}}}} {{{{+( { 2z}_{0 }+m )(1-s) { L}_{d } { p}_{7 } ]=0 }}}} (b) in the orifice type of intake sluice, {{{{ { zp}_{1 } { Lh}_{1 }- { { { 3Q}_{1 } { p}_{6 } { h}_{1 } }^{- {5 } over {2 } } } over { { 2m}_{2 }m' SQRT { 2gs} }+[ LEFT { b+z( { d}_{0 }+ { h}_{0 } )RIGHT } { p}_{1 }L+(1+ SQRT { 1+ { z}^{2 } } ) { p}_{2 }L}}}} {{{{+( { 2z}_{0 }+m )(1-s) { L}_{d } { p}_{7 } ]=0}}}} The construction cost of weir cut-off and revetment on outside slope of leeve, and the damages suffered from inundation in upstream area were not included in the process of deriving the above conditional equations, but it is true that magnitude of intake water depth influences somewhat on the cost and damages. Therefore, in applying the above equations the fact that should not be over looked is that the design value of intake water depth to be adopted should not be more largely determined than the value of h1 satisfying the above formulas.

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An Experimental Study for Reduction of Energy losses at Surcharged Four-way Combining Square Manhole (과부하 4방향 사각형 합류맨홀에서의 에너지 손실 저감을 위한 실험 연구)

  • Kim, Jung Soo;Kim, Chae Rin;Yoon, Sei Eui
    • KSCE Journal of Civil and Environmental Engineering Research
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    • v.37 no.2
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    • pp.311-324
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    • 2017
  • Energy loss at manholes under surcharged flow is considered as one of the major causes of inundation in urban area. Therefore, it is necessary to analyze the flow characteristics to reduce the energy loss in the surcharged four-way combining manhole. In this study, hydraulic experimental apparatus was constructed considering the results of the present survey. Square manholes and pipe diameters were reduced to 1/5 by applying sewer facility standards. Numerical simulations were carried out with the Fluent 6.3 model to derive the invert condition which can reduce the energy loss in the surcharged four-way combining square manhole. The hydraulic experiments were carried out according to the various conditions of the lateral flow rate($Q_{lat}/Q_{out}$), discharge of outflow pipe (2.0, 3.0, 4.0, 4.8 l/sec), and invert shape (rectangle and square open conduit type). The crossed invert was not found to improve the drainage capacity of the surcharged four-way rectangular combining manhole. However, the improved rectangle open conduit type invert and square open conduit type invert were analyzed to improve the drainage capacity by reducing the head loss coefficients by about 8% and 28%, respectively. Therefore, in order to increase the drainage capacity of urban facilities, it is possible to install and use the improved invert proposed in this study.

A Study on Process Optimization for CSOs Application of Horizontal Flow Filtration Technology (수평흐름식 여과기술의 CSOs 적용을 위한 공정 최적화 연구)

  • Kim, Jae-Hak;Yang, Jeong-Ha;Lee, Young-Shin
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.19 no.2
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    • pp.56-63
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    • 2018
  • The management of Combined Sewer Overflows(CSOs) and Separated Sewer Overflows(SSOs) discharge directly to the effluent system in an untreated state, which occurs when the facility capacity is exceeded due to heavy rain, has become an important issue in recent years as the heavy rain becomes a regular phenomenon. Despite the continuous development of filtration technology, targeting densely populated urban areas, CSOs are rarely applied. Therefore, this study was carried out to optimize the process to apply CSOs in a pilot-scale horizontal flow filtration system with a rope-type synthetic fiber. The research was carried out in two steps: a preliminary study using artificial samples and a field study using sewage. In the preliminary study using an artificial sample, head loss of the filter media itself was analyzed to be approximately 1.1cm, and the head loss was increased by approximately 0.1cm as the linear velocity was increased by 10m/hr. In addition, the SS removal efficiency was stable at 81.4%, the filtration duration was maintained for more than 6 hours, and the average recovery rate of 98% was obtained by air backwashing only. In the on-site evaluation using sewage, the filtration duration was approximately 2 hours and the average removal efficiency of 83.9% was obtained when belt screen (over 450 mesh) was applied as a pre-treatment process to prevent the premature clogging of filter media. To apply the filtration process to CSOs and SSOs, it was concluded that the combination with the pre-treatment process was important to reinforce the hydraulic dimension for the stable maintain of operation period, rather than efficiency. Compared to the dry season, the quality of incoming sewage was lower in the rainy season, which was attributed to the characteristics of the drainage area with higher sanitary sewerage. In addition, the difference in removal efficiency according to the influent quality of the wet season and dry season was small.

Verification of the Filter Media Applied to Filter Type Facility Considering the Treatment Efficiency Factor (여과형 시설에 적용되는 여재의 처리효율 영향인자를 고려한 실증화 평가)

  • Kim, Taeyoon;Lee, Junebae;Lee, Dongwoo;Shin, Hyunsuk;Kim, Hyunchul;Kwon, Soonchul
    • Journal of Korean Society on Water Environment
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    • v.33 no.5
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    • pp.572-579
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    • 2017
  • Increased impervious surface caused by rapid urbanization serves to produce the discharge of non-point source pollutants such as total suspended solid (TSS). There exist various methods of removing TSS, including a filtration process using granular media (a well-known method to be practically used after the consideration of removal efficiency, clogging, and backwashing efficiency). To determine the TSS removal capability of the filter, we initially performed lab-scale experiments which assessed flow rates, influent concentrations, permeability co-efficients, the particular shapes of suspended solids and potential clogging, and also evaluated TSS removal efficiency when applied to filtration facility in a pilot-scale. In low filtration flux condition, the removal efficiency of suspended solids was more than 95 %, while decreased to 83% in high filtration flux. Regarding the clogging aspect of the experiment, total cumulative solids were loaded up to $19.15kg/m^2$, and TSS removal efficiency was noted to commence to decrease when the loaded solids exceeded $9.0kg/m^2$. It was also noted, however, that superior efficiency was maintained for six hours. In addition, for pilot-scale experiment, the removal efficiency was still high enough (83.4 %) for the solid concentration of 140 ~ 343 mg SS/L and after backwashing, head loss was recovered to 92 ~ 95 % during two hour filtration. With these results, It was confirmed that lifetime of the filter applied to the test was prolonged due to the high treatment efficiency and good backwashing efficiency for the cumulative solids load.

Evaluation of Filtration and Backwash Efficiency of Non-point Source Pollution Reduction Facility (장치형 비점오염원 저감시설의 여과 및 역세 효율 평가)

  • Yun, Sangleen;Lee, Yong-Jae;Ahn, Jae-Hwan;Choi, Won-Suk;Lee, Jungwoo;Oh, Hye-Cheol;Kim, Seog-Ku
    • Journal of Korean Society of Environmental Engineers
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    • v.39 no.12
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    • pp.664-671
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    • 2017
  • Non-point source pollution is the emission source that unspecifically releases pollutants to water system from unspecific places such as cities, agricultural lands, mountains, and construction sites and its discharge path is not easily identified. Also, it is difficult to design and manage the reduction facilities for the emission quantity is primarily affected from weather conditions like rainfall. Since 2006, the significance of non-point source pollution reduction has been grown in Republic of Korea and this reinforces needs for the installation of reduction facilities. However, because the standards for the installation details and reduction efficiency are not clarified by law, people are preferring technologies that do not require particular maintenance and high expenses. The purpose of this study is to examine and maintain the efficiency of non-point source pollutants reduction facility which uses expended polypropylene as a media. The higher the depth of the media, the less range of variations in the reduction efficiency was observed and the final efficiency was also increased. When the media depth was 60 cm, the average reduction efficiency was 94% and 90% where linear velocities were 10 m/hr and 20 m/hr respectively. The results from 180 minutes operation in 10 m/hr and 20 m/hr of linear velocities were slightly different in head loss changes which were caused by media depth variations. The backwash experiments which were conducted in triplicate showed the reduction efficiency decreased as the time went on because of the media clogging. However, it was found that after the backwashing the reduction efficiency was increased as effective as the efficiency of the initial filtration.