• Title/Summary/Keyword: HNBR

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Life-Time Prediction of HNBR Diaphragm in Oil Reservoir (유압구동장치 동력원용 고무 다이아프램 저유기의 수명 예측 연구)

  • Kim, Sol A
    • Journal of Drive and Control
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    • v.18 no.2
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    • pp.32-37
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    • 2021
  • The piston reservoir is mainly used in hydraulic blow-down system for aerospace engineering. The reservoir is heavy due to both hydraulic cylinder and piston in pressurization. The positive expulsion tank with rubber diaphragm has been mostly applied propellant and fuel tank at low pressure to satellites. To reduce weight, the reservoir that can be used at high pressure with rubber diaphragm was developed. In this research, the prediction of life-time for the rubber diaphragm was implemented through an accelerated life test, as a part of development of new reservoir. Also, the diaphragm was stored in an temperature chamber at the same condition as and operation with hydraulic oil. As a result, the life-time for a rubber diaphragm was successfully evaluated via Arrhenius law and Time-Temperature Superposition based on failure times over temperatures in the accelerated test.

Injection Flow Rate Improvement of Injectors for DME Common-rail Systems (DME 커먼레일 시스템을 위한 인젝터 분사 유량 개선)

  • Lee, G.S.;Shin, S.S.;Park, J.H.
    • Journal of ILASS-Korea
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    • v.18 no.1
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    • pp.55-60
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    • 2013
  • In this study, injection flow rates and material of the solenoid sealing of the injectors were improved for the development of a di-methyl Ether(DME) common-rail system. To deliver the same amount of energy provided by injection pressure of diesel $P_{inj}$ = 160 MPa, the DME injectors need to have larger diameter of nozzle hole and more No. of hole at low injection pressure of $P_{inj}$ = 40~50 MPa. The simplified nozzle flow model, which takes account of nozzle geometry and injection condition, was employed in order to design the concept of a injector nozzle such as No. of hole, diameter of hole and diameter of needle seat, etc. Injection amount and rate were tested by diesel and DME test stand. As a result, the diameter of nozzle hole were enlarged by 0.25 mm. The diameter of the orifice in the high pressure line was increased by 1.0 mm to maintain hydraulic force in the nozzle. The material of the solenoid sealing was changed to HNBR, which was strong against the corrosive. Experimental results showed that the injection amount of the DME injector drastically increased by 191.9% comparison to that of diesel at $P_{inj}$ = 40 MPa.