• Title/Summary/Keyword: Ground Firing Test

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Characteristics on Combustion Mode in Dual Mode Scramjet Engine (이중모드 스크램제트 엔진의 연소모드 특성)

  • Namkoung, HyuckJoon;Shim, ChangYeul;Kim, SunYong;Lee, MinSoo;Park, JooHyon;Kim, DongHwan
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2017.05a
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    • pp.330-335
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    • 2017
  • Recently many studies have been made for the development of propulsion system with wide range flight from supersonic to hypersonic. Dual Mode scramjet engine as a hybrid cycle with advantage of ramjet and scramjet has one combustor. It works under the ramjet mode (subsonic combustion) and scramjet mode (supersonic combustion) respectively. In this study, Experimental results of hot firing tests of dual scramjet engine designed on the condition of Mach 3.5~6 as a flight Mach number are discussed. The tests were carried out on a ground test bench under free stream condition of Mach 6 at 27.6km altitude. In the tests, the adopted design and technological solutions were verified and efficient operation of the dual mode ramjet engine with Kerosene combustion during 5 seconds was demonstrated.

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A Preliminary Configuration Design of Methane/Oxygen Bipropellant Small-Rocket-Engine through Theoretical Performance Analysis (이론성능해석에 의한 메탄/산소 이원추진제 소형로켓엔진의 예비형상설계)

  • Bae, Seong Hun;Jung, Hun;Kim, Jeong Soo
    • Journal of the Korean Society of Propulsion Engineers
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    • v.19 no.3
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    • pp.47-53
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    • 2015
  • Design parameters required for Methane/oxygen bipropellant small-rocket-engine were derived through a theoretical performance analysis. The theoretical performance of the rocket engine was analyzed by using CEA and optimal propellant mixture ratio, characteristic length, and optimal expansion ratio were calculated by assuming chemical equilibrium. A coaxial-type swirl injector was chosen because of its outstanding atomization performance and high combustion efficiency compared to other types of injector and also a bell nozzle with 80% of its full length was designed. The rocket engine configuration with 1.72 MPa of chamber pressure, 0.18 kg/s in total propellant mass flow, and O/F ratio of 2.7 was proposed as a ground-firing test model.

A Study on the estimation of shelf-life and assessment plan of illuminating cartridges for mortar (박격포용 조명탄의 저장수명 예측 및 평가방안 연구)

  • Lee, Jongchan;Lee, Junhyuk;Jung, Hyunsuk
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.21 no.9
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    • pp.291-300
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    • 2020
  • The cartridges used for illuminating a desired point or area are virtually limited in tests and evaluations because of limitations, such as noise during launch, the possibility of fires caused by illuminant charge, and the annual testable quantity. Therefore, to solve these problems, a ground fixed test, which replaces the firing test, or an evaluation method to perform limited tests, can be applied more efficiently. In this paper, the results of an 81mm illuminating cartridge, KM series performed in 2019 were analyzed comprehensively to identify the trends in reliability and quality characteristics and to estimate the shelf life. The shelf life was estimated to be at least 10 years based on the time when the lower confidence level reached 80% at a confidence level of 90%. Considering only major defects, the shelf life can be estimated to be approximately 23 years. On the other hand, the shelf life was estimated to be approximately 11 to 15 years and 25 to 28 years according to the effective illuminating time. Finally, an assessment plan of illuminating cartridges for the mortars was also presented as an improvement plan for an assessment method in the future.