• Title/Summary/Keyword: Gaseous flow

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Measurement of I-TEDA Removal Rate Using QCM in Supercritical Carbon Dioxide (초임계이산화탄소 하에서 QCM을 이8한 I-TEDA의 제거특성 측정)

  • Yoo, Jae-Ryong;Koh, Moon-Sung;Sung, Jin-Hyun;Lee, Jeong-Ken;Park, Kwang-Heon
    • Clean Technology
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    • v.14 no.2
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    • pp.110-116
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    • 2008
  • The radioactive wastes generated from the nuclear industry can be divided into the forms of solid, liquid, or gas. Radioactive methyl iodide, a gaseous radioactive waste, is absorbed by activated carbon with 5 wt% of Trietylenediamine (1,4-diazania-bicycle[2.2.2]octane, TEDA) impregnated on the surface. Methyl Iodide ($CH_3I$) is combined chemically with TEDA (the final product : I-TEDA). To recycle radioactive activated carbon, removal of I-TEDA from activated carbon is needed. A wet method for recycling impregnated active carbon was developed to remove radioactive I-TEDA using an acetonitrile solution, which produces lots of secondary wastes. We suggest the removal of I-TEDA by supercritical carbon dioxide with co-solvents. In this experiment, we used a quartz crystal microbalance (QCM) for measuring the removal rate of the I-TEDA. From the experimental results, methanol was found to be the optimum co-solvent, and the optimum conditions such as temperature, pressure, and co-solvent flow rate were obtained. Possibility of using supercritical fluid in the removal of I-TEDA from radioactive activated carbon was also discussed.

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An Experimental Study on the Fundamental Characteristics of LPG Gas Injections System (LPG 가스분사시스템의 기초특성에 대한 실험적 연구)

  • Jang, Yeol-Sung;Woo, Sung-Dong;Kim, Hyeong-Sig;Park, Chan-Jun;Ohm, In-Yong
    • Journal of Energy Engineering
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    • v.15 no.4 s.48
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    • pp.277-283
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    • 2006
  • In this study, butane 100% was used as fuel to verify the real fuel effect such as vapor pressure variation due to temperature change. A MPI fuel injection system for V-6 engine, which has reverse 'L' type cross section to minimize the possibility of liquid phase injection, was composed and one bank was operated under sequential injection scheme. Flow rate were measured according to injection duration, interval, and pressure. Also occurring of liquid phase injection was monitored with varying vaporizer and fuel rail temperature. The result shows that basic characteristics of injection is a relatively difference between air and LPG injection. Under cold start condition, however, the occurrence of liquid injection becomes more severe as the pressure increases, and sufficiently high temperature both in vaporizer and fuel rail is very important to insure gaseous injection. In addition, the temperature of vaporizer plays more important role in keeping LPG vapor state and the reverse 'L' type cross section of the rail is available to prevent liquid injection.

Recovery of $SF_6$ gas from Gaseous Mixture ($SF_6/N_2/O_2/CF_4$) through Polymeric Membranes (고분자 분리막을 이용한 혼합가스($SF_6/N_2/O_2/CF_4$)로부터 $SF_6$의 회수)

  • Lee, Hyun-Jung;Lee, Min-Woo;Lee, Hyun-Kyung;Choi, Ho-Sang;Lee, Sang-Hyup
    • Membrane Journal
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    • v.21 no.1
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    • pp.22-29
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    • 2011
  • During the maintenance, repair and replacement process of circuit breaker, $SF_6$ reacted with input air in arc discharge, which led to the production of by-product gases (eg, $N_2$, $O_2$, $CF_4$, $SO_2$, $H_2O$, HF, $SOF_2$, $CuF_2$, $WO_3$). Among these various by-product gases, $N_2$, $O_2$, $CF_4$ is major component. Therefore, the effective separation process is necessary to recycle the $SF_6$ gas from the mixture gas containing $N_2$, $O_2$, $CF_4$. In this study, the membrane separation process was applied to recycle the $SF_6$ gas from the mixture gas containing $N_2$, $O_2$, $CF_4$. The concentration of $SF_6$ gas in gas produced from the electric power industry is over than 90 vol%. Therefore, we made the simulated gas containing $N_2$, $O_2$, $CF_4$, $SF_6$ which the concentration of $SF_6$ gas is minimum 90 vol%. From the results of membrane separation process of $SF_6$ gas from $N_2$, $O_2$, $CF_4$ $SF_6$ mixture gases, PSF membrane shown the highest recovery efficiency 92.7%, in $25^{\circ}C$ and 150 cc/min of retentate flow rate. On the other hand, PC membrane shown the highest recovery efficiency 74.8%, in $45^{\circ}C$ and 150 cc/min of retentate flow rate. Also, the highest rejection rate of $N_2$, $O_2$, $CF_4$ is 80, 74 and 58.9% seperately in the same operation condition of highest recovery efficiency. From the results, we supposed the membrane separation process as the effective $SF_6$ separation and recycle process from the mixture gas containing $N_2$, $O_2$, $CF_4$, $SF_6$.

Investigation into Air Pollution in Car Shipping Workshop in Pyeongtaek Port (자동차 선적작업장의 공기오염 실태조사)

  • Kim, Ji-Ho;Won, Jong-Uk;Kim, Chi-Nyon;Roh, Jaehoon
    • Journal of Korean Society of Occupational and Environmental Hygiene
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    • v.16 no.1
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    • pp.44-53
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    • 2006
  • This study purposed to investigate air pollution in car shipping yards and, for this purpose, we selected an outdoor open-air yard and an indoor ramp into the ship and measured the concentrations of sulfur dioxide, nitrogen dioxide, carbon monoxide, PM10, PM2.5 and heavy metals in the air. The results of this study are as follows. No significant difference was observed in temperature and humidity between the outdoor and indoor workshop, and the average air flow was 0.52 m/s in the indoor workshop, which is higher than 0.19 m/s in the outdoor workshop(p<0.01). The average concentrations of sulfur dioxide, nitrogen dioxide, carbon monoxide, PM10 and PM2.5 according to workplace were 0.03 ppm(${\pm}0.01$), 0.03 ppm(${\pm}0.01$), 0.46 ppm(${\pm}0.22$), $39.44{\mu}g/m^3$(${\pm}2.45$) and $5.45{\mu}g/m^3$(${\pm}1.15$) respectively in the outdoor workshop, and 0.15 ppm(${\pm}0.05$), 0.22 ppm(${\pm}0.06$), 8.85 ppm(${\pm}3.35$), $236.39{\mu}g/m^3$(${\pm}58.21$) and $152.43{\mu}g/m^3$(${\pm}35.42$) respectively in the indoor workshop. Thus, the concentrations of gaseous substances in the indoor workshop were 4.9-19.2 times higher than those in the outdoor workshop, and the concentrations of fine dusts were 5.9-27.9 times higher(p<0.01). In addition, according to the result of investigating pollutant concentrations according to displacement and the number of car loaded when shipping gasoline cars into the ship, no significant relation between the number of cars loaded and pollutants was observed in shipping passenger cars, but the concentrations of nitrogen dioxide and carbon monoxide got somewhat higher with the increase of the number of cars loaded(p<0.05). In addition, the concentrations of nitrogen dioxide, carbon monoxide, PM10 and PM2.5 in the air were significantly higher when shipping recreational vehicles, the displacement of which is larger than passenger cars, than when shipping passenger cars(p<0.01). On the other hand, the average heavy metal concentrations of the air in indoor workshop were: lead $-0.05{\mu}g/m^3$(${\pm}0.10$); chromium $-0.90{\mu}g/m^3$(${\pm}0.18$); zinc $-0.38{\mu}g/m^3$(${\pm}0.24$); copper $-0.18{\mu}g/m^3$(${\pm}0.22$); and manganese and cadmium not detected. In addition, the complaining rates of 'asthma,' a major symptom of chronic respiratory diseases, were 18.5% and 22.5% respectively in indoor workers and outdoor workers. Thus the rate was somewhat higher in indoor workers but the difference was not statistically significant. The complaining rates of 'chronic cough' and 'chronic phlegm' were very low and little different between indoor and outdoor workers. The results of this study show that the reason for the higher air pollution in indoor than in outdoor workshop is incomplete combustion of fuel due to sudden start and over-speed when cars are driven inside the ship. In order to prevent high air pollution, efficient management measures should be taken including the observance of the optimal speed, the improvement of old ships and the installation of efficient ventilation system.