• Title/Summary/Keyword: Combustion rate

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Prediction of Isothermal and Reacting Flows in Widely-Spaced Coaxial Jet, Diffusion-Flame Combustor (큰 지름비를 가지는 동축제트 확산화염 연소기내의 등온 및 연소 유동장의 예측)

  • O, Gun-Seop;An, Guk-Yeong;Kim, Yong-Mo;Lee, Chang-Sik
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.20 no.7
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    • pp.2386-2396
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    • 1996
  • A numerical simulation has been performed for isothermal and reacting flows in an exisymmetric, bluff-body research combustor. The present formulation is based on the density-weighted averaged Navier-Stokes equations together with a k-epsilon. turbulence model and a modified eddy-breakup combustion model. The PISO algorithm is employed for solution of thel Navier-Stokes system. Comparison between measurements and predictions are made for a centerline axial velocities, location of stagnation points, strength of recirculation zone, and temperature profile. Even though the numerical simulation gives acceptable agreement with experimental data in many respects, the present model is defictient in predicting the recoveryt rate of a central near-wake region, the non-isotropic turbulence effects, and variation of turbulent Schmidt number. Several possible explanations for these discrepancies have been discussed.

Investigation into Air Pollution in Car Shipping Workshop in Pyeongtaek Port (자동차 선적작업장의 공기오염 실태조사)

  • Kim, Ji-Ho;Won, Jong-Uk;Kim, Chi-Nyon;Roh, Jaehoon
    • Journal of Korean Society of Occupational and Environmental Hygiene
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    • v.16 no.1
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    • pp.44-53
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    • 2006
  • This study purposed to investigate air pollution in car shipping yards and, for this purpose, we selected an outdoor open-air yard and an indoor ramp into the ship and measured the concentrations of sulfur dioxide, nitrogen dioxide, carbon monoxide, PM10, PM2.5 and heavy metals in the air. The results of this study are as follows. No significant difference was observed in temperature and humidity between the outdoor and indoor workshop, and the average air flow was 0.52 m/s in the indoor workshop, which is higher than 0.19 m/s in the outdoor workshop(p<0.01). The average concentrations of sulfur dioxide, nitrogen dioxide, carbon monoxide, PM10 and PM2.5 according to workplace were 0.03 ppm(${\pm}0.01$), 0.03 ppm(${\pm}0.01$), 0.46 ppm(${\pm}0.22$), $39.44{\mu}g/m^3$(${\pm}2.45$) and $5.45{\mu}g/m^3$(${\pm}1.15$) respectively in the outdoor workshop, and 0.15 ppm(${\pm}0.05$), 0.22 ppm(${\pm}0.06$), 8.85 ppm(${\pm}3.35$), $236.39{\mu}g/m^3$(${\pm}58.21$) and $152.43{\mu}g/m^3$(${\pm}35.42$) respectively in the indoor workshop. Thus, the concentrations of gaseous substances in the indoor workshop were 4.9-19.2 times higher than those in the outdoor workshop, and the concentrations of fine dusts were 5.9-27.9 times higher(p<0.01). In addition, according to the result of investigating pollutant concentrations according to displacement and the number of car loaded when shipping gasoline cars into the ship, no significant relation between the number of cars loaded and pollutants was observed in shipping passenger cars, but the concentrations of nitrogen dioxide and carbon monoxide got somewhat higher with the increase of the number of cars loaded(p<0.05). In addition, the concentrations of nitrogen dioxide, carbon monoxide, PM10 and PM2.5 in the air were significantly higher when shipping recreational vehicles, the displacement of which is larger than passenger cars, than when shipping passenger cars(p<0.01). On the other hand, the average heavy metal concentrations of the air in indoor workshop were: lead $-0.05{\mu}g/m^3$(${\pm}0.10$); chromium $-0.90{\mu}g/m^3$(${\pm}0.18$); zinc $-0.38{\mu}g/m^3$(${\pm}0.24$); copper $-0.18{\mu}g/m^3$(${\pm}0.22$); and manganese and cadmium not detected. In addition, the complaining rates of 'asthma,' a major symptom of chronic respiratory diseases, were 18.5% and 22.5% respectively in indoor workers and outdoor workers. Thus the rate was somewhat higher in indoor workers but the difference was not statistically significant. The complaining rates of 'chronic cough' and 'chronic phlegm' were very low and little different between indoor and outdoor workers. The results of this study show that the reason for the higher air pollution in indoor than in outdoor workshop is incomplete combustion of fuel due to sudden start and over-speed when cars are driven inside the ship. In order to prevent high air pollution, efficient management measures should be taken including the observance of the optimal speed, the improvement of old ships and the installation of efficient ventilation system.

A Study on Fuel Characteristics of Mixtures Using Torrefied Wood Powder and Waste Activated Carbon (반탄화 목분과 폐활성탄 혼합물의 복합연료활용을 위한 연료적 특성에 관한 연구)

  • Lee, Chang Goo;Kang, Seog Goo
    • Journal of the Korean Wood Science and Technology
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    • v.43 no.1
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    • pp.135-143
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    • 2015
  • This study evaluated fuel properties of composite materials which were prepared by mixing a waste activated carbon from the used purifier filter with torrefied wood powder. Wood species of the raw material of torrefied wood powder are oak wood (Quercus serrata Thunb. ex Murray) and pine wood (Pinus densiflora Siebold & Zucc). And the treatment conditions used for this study were 300 s, 450 s, and 600 s at $200^{\circ}C$ for the wood roaster. Also, the mixing ratios are 5 : 95, 10 : 90, 15 : 85, 20 : 80, 40 : 60, 60 : 40 and 80 : 20 (waste activated carbon : torrefied wood powder). The fuel properties such as highly heating value (HHV), elementary analysis and ash content were evaluated. The results obtained are followings; 1. Despite the same treatment condition of wood roasting, pine wood has higher carbon contents than oak wood. Therefore, pine wood indicated the optimum carbonization at low temperature and short treatment times. 2. The gross calorific value and ash content increased as the mixing ratio of waste activated carbon increased. 3. Mixtures of the waste activated carbon and torrefied wood powder showed greater gross calorific value than those of the mixtures of waste activated carbon and the untreated wood powder. Also, the pine wood resulted in higher heating value that thaose of the oak wood. 4. When composite fuels that were composed waste activate carbon and wood powder are used, higher temperature conditions are required because the combustion is incomplete at $800^{\circ}C$ and 4 hours. 5. The increasing rate of the gross calorific value of mixtures of waste activated carbon and untreated wood powder is higher than does the mixtures of waste activated carbon and torrefied wood powder. Also, this phenomenon is more obvious for pine woods. Therefore, an optimal mixing ratio of waste activated carbon was determined to be between 5% and 10% (wt%). Also, this condition satisfied the requirement of the No.1 grade of wood pellet.