• 제목/요약/키워드: Combustion Noise

검색결과 186건 처리시간 0.025초

맥동류의 연소소음 연구 (Study on Combustion Noise of Unsteady Flow)

  • 양영준;도승주
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2014년도 추계학술대회 논문집
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    • pp.355-357
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    • 2014
  • The usefulness of unsteady combustion was experimentally investigated using confined premixed flames stabilized by a rearward-facing step. For this purpose, apparatus of forced pulsating mixture supply, which could be modulated its amplitude and frequency, was designed. The unsteady combustion used in this experiment plays an important role in controlling self-excited combustion oscillations and furthermore it exhibits desirable performance, from a practical point of view, such as high load combustion and reduction of pollutant emission like nitric oxide.

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가스터빈 연소기에서 엔트로피파에 대한 고찰 (Review of Entropy Wave in a Gas Turbine Combustor)

  • 김대식;윤명곤
    • 한국연소학회지
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    • 제23권1호
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    • pp.28-35
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    • 2018
  • Entropy waves(or hot spots) in a gas turbine combustor are generated by irregular heat release from flames, then can be coupled with acoustic waves when they are accelerated at the exit of the combustor. This coupling mechanism between the entropy and the acoustic waves is generally known to be one of the triggers for combustion instability, which is commonly called "indirect" combustion noise. This paper reviews the fundamental theories on generation, propagation, and coupling with acoustic field of entropy waves and recent research results on the indirect combustion noise for gas turbine combustors.

디지탈 신호처리 기법을 이용한 맥동연소기의 소음원 규명에 관한 연구 (Noise Source Identification of a Pulse Combustion Burner Using Digital Signal Processing Techniques)

  • 김도원;조정길;이관수;오재응
    • 설비공학논문집
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    • 제3권2호
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    • pp.103-113
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    • 1991
  • This paper presents a method for estimating the noise source contribution of a pulse combustion burner in a multiple input system where the input sources may be coherent each other. By coherence function method, it is found that the biggest part of the noise source in the pulse combustion burner is generated by the part of the combustion chamber. This analysis is modeled as three input / single output system because the noise generating mechanism of the pulse combustion burner is very complicated. The coherence function method is proved to be useful tool for the identification of noise source. The overall levels of the radiated source pressure by coherence function method are compared with those measured and calculated by the frequency response function approach. The experimental results have shown a good agreement with the results calculated by the coherence function method when the input sources are coherent strongly each other. The estimation of shield effect by FRF method indicates that significant reduction can be achieved in sound radiation if only transmission path generated by the part of combustion chamber is acoustically shield.

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발전용 보일러의 후부 전열면 소음진동 저감에 관한 사례 연구 (A Case Study on The Reduction and Examination for Noise and Vibration of Backpass Heat Surface in the Power Plant Boiler)

  • Lee, Gyoung-Soon;Lee, Tae-Hoon;Moon, Seung-Jae;Lee, Jae-Heon
    • 한국전산유체공학회:학술대회논문집
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    • 한국전산유체공학회 2008년도 춘계학술대회논문집
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    • pp.642-647
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    • 2008
  • The boiler structure is determined by combustion characteristics and construction costs in the combustion chamber of a large commercial boiler. The heat transfer in boiler is composed of the radiation and the convection. The convective heat transfer has happened to back-pass heating surface. The combustion gas sequentially passes through the reheater tube, 1st economizer tube, and 2nd economizer tube. In case of being lowered in boiler height, we have to install additional tube bundle in back-pass heating surface for increasing the heat transfer of boiler, which causes the noise and vibration from combustion gas. When the combustion gas passes through the back-pass tube bundle in specified load of commercial boiler, this paper analyzes the acoustic characteristics between vortex-shedding frequency and natural frequency in tube bundle cavity. The case study reduce the resonance by changing natural frequency characteristics of tube-bundle cavity using a way to install ant-noise baffle in the direction of combustion gas flow.

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대형 디젤엔진의 소음 개선에 대한 기초 연구 (Basic Study on the Performance Improvement of HD Diesel Engine)

  • 김규철;이삼구;주봉철;노병준
    • 한국자동차공학회논문집
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    • 제9권1호
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    • pp.181-188
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    • 2001
  • The evaluation of the noise for the an existing engine was carried out to improve the current noise level. The applied techniques were 1m air-borne noise, combustion noise analysis, torsional analysis at the front pulley and sound pressure intensity. In addition, the evaluation of the possibility to the noise reduction by means of wrapping the parts was performed to propose the detailed information in engine design. In view of the obtained results, the following countermeasures were recommended to reduce the current noise level through the above methods. Furthermore, in order to assess the influence of combustion noise on the overall engine noise, the noise test was also performed by the change of intake air temperature up to 5$0^{\circ}C$ in steps of 1$0^{\circ}C$. Finally, the fixed design specifications to reduce the engine noise will be decided in consideration of the test data for proto type engine.

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화력 발전용 시험연소로의 연소시험 중의 연소진동 실험(I) (Experiments of Combustion Vibration in the Pilot Furnace for Fossil Power Plant under Combustion Test (I))

  • 주영호;김철홍
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2004년도 추계학술대회논문집
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    • pp.341-344
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    • 2004
  • This paper presents results of test for combustion vibration in the pilot furnace for fossil power plant under combustion test. We measured static pressure variation in the pilot furnace together with air and fuel flow. From test results, it shows that vibration magnitude is affected by air and fuel flow. Also, a finite element analysis using a commercial S/W is performed to calculate acoustic mode of the pilot furnace. These results show that dominant frequency occurred is related to acoustic natural frequency of furnace. After this, it needs to be studied the relation between dominant frequency of combustion vibration and air flow rate.

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대형 디젤 엔진에서 최적 성능 도출을 위한 연료 분사 전략에 관한 연구 (Fuel Injection Strategy for Optimized Performance in Heavy-Duty Diesel Engine)

  • 이진우
    • 한국산학기술학회논문지
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    • 제20권10호
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    • pp.33-39
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    • 2019
  • 대형 디젤 엔진에서 NOx, Smoke 등의 배기가스 저감과 연비를 개선하는 것은 주요한 개발 목표이다. 이 목표를 달성하기 위한 다양한 방식 중 연료를 분할하여 분사하는 다단 분사 전략은 주요하게 적용되고 있다. 본 연구에서는 다양한 조건의 다단분사 전략을 적용하여 배기가스, 연비 그리고 연소 소음 관점에서 최적의 성능을 확보할 수 있는 조건을 확인하여 개선정도를 확인하고자 하였다. 1단 파일럿 적용 시, 단일 분사 대비 NOx 저감이 가능한 영역이 있으나, Smoke가 악화되는 문제가 확인되었다. 2단 파일럿 적용 시, 최대 NOx와 Smoke를 각각 73%, 84%까지 저감할 수 있었다. 연소 소음은 최대 압력 상승률 분석을 통해, 또한 연료소비율은 도시 연료 소비율을 계산하여 단일 분사와 비교하여 개선수준을 평가하였다. 이를 통해 15%:15% 2단 파일럿 전략 적용 시, 단일 분사 대비 NOx 32.9%, Smoke 60.4%, 연비 1.95%, 연소소음 19.3%의 개선을 이룰 수 있음을 확인하였다. 향후, 본 연구 결과를 기반으로 운전 영역을 확장하여 각 조건에서의 최적 연료 분사 방식 도출을 통해 전체적인 성능개선을 구현하고자 한다.

Wiebe 燃燒函數에 의한 디이젤機關 의 燃燒騷音低減 에 관한 硏究 (A Study for Reduction of Combustion Noise in Diesel Engine by Wiebe's Combustion Function)

  • 이성노;궁본등;촌산정;노상순
    • 대한기계학회논문집
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    • 제9권5호
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    • pp.548-554
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    • 1985
  • 본 논문에서는 디이젤기관의 연소소음의 저감을 최종목표로 하여 Wiebe의 연 소함수에 의해 근사시킨 열발생속도의 변화가 디이젤기관의 연소소음 및 도시열효율에 미치는 영향에 관하여 수치실험을 통하여 해석검토하였다.

연소장내 화염계측 오차 평가 (Error Evaluation on Flame Measurement in Combustion Field)

  • 양영준;허태영
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2014년도 추계학술대회 논문집
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    • pp.167-169
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    • 2014
  • Spray combustion has been used in many industrial fields, for instance, such as diesel engines, gas turbines and industrial furnaces, and furthermore various measurement techniques have been applied to elucidate the phenomenon of spray combustion. In order to measure simultaneously the droplet velocity and the droplet size of spray, Phase Doppler Anemometry (PDA) was frequently used in spray combustion. However, the measurement error is occurred due to existence of flame, which is considered as influencing the precision of measurement. Therefore, the purpose of this study is experimentally to conduct the systematic evaluation on the measurement error when PDA measurement is applied to combustion field.

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