• Title/Summary/Keyword: Aero-pulsation Noise

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Development of the Evaluation Method for Aerodynamic Noise Caused by Pressure Pulsation in the Turbocharged Diesel Engine (디젤엔진 공기과급기의 압력맥동 기인소음 평가기법 개발)

  • Lee, Jong-Kyu;Kim, Hyung-Jin;Kang, Koo-Tae
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2007.11a
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    • pp.918-922
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    • 2007
  • Aero-pulsation noise, generally caused by geometric asymmetry of a rotating device, is considerable source of annoyance in passenger cars using the turbocharged diesel engine. Main source of this noise is the compressor wheel in the turbocharger system, and can be reduced by after-treatment such as silencers, but which may increase the manufacturing cost. More effective solution is to improve the geometric symmetry over all, or to control the quality of components by sorting out inferior ones. The latter is more effective and reasonable than the former in view of manufacturing. So, an appropriate discrimination method should be needed to evaluate aero-pulsation noise level at the production line. In this paper, we introduce the accurate method which can measure the noise level of aeropulsation and also present its evaluation criteria. Besides verifying the reliability of a measurement system - a rig test system -, we analyze the correlation between the results from rig tests and those from vehicle tests. The gage R&R method is carried out to check the repeatability of measurements over 25 samples. From the result, we propose the standard specification which can discriminate inferior products from superior ones on the basis of aero-pulsation noise level.

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Measurement and Discrimination Method for the Evaluation of Aero-Pulsation Noise Generated by the Turbocharger System (터보차저의 공기맥동음 평가를 위한 측정 및 판별법)

  • Kim, Jae-Heon;Lee, Jong-Kyu
    • The Journal of the Acoustical Society of Korea
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    • v.26 no.7
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    • pp.361-365
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    • 2007
  • Aero-pulsation noise, generally caused by geometric asymmetry of a rotating device, is one of considerable sources of annoyance in passenger cars using the turbocharged diesel engine. Main source of this noise is the compressor wheel in the turbocharger system, and can be reduced by after-treatment devices such as silencers, but which may increase the manufacturing cost. More effective solution is to improve the geometric symmetry over all, or to control the quality of components by sorting out inferior ones. The latter is more simple and reasonable than the former in view of manufacturing. Thus, an appropriate discrimination method should be needed to evaluate aero-pulsation noise level at the production line. In this paper, we introduce the accurate method which can measure the noise level of aero-pulsation and also present its evaluation criteria. Besides verifying the reliability of a measurement system - a rig test system-, we analyze the correlation between the results from rig tests and those from vehicle tests. The gage R&R method is carried out to check the repeatability of measurements over 25 samples. From the result, we propose the standard specification which can discriminate inferior products from superior ones on the basis of aero-pulsation noise level.

A Study on the Reduction of Pulsations in a 3/4 Open Jet Wind Tunnel (3/4 Open Jet 실차풍동에서의 Pulsation 감소에 관한 연구)

  • Kim Moo-Sang;Kee Jung-Do;Lee Jung-Ho;Jang Jin-Hyuk
    • Proceedings of the KSME Conference
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    • 2002.08a
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    • pp.839-842
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    • 2002
  • Some open jet wind tunnels have been operating under limitations due to large pressure fluctuations at some wind tunnel speeds. The Hyundai Aero-acoustic full scale Wind Tunnel (HAWT), which was completed in 1999, shows that most of the specifications were fulfilled but wind tunnel pulsations at some wind speeds were observed. Hyundai Motor Company started the wind tunnel modification in order to solve this problem in 2001. After the modification work the amplitude of pressure fluctuation was reduced and below required level over full wind speed range. Aero-acoustic performance, e.g. background noise, as well as aerodynamic performance were improved after this work.

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