• 제목/요약/키워드: ASME PTC 코드

검색결과 2건 처리시간 0.015초

오리피스 유량계의 입구 속도 분포에 따른 유량 계측 왜곡 특성 (DISTORTION OF FLOW MEASUREMENT BY VARIOUS INLET VELOCITY PROFILE OF ORIFICE FLOWMETER)

  • 신병수;김남석;이상규;배용범;금오현
    • 한국전산유체공학회:학술대회논문집
    • /
    • 한국전산유체공학회 2011년 춘계학술대회논문집
    • /
    • pp.596-600
    • /
    • 2011
  • In this numerical analysis, the distortion of flow measurement by inlet velocity profile of orifice flowmeter was investigated. To validate the numerical method, the convergence was monitored and the grid dependency was also checked. realizable k-e model was selected and y+ was about 50 in this calculation. the results shows that the pressure at the pressure tab near pipe wall was changed by inclined inlet velocity profile and it leads to distorted a measurement values of flow through the orifice plate from -3.8% to 9%. Therefore, the fully developed inlet flow was required for accurate flow measurement by orifice flowmeter. If not, the orifice plate installed at wrong location should be re-installed or additional actions should be taken.

  • PDF

300MW 태안 IGCC 플랜트 종합성능 특성 (Overall Performance characteristic for 300MW Taean IGCC Plant)

  • 김학용;김재환
    • 한국신재생에너지학회:학술대회논문집
    • /
    • 한국신재생에너지학회 2010년도 추계학술대회 초록집
    • /
    • pp.129.2-129.2
    • /
    • 2010
  • As a part of the government renewable energy policy, KOWEPO is constructing 300MW IGCC plant in Taean. IGCC plant consists of gasification block, air separation unit and power block, which performance test is separately conducted. Overall performance test for IGCC plant is peformed to comply with ASME PTC 46. Major factors affected on the overall efficiency for IGCC plant are external conditions, each block performance(gasification, ASU, power block), water/steam integration and air integration. Performance parameters of IGCC plant are cold gas efficiency, oxygen consumption, sensible heat recovery of syngas cooler for gasification block and purity of oxygen, flow amount of oxygen and nitrogen, power consumption for air separation unit and steam/water integration among the each block. The gas turbine capacity applied to the IGCC plant is 20 percent higher than NGCC gas turbine due to the low caloric heating value of syngas, therefor it is possible to utilize air integration between gas turbine and air separation unit to improve overall efficiency of the IGCC plant and there is a little impact on the ambient condition. It is very important to optimize the air integration design with consideration to the optimized integration ratio and the reliable operation. Optimized steam/water integration between power block and gasification block can improve overall efficiency of IGCC plant where the optimized heat recovery from gasification block should be considered. Finally, It is possibile to achieve the target efficiency above 42 percent(HHV, Net) for 300MW Taean IGCC plant by optimized design and integration.

  • PDF