• Title/Summary/Keyword: 2단 압축 트윈 로타리 압축기

Search Result 2, Processing Time 0.017 seconds

Performance Analysis of a $CO_2$ Two-Stage Twin Rotary Compressor ($CO_2$ 2단 트윈 로타리 압축기 성능해석)

  • Kim, Woo-Young;Ahn, Jong-Min;Kim, Hyun-Jin;Cho, Sung-Oug
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
    • /
    • v.19 no.1
    • /
    • pp.19-27
    • /
    • 2007
  • Analytical investigation on the performance of a two stage twin rotary compressor for $CO_2$ heat pump water heater system has been carried out. A computer simulation program was made based on analytical models for gas compression in control volumes, leakages among neighboring volumes, and dynamics of moving elements of the compressor. Calculated cooling capacity, compressor input, and COP were well compared to those of experiments over the compressor speeds tested. For the operating condition of suction pressure of 3 MPa, and discharge pressure of 9 MPa, and compressor inlet temperature of $35^{\circ}C$, the compressor efficiency was calculated to be 80.2%: volumetric, adiabatic, and mechanical efficiencies were 88.3%, 93.2%, and 92.7%, respectively. For the present compressor model, volumetric and adiabatic efficiencies of the second stage cylinder were lower by about $6{\sim}7%$ than those of the first stage mainly due to the smaller discharge port at the second stage. Parametric study on the discharge port size showed that the compressor performance could be improved by 3.5% just by increasing the discharge port diameter by 20%.

Solubility Consideration in Performance Analysis of a $CO_2$ Twin Rotary Compressor (오일 용해도를 고려한 $CO_2$ 트윈 로타리 압축기 성능해석)

  • Kim, Woo-Young;Ahn, Jong-Min;Kim, Hyun-Jin;Cho, Sung-Oug
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
    • /
    • v.19 no.12
    • /
    • pp.842-849
    • /
    • 2007
  • For a $CO_2$ two-stage twin rotary compressor used for heat pump water heater system, changes of $CO_2$ solubility in PAG oil were investigated along the gas passages from the first stage suction to final discharge. Only slight changes in solubility took place in suction chambers for both of the first and second stages, but for compression chambers, solubility variation ranged from 0.115 to 0.136, and from 0.133 to 0.182, respectively for the first and second stages. Calculation of gas flashing in parts of leakage oil flows and of oil contained in control volumes due to solubility changes was conducted and included in gas pressure calculation. For the second stage, gas flashing amounts to around $5%\sim6%$ for most leakage flows. Cooling capacity, compressor input, and COP obtained by calculation were well compared to the experimental results. Effects of operation speed on the compressor performance was also studied: as the shaft speed increased, adiabatic efficiency decreased rapidly due to increased over-compression loss.