• Title/Summary/Keyword: 희박 연소 엔진

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Effects of Port Masking on Part Load Performance: Part I - Lean Misfire Limit (포트 마스킹이 엔진의 부분부하 성능에 미치는 영향: Part I - 희박연소 한계)

  • 이원근;엄인용
    • Transactions of the Korean Society of Automotive Engineers
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    • v.9 no.5
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    • pp.17-22
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    • 2001
  • This paper is the first of companion papers, which investigate port-masking effects on lean misfire limit. Port-masking was applied to commercial SOHC 3-valve and DOHC 4-valve engine by inserting masking plates between manifold and port. To induce various conditions of stratification, six types of masking plates were applied. The masking plates were placed in the upstream of injector to prevent wall wetting and two ports were not separated to permit both fuel and air entering through masked port. The results were compared with those by conventional port throttling. The results show that lean misfire limit mainly depends on masking direction, that is, high lean misfire limit is achieved when the port near the spark plug is masked. The mechanism of stratification by masking is different from axial stratification by port throttling. In this case, the rich mixture entering through masked port plays a very important role in the stratification process.

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A Study on the Kernel Formation & Development for Lean Burn and EGR Engine (희박연소 및 EGR 엔진에서 초기 화염액 생성 및 성장에 관한 연구)

  • 송정훈;선우명호
    • Transactions of the Korean Society of Automotive Engineers
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    • v.7 no.8
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    • pp.24-33
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    • 1999
  • This paper investigate the effects of the variations of engine operation condition in the flame kernel formation and developmnet . A model for calculating the initial kernel development in spark ignition engines is formualted. It considered input of electrical energy, combustion energy release and heat transfer to the spark plyg, cylinder head, and unburned mixture. The model also takes into accounts strain rate of initial kernel and residual gas fraction. The breakdown process and the subsequent electrical power input initially control the kernel growth while intermediate growth is mainly dominated by diffusion or conduction. Then, the flame propagates by the chemical energy and turbulent flame expansion. Flame kernel development also influenced by engine operating conditions, for example, EGR rate, air-fuel ration and intake manifold pressure.

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Comparison of Lean Combustion Performance in a Spark-Ignition Engine Fueled with Natural Gas and Hydrogen (스파크점화 엔진에서 천연가스와 수소의 희박연소 성능 비교)

  • Park, Hyunwook;Lee, Junsun;Oh, Seungmook;Kim, Changup;Lee, Yonggyu;Kang, Kernyong
    • Journal of ILASS-Korea
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    • v.26 no.4
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    • pp.204-211
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    • 2021
  • Lean combustion performance of natural gas and hydrogen was compared in a spark-ignition engine. The lean combustion engine operation with natural gas was limited due to combustion instability at an excess air ratio (EAR) above 1.8. The total hydrocarbon (THC) emissions increased significantly with increasing EAR. The nitrogen oxides (NOX) emissions were also high due to the limitation of increasing EAR. The lean combustion engine operation with hydrogen showed superior combustion stability as well as low THC and NOX emissions, even at high EARs. However, boosting technology was required to reach the high EARs.

Performance Characteristics of GCH4-LOx Small Rocket Engine According to the Equivalence Ratio Variation at a Constant Pressure of Combustion Chamber (동일한 연소실 압력에서의 당량비 변화에 따른 기체메탄-액체산소 소형로켓엔진의 성능특성)

  • Yun Hyeong Kang;Hyun Jong Ahn;Chang Han Bae;Jeong Soo Kim
    • Journal of the Korean Society of Propulsion Engineers
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    • v.26 no.6
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    • pp.34-42
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    • 2022
  • A correlation between propellant supply condition and chamber pressure in GCH4-LOx small rocket engine was explored and hot-firing tests were conducted to analyze the engine performance characteristics according to the equivalence ratio variation at a constant chamber pressure. Correlation studies have shown that chamber pressure is linearly proportional to oxidizer supply pressure. As a result of the test, the thrust, specific impulse and characteristic velocity that are the main performance parameters of a rocket engine, were found to be enhanced as the equivalence ratio starting from a fuel-lean condition approached the stoichiometric ratio, but the efficiencies of characteristic velocity and specific impulse were on the contrary, in their dependency on the equivalence ratio.

Numerical analysis on performances and emission characteristics of HCCI engine fueled with hydrogen added biogas (반응 메커니즘 기반의 수소 첨가 바이오가스 HCCI 엔진 성능 및 배출가스에 대한 수치 해석적 연구)

  • Park, Jungsoo
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.19 no.12
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    • pp.41-46
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    • 2018
  • In this research, numerical analysis was performed to determine the effects of hydrogen on biogas combustion for homogeneous charged compression ignition (HCCI) engines. The target engine specifications were a 2300cc displacement volume, 13:1 compression ratio, 15kW of electricity, and 1.2 bar boost pressure. The engine speed was fixed to 1800rpm. By varying the excess air ratio and hydrogen contents, the cylinder pressure, nitric oxide, and carbon dioxide were measured as a function of the hydrogen contents. According to preliminary studies related to the reaction mechanism for methane combustion and oxidation, a GRI 3.0 mechanism as the base mechanism was selected for HCCI combustion calculations describing the detailed reaction mechanism. By adding hydrogen, NO was increased while $CO_2$ was decreased. The cylinder pressure was also increased, having advanced timing for the maximum cylinder pressure and pressure rise region. Furthermore, lean operation limits were extended by adding hydrogen to the HCCI engine.

A Study of Flame Visualization of the APU Gas Turbine Engine Sector Combustor (APU용 가스터빈 엔진 분할연소기의 화염가시화 연구)

  • Kim, Bo-Ra-Mi;Choi, Chea-Hong;Choi, Seong-Man
    • Journal of the Korean Society of Propulsion Engineers
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    • v.15 no.4
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    • pp.11-17
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    • 2011
  • In order to see flame behavior in the annular reverse gas turbine combustor, sector combustion test was performed. Ignition test by using torch ignition system was carried out at various combustor inlet velocity and air fuel ratio. Also, flame blow out limit was measured by changing fuel flow rate with constant air mass flow rate. In test results, stable ignition is possible at air excess ratio of 6 and this limit is gradually increased with combustor inlet velocity. The minimum blow out limit is about 4 at 40 m/s of combustor inlet velocity. This blow out limit is also increased up to about 10 with increasing combustor inlet velocity. Test result shows that lean blow out limits are increased with air velocity. The highest blow out limit was found at the combustor inlet velocity of 65 m/s.

A Study of Flame Visualization of the APU Gas Turbine Engine Sector Combustor (APU용 가스터빈 엔진 분할연소기의 화염가시화 연구)

  • Kim, Bo-Ra-Mi;Choi, Chea-Hong;Choi, Seong-Man
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.153-159
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    • 2010
  • In order to see the flame behavior in the annular reverse gas turbine combustor, sector combustion test was performed. Ignition test by using torch ignition system was carried out at the various combustor inlet velocity and air fuel ratio. Also, flame blow out limit was measured by changing fuel flow rate with constant air mass flow rate. In the test results, stable ignition is possible at air excess ratio of 6 and this limit is gradually increased with combustor inlet velocity. The minimum blow out limit is about 4 at 40 m/s of combustor inlet velocity. This blow out limit is also increased up to about 10 with increasing combustor inlet velocity. Test result shows that lean blow out limits are increased with air velocity. The highest blow out limit was found at the combustor inlet velocity of 65m/s.

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Lean Operation Characteristics of a Spark Ignition Engine with Reformed Gas Addition (전기점화 엔진에서 개질가스 첨가에 의한 희박연소특성 연구)

  • Oh, Seung-Mook;Kim, Chang-Up;Kang, Kern-Yong;Choi, Young
    • Transactions of the Korean Society of Automotive Engineers
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    • v.14 no.3
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    • pp.170-177
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    • 2006
  • Hydrogen can extend the lean misfire limit to a large extent when it is mixed with conventional fuels for a spark ignition engine. In this study, hydrogen-enriched gaseous fuels by reforming process were simulated according to their proportions of $H_2$, CO, $CO_2$ and $N_2$ gases. Pure hydrogen and two different hydrogen-enriched gaseous mixtures(A-, B-composition) were tested for their basic effects on the engine performances and emissions in a single cylinder research engine. A- and B-composition showed different results from 100% $H_2$ addition because air/fuel mixtures were more diluted by their additions. Even though the energy fraction of reformed gases was increased, combustion stabilities and lean misfire limits were not sensitively improved. It means that combustion augmentation by $H_2$ addition was offset by the charge dilution of $N_2$ and $CO_2$. In addition, the low flammability of CO gas deteriorated thermal efficiencies. CO emission was drastically increased with B-composition which included higher CO component. However, $NO_x$ was reduced as energy fraction($X_e$) rised except for the case of 100% $H_2$ addition at $\lambda=1.2$ and was, for A-composition, lowered to a factor of ten when compared with that of $H_2$ addition. HC emissions were largely influenced by $COV_{imep}$ due to misfire and partial burns.

Evaluation of EGR applicability for NOx reduction in lean-burn LPG direct injection engine (초희박 LPG 직접분사식 엔진에서 질소산화물 저감을 위한 배기재순환 적용성 평가)

  • Park, Cheolwoong;Cho, Seehyeon;Kim, Taeyoung;Cho, Gyubaek;Lee, Janghee
    • Journal of the Korean Institute of Gas
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    • v.19 no.4
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    • pp.22-28
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    • 2015
  • In order to keep the competitiveness of LPG fuel for transportation fuel, the difference in fuel consumption with gasoline and cost for an aftertreatment system should be reduced with continuous development of technology for LPG engine. In the present study, spray-guided type direct injection combustion system, whose configuration is composed of direct injector in the vicinity of spark plug, was employed to realize stable lean combustion. A certain level of nitrogen oxides($NO_x$) emits due to a locally rich mixture regions in the stratified mixture. With the application of EGR system for the reduction of $NO_x$, 15% of $NO_x$ reduction was achieved whereas fuel consumption and hydrocarbon emission increased. By the application of EGR, the combustion speed reduced especially appeared at initial flame development period and peak heat release rates and increasing rates for heat release rate decreased as EGR rate increased due to the dilution effect of intake air.

A Study on the Lean Combustion Characteristics with Variation of Combustion Parameter in a Gasoline Direct Injection Engine (직접분사식 가솔린 엔진의 연소제어인자에 따른 희박연소 특성 연구)

  • Park, Cheol-Woong;Oh, Jin-Woo;Kim, Hong-Suk
    • Transactions of the Korean Society of Automotive Engineers
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    • v.20 no.4
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    • pp.39-45
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    • 2012
  • Today gasoline engines for vehicular application are not only faced with stringent emission regulation but also with increasing requirements to better fuel economy, while guaranteeing power density. The spray-guided type gasoline direct injection (GDI) engine has an advantage of improved thermal efficiency and lower harmful emissions. Centrally mounted high pressure injector and adjacent spark plug allow stable lean combustion due to the flexible mixture stratification. In the present study, the performance and emissions characteristics of developed spray-guided type GDI combustion system were evaluated at various excess air ratio conditions. The specific fuel consumption and nitrogen oxides ($NO_x$) emissions were reduced due to the achievement of stable lean combustion under flammability limit. Multiple injection strategy was not helpful to improve fuel consumption while further reduction of $NO_x$ emissions was possible.