• Title/Summary/Keyword: 탱크 운전

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변환시설 발생 해체금속폐기물의 용용제염처리

  • Hwang, Du-Seong;Kim, Dong-Ho;Lee, Gyu-Il;Choe, Yun-Dong;Park, Jin-Ho;Jeong, Un-Su
    • Proceedings of the Korean Radioactive Waste Society Conference
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    • 2009.06a
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    • pp.63-64
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    • 2009
  • 변환시설의 해체 시 발생한 해체폐기물은 2009년 현재까지 약 354톤이며, 이들 중 탱크, 배관, 반응기, 펌프류 동의 해체금속폐기물이 약 191톤으로 54% 를 차지하고 있다. 이들 해체금속폐기물은 제염 처리공정을 통하여 전량 자체처분폐기물로 전환시키는 것을 목표로 두고 있다. 이는 오염된 금속류를 효과적으로 제염한 다음 자체처분시킴으로서 방사성폐기물에 대한 처분비용을 저감할 수 있기 때문이다. 해체금속폐기물 중 스테인레스강 해체폐기물은 질산 용액을 사용한 초음파화학제염공정으로 제염한 후 자체처분폐기물로 53톤을 전환하였다. 탄소강 해체물의 경우 스팀제염공정으로 제염한 결과 제영 효율은 좋았으나 변환시설 가동 중 유지 보수를 위하여 페인팅을 하였던 해체물의 경우 페인트를 제거하지 않을 경우 스팀제염장치로는 제염이 안 되었다. 탄소강 해체금속폐기물은 약 117톤 발생하였으며, 이들 중 모터, 펌프 등을 제외한 제염 대상 폐기물은 약 80톤이며, 이들을 용융 제염 및 감용을 위하여 기초 연구를 수행한 결과를 바탕으로 약 180kg/batch 용량의 금속용융제염 설비를 제작 설치하여 탄소강 해체금속폐기물 용융제염 처리를 수행 중에 있다. 금속용융은 장치가 간단하고 폐기물 처리량이 비교적 적고 단속적인 운전에 매우 효과적인 고주파 유도로를 사용하였다. 용융장치는 고주파 발진장지와 용해로체로 구성된 고주파 유도설비와 냉각계통으로 구성된다. 고주파발진장치는 철제 200kg을 용해할 수 있는 용량을 갖추었으며, 실험 및 실제 처리 등 용해로체의 크기 변경이 필요할 경우에는 고주파발진기의 출력 주파수를 변경할 수 있게 하였다. 용융 장치의 발진기 부분의 입력전원은 3상, 440V, 60Hz 이며, 출력전원은 200kW, 출력주파수는 lkHz, 3kHz, 5kHz로 구성되어 있으며, 회당 180kg 의 폐기물을 용융할 시에는 3kHz로 고정하여 사용하였다. 용해로체 부분 중 고주파유도가열부는 heating coil 및 절연부로 구성되어 있고, 그 외 support frame과 lever로 구성되어 있다. 용해로체와 고주파 발진장치의 냉각을 위한 냉각설비는 냉각기와 냉매의 저장을 위한 저장조로 구성되어 있으며, 냉각기의 용량은 20RT 이다. 용융로체의 직경은 약 28cm로 크기가 큰 해체물의 장입이 어려워 작은 크기로 세절을 해야만 하며,용융로의 용량을 증가시킬 경우 해체물을 작은 크기로 세절하는 비용을 절감할 수 있을 것이다. 용융 중 시료 채취는 매 배치마다 수행하였으며, 그림3과 같은 시료 채취용 주형 틀에 국자모양의 채취기로 채취하였다. 해체물의 용융시 ingot를 생성하기 위해서 주형틀에 용융물을 장입하기 전 시료를 채취하였다 그림4는 생성된 ingot이며, 이들의 방사능 농도는 배치마다 차이는 있지만 최대 0.05 Bq/g 이하로 나타나 자체처분 폐기물로 전량 전환 가능하였다 그림5 는 해체물에 함유된 우라늄과 불순물을 제거한 슬래그로 방사능농도는 약 12Bq/g 으로 나타났으며, 이들의 발생량은 약 3wt% 정도로 폐기물 발생량이 작았다. 따라서 금속폐기물의 경우 용융제염으로 처리할 경우 폐기물 발생량을 최대로 줄일 수 있어 처리 효율이 기타 처리 공정보다 효율적인 것으로 판단된다.

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A Study on Management of Seafood Wastewater Treatment Facility using Submerged MBR (침지식 MBR을 이용한 수산물 폐수처리장 운영에 관한 연구)

  • Choi, Yong-Bum;Lee, Hae-Seung;Han, Dong-Joon;Kwon, Jae-Hyouk
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.16 no.11
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    • pp.7227-7236
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    • 2015
  • The survey revealed that, due to the discharge characteristics of seafood wastewater, irregular inflow loads were caused, making it difficult to treat the wastewater safely. It is crucial for the operation of pressure and floating tanks for the treatment of high-concentration organic wastewater such as seafood wastewater. The survey of operation factors for the pressure and floating tanks revealed this: A/S ratio 0.05 (design criteria 0.01), the pressurized air pressure 8bar(design criteria 6bar), the pressure tank pressure 6bar (design criteria 4.5bar), and HRT 60sec(design criteria: 10sec). Also, the recirculation rate was changed to over 40%(design criteria: 30%), and the surface load rate was changed to under $13.7m^3/m^2{\cdot}hr$(design criteria: under $17.7m^3/m^2{\cdot}hr$); thus, compared to the initial design criteria, the operation factors were changed according to inflow characteristics, thus enhancing the pressure and floating tank performance. The survey of inflow load revealed BOD 140.7%, $COD_{Mn}$ 120.32%, and SS 106.3%, compared to the inflow design criteria, as well as T-N 135.5% and T-P173.3%, higher than the design criteria. The survey of the treatment facility annual operation cost revealed high portions in sludge treatment cost(27.7%) and chemicals costs(26.0%), and the sludge treatment cost will likely further increase due to the ban on ocean dumping. The unit cost for the treatment of seafood wastewater was found to be KRW 3,858 per ton, more than 27 times higher than the sewage treatment cost(KRW 142.6/ton), presumably because the seafood wastewater contains high-concentration organic substances and nutritive salts.

Evaluation of $^{14}C$ Behavior Characteristic in Reactor Coolant from Korean PWR NPP's (국내 경수로형 원자로 냉각재 중의 $^{14}C$ 거동 특성 평가)

  • Kang, Duk-Won;Yang, Yang-Hee;Park, Kyong-Rok
    • Journal of Nuclear Fuel Cycle and Waste Technology(JNFCWT)
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    • v.7 no.1
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    • pp.1-7
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    • 2009
  • This study has been focused on determining the chemical composition of $^{14}C$ - in terms of both organic and inorganic $^{14}C$ contents - in reactor coolant from 3 different PWR's reactor type. The purpose was to evaluate the characteristic of $^{14}C$ that can serve as a basis for reliable estimation of the environmental release at domestic PWR sites. $^{14}C$ is the most important nuclide in the inventory, since it contributes one of the main dose contributors in future release scenarios. The reason for this is its high mobility in the environment, biological availability and long half-life(5730yr). More recent studies - where a more detailed investigation of organic $^{14}C$ species believed to be formed in the coolant under reducing conditions have been made - show that the organic compounds not only are limited to hydrocarbons and CO. Possible organic compounds formed including formaldehyde, formic acid and acetic acid, etc. Under oxidizing conditions shows the oxidized carbon forms, possibly mainly carbon dioxide and bicarbonate forms. Measurements of organic and inorganic $^{14}C$ in various water systems were also performed. The $^{14}C$ inventory in the reactor water was found to be 3.1 GBq/kg in PWR of which less than 10% was in inorganic form. Generally, the $^{14}C$ activity in the water was divided equally between the gas- and water- phase. Even though organic $^{14}C$ compound shows that dominant species during the reactor operation, But during the releasing of $^{14}C$ from the plant stack, chemical forms of $^{14}C$ shows the different composition due to the operation conditions such as temperature, pH, volume control tank venting and shut down chemistry.

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Water Quality Improvement of Stagnant Water using an Upflow Activated Carbon Biofilm Process and Microbial Community Analysis (상향류 활성탄 생물막 공정을 이용한 정체 수역 수질 개선 및 공정 내 미생물 군집 해석)

  • Oh, Yu-Mi;Lee, Jae-Ho;Park, Jeung-Jin;Choi, Gi-Choong;Park, Tae-Joo;Lee, Tae-Ho
    • Journal of Korean Society of Environmental Engineers
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    • v.32 no.1
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    • pp.23-32
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    • 2010
  • The capacity of natural purification was limited by the interruption of natural flow and the problems such as eutrophication were occurred by nutritive salts accumulation in stagnant stream. Moreover, the inflow of non-point sources causes non-degradable materials to increase in stagnant stream. In this study, an upflow biological activated carbon (BAC) biofilm process comprised of anoxic, aerobic 1, and aerobic 2 reactors were introduced for treatment of stagnant stream and SS, $BOD_5$, $COD_{Mn}$, $COD_{Cr}$, TN, and TP were monitored in the upflow BAC biofilm reactors with continuous cycling. In order to simulate stagnant stream, the lake water of amusement park and golf course were stored as influent in a tank of $2m^3$ and hydraulic retention time (HRT) was changed into 6, 4, and 2 hours. At HRT 4hr and the lake water of amusement park as influent, the removal efficiencies of SS, $BOD_5$, $COD_{Mn}$, $COD_{Cr}$, TN, and TP showed the best water quality improvement and were 69.8, 83.0, 91.3, 74.1, 74.7, and 88.9%, respectively. At HRT 4hr and the lake water of golf course as influent, the removal efficiencies of SS, $BOD_5$, $COD_{Mn}$, $COD_{Cr}$, TN and TP were 78.5, 78.0, 80.2, 74.9, 55.6 and 97.5%, respectively. As the results of polymerase chain reaction - denaturing gel gradient electrophoresis (PCR-DGGE), microbial community was different depending on influent type. Fluorescence in situ hybridization (FISH) showed that nitrifying bacteria was dominant at HRT 4 hr. The biomass amount and microbial activities by INT-DHA test were not decrease even at lower HRT condition. In this study, the upflow BAC biofilm process would be considered to the water quality improvement of stagnant stream.

Project of Improving Good Agriculture Practice and Income by Intergrated Agricultural Farming (미얀마 우수농산물 재배기술 전수사업)

  • Lee, Young-Cheul;Choi, Dong-Yong
    • Journal of Practical Agriculture & Fisheries Research
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    • v.16 no.1
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    • pp.193-206
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    • 2014
  • The objectives of the project are to increase farmers' income through GAP and to reduce the loss of agricultural produce, for which the Korean partner takes a role of transferring needed technologies to the project site. To accomplish the project plan, it is set to implement the project with six components: construction of buildings, installation of agricultural facilities, establishment of demonstration farms, dispatching experts, conducting training program in Korea and provision of equipments. The Project Management Committee and the Project Implementation Team are consisted of Korean experts and senior officials from Department of Agriculture, Myanmar that managed the project systematically to ensure the success of the project. The process of the project are; the ceremony of laying the foundation and commencing the construction of training center in April, 2012. The Ribbon Cutting Ceremony for the completion of GAP Training Center was successfully held under PMC (MOAI, GAPI/ARDC) arrangement in SAl, Naypyitaw on June 17, 2012. The Chairman of GAPI, Dr. Sang Mu Lee, Director General U Kyaw Win of DOA, officials and staff members from Korea and Myanmar, teachers and students from SAl attended the ceremony. The team carried out an inspection and fixing donors' plates on donated project machineries, agro-equipments, vehicles, computers and printer, furniture, tools and so forth. Demonstration farm for paddy rice, fruits and vegetables was laid out in April, 2012. Twenty nine Korean rice varieties and many Korean vegetable varieties were introduced into GAP Project farm to check the suitability of the varieties under Myanmar growing conditions. Paddy was cultivated three times in DAR and twice in SAl. In June 2012, vinyl houses were started to be constructed for raising seedlings and finished in December 2012. Fruit orchard for mango, longan and dragon fruit was established in June, 2012. Vegetables were grown until successful harvest and the harvested produce was used for panel testing and distribution in January 2013. Machineries for postharvest handling systems were imported in November 2012. Setting the washing line for vegetables were finished and the system as run for testing in June 2013. New water tanks, pine lines, pump house and electricity were set up in October 2013.