• Title/Summary/Keyword: 와류 진동 모드

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Study on Unsteady Flow Field around Rectangular Cylinders using Proper Orthogonal Decomposition (POD) (POD를 이용한 구조기본단면 주변 비정상흐름장 특성에 관한 연구)

  • Lee, Jae-Hyung;Matsumato, Masaru
    • Journal of Korean Society of Steel Construction
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    • v.20 no.6
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    • pp.751-759
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    • 2008
  • In this study, the effect of an unsteady flow field around a body of aerostatic/aerodynamic forces were investigated using rectangular cylinders (B/D = 2, 3, 4, 5). Proper orthogonal decomposition (POD) was introduced to the analysis of the fluctuating pressure field that was measured on the stationary/oscillatory B/D=4 rectangular cylinder, and the characteristics of the proper functions with flow patterns were identified. In addition, the physical decoupling and interactions in the different co-existing flow patterns were investigated through POD. The comparison with the identified proper function associated with a particular flow pattern revealed that the Karman vortex is almost not affected by the separation bubble, but that the Karman vortex considerably interferes in the development of the separation bubble around the trailing edge. It can be considered that the Karman vortex induces the increment of the curvature of the substantial separated flow.

FEM acoustic modal analysis due to location of acoustic baffles to avoid acoustic resonance in the tube bank of boiler for power plant (보일러 튜브군의 음향공진 회피를 위한 음향배플의 위치에 따른 FEM 음향모드해석)

  • Ahn, Sung-Jong;Ju, Young-Ho;Kim, Cheol-Hong
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2012.04a
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    • pp.150-154
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    • 2012
  • A flow induced mechanical vibration and acoustic resonance should be considered at design stage because they are mainly occurred in the tube bank of boiler. Acoustic resonance is occurred when the vortex shedding frequency of tube bank coincides with the acoustic natural frequency of the cavity. Effective solution to avoid acoustic resonance is installing acoustic baffles in the tube banks parallelly inside of the flow cavity. Thus, location and number of acoustic baffles should be exactly calculated to eliminate the acoustic resonance. This paper presents case study of acoustic resonance due to inappropriate number and location of acoustic baffles. Measured frequency and mode in the study is verified by FEM acoustic modal analysis. The number and location of acoustic baffles to avoid acoustic resonance are calculated by using FEM acoustic modal analysis.

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Dynamic Response Analysis of Top-tensioned Riser Under Sheared Current Load (전단류 하중을 받는 상부장력 라이저의 동적 응답 해석)

  • Kim, Kookhyun
    • Journal of Ocean Engineering and Technology
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    • v.27 no.4
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    • pp.83-89
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    • 2013
  • A numerical scheme based on a mode superposition method is presented for the dynamic response analysis of a top-tensioned riser (TTR) under sheared current loads. The natural frequencies and mode shapes of the TTR have been calculated analytically for a beam with a slowly varying tension and pinned-pinned boundary conditions at the top and bottom ends. The lift coefficients and corresponding amplitudes used to estimate the vortex-induced modal force and damping for each mode were predicted via iterative calculations based on the input and output power balancing concept. Here, the power-in regions were controlled by the normal distribution function, for which the center was coincident with the lock -in location by local vortex-shedding, and the range was defined by the constant standard deviation for the reduced velocity by the local current speed. Finally, dynamic responses such as root-mean-squared displacement and stress were calculated using the mode superposition technique. In order to verify the presented scheme, a numerical calculation was performed for a TTR under an arbitrary linearly sheared current and linearly varying tension. A comparison with the results of the existing software showed that the presented scheme could give reliable and feasible solutions. Case studies were performed to investigate the effects of various current loads and tensions.

Application of proper orthogonal decomposition on cylinder wake (원기둥 후류에 대한 적합 직교 분해법 적용)

  • Ree, Kwan Ho;Hwang, Jin Hwan
    • Proceedings of the Korea Water Resources Association Conference
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    • 2022.05a
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    • pp.256-256
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    • 2022
  • 레이놀즈 분해법은 유속을 비롯한 변수를 평균 성분과 변동 성분으로 분해하는 분석 방법으로, 난류 분석의 기본이 되는 방법이다. 그러나 유체 내에 장애물이 존재할 경우, 흐름에 큰 와류가 존재하여 난류 변동 성분과 구분되는 고유 구조가 형성되는데, 이러한 경우에 레이놀즈 분해법을 적용하면 고유 구조의 변동 성분이 난류로 처리되어 난류 강도가 과다하게 책정될 수 있다는 한계점이 있다. 이에 대한 대안으로 제안된 것이, 변수를 평균 성분, 파동 성분, 변동 성분으로 분해하는 삼중 분해법이다. 삼중 분해법은 흐름 내의 고유 구조를 추출하는 것을 가능하게 하여 다양한 연구에서 사용되어왔다. 삼중 분해법을 구현하기 위해 이용되는 방법론 중 하나로, 공분산 행렬을 이용하여 유속장을 분해하는 방법인 적합 직교 분해법이 많이 사용된다. 본 연구에서는 원기둥 후류에 적합 직교 분해법을 사용하여 삼중 분해법을 시행하고, 후류의 흐름 구조를 분석하는 것을 목표로 하였다. 영상 유속계를 사용하여 실험을 통해 원기둥 후류의 수평 유속장을 측정하였고, 측정 자료에 적합 직교 분해법을 적용한 결과, 첫 두 모드에서 큰 규모의 와류가 파동 형태로 전파되는 것이 관찰되어 고유 구조의 존재를 확인할 수 있었다. 해당 성분을 삼중 분해법의 파동 성분으로 상정하였고, 푸리에 분석을 적용한 결과에서도 원기둥 후류의 고유 진동수가 뚜렷하게 나타나는 것을 확인하였다. 또한, 원기둥 후류의 에너지 전달 구조를 확인하기 위하여 에너지 방정식에 삼중 분해법을 적용하여 식을 유도하고, 실험 자료로부터 각 항을 계산하여 비교해보았다.

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Low frequency Instability in Hybrid Rocket Post-chamber Configuration (연소실 형상 변화에 의한 하이브리드 로켓의 저주파수 연소불안정)

  • Park, Kyungsu;Lee, Changjin
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.42 no.1
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    • pp.29-36
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    • 2014
  • Hybrid rocket displays many different low frequency pressure oscillations during combustion. Thermal lag between solid and gas phase is the primary mechanism to trigger low frequency pressure oscillations of around 10Hz, and Helmholtz or $L^*$ mode also produces other types of low frequency oscillations above 10 Hz which is associated with the change in combustion volume. Since the flow characteristics in hybrid rocket is very similar to those in solid rocket combustion, it is not surprising to observe similar pressure oscillation behaviors. Experimental test shows that combustion pressure suddenly turns into to a big amplitude oscillation around 10Hz then followed by returning to an original pressure level after a short period combustion. Further investigations show that this instability is independent of the change in O/F ratio at all. One of the possible candidates is the vortex shedding dynamics over the backward step in the post combustion chamber. It is required to investigate the low frequency oscillation mechanism in the future study.