• Title/Summary/Keyword: 연료 그레인

Search Result 43, Processing Time 0.02 seconds

Development and Performance Analysis of Gas Generator with Plunger-type Flow Control Valve for Ducted Rocket : Part II (Plunger 타입 유량조절장치를 적용한 덕티드 로켓용 가스발생기 개발 및 성능분석 : Part II)

  • Han, Seongjoo;Lee, Jungpyo;Cho, Sungbong;Khil, Taeock;Kim, Minkyum
    • Journal of Aerospace System Engineering
    • /
    • v.15 no.3
    • /
    • pp.87-92
    • /
    • 2021
  • In this study, a numerical approach was utilized to observe the phenomena in the ground combustion test of a gas generator for a ducted rocket with a plunger-type flow control device. The design factors were also identified through the analysis. It was observed that the pressure increase without the adhesion of the combustion product at the discharge pipe was quite similar to the analysis assuming a cone-shaped erosive burning effect. The pressure increase in most cases was similar to the analysis results when assuming the change in discharge pipe area due to the adhesion of combustion products. Moreover, it was also established that for a given grain shape and discharge flow area, the effect of the adhesion of combustion products has a significant effect on the combustion chamber pressure for cases over n=0.45.

Combustion Characteristics and Performance Prediction of PE-GOX Hybrid Rocket Motor Part II : Internal Ballistic Performance (PE-GOX 하이브리드 모터의 연소특성 및 성능 예측 기법 Part II : 내탄도 성능)

  • Yoon, Chang-Jin;Song, Na-Young;Yoo, Woo-Jun;Jeon, Chang-Soo;Kim, Jin-Kon;Moon, Hee-Jang;Sung, Hong-Gye
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.11 no.2
    • /
    • pp.79-85
    • /
    • 2007
  • An internal ballistic model to predict the performance of a Polyethylene-GOX (PE-GOX) hybrid motor was proposed and evaluated. A theoretical treatment of the model was followed by detail discussion of each of the factors affecting the overall performance. The present model consists of the governing equations by considering the unsteady burn-back rate of the fuel grain and on-off response characteristics of a oxygen-supply valve. The numerical results using the 4th order Runge-Kutta scheme with temporal physicochemical properties showed good agreements with test results and the global effects of the performance parameters, such as the burning area of the fuel grain, O/F ratio, and etc., on the performance of the motor were analyzed.

Manufacture & Launch of Small PE/$LN_2O$ Hybrid Rocket with 50 kgf Thrust Level (추력 50 kgf 급 PE/$LN_2O$ 소형 하이브리드 로켓 제작 및 시험발사)

  • Kim, Hyeon-Woo;Jeon, Min-Ho;Oh, Ji-Sung;Han, See-Hee;Kang, Min-Seok;Jang, Hyoung-Gui;Kim, Hee-Yong;Bae, Tae-Hyun;Lee, Sun-Jae;Kim, Jin-Kon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2009.11a
    • /
    • pp.507-510
    • /
    • 2009
  • The small size of hybrid rocket using PE-$LN_2O$ was designed, constructed and launched for a development basic technology of Hybrid rocket vehicle. The hybrid engine ignition system was designed with valve system using external actuator and confirmed working without any fault. To design fuel grain an internal ballistics design was carried out, and to estimate rockets flight path an external ballistics analysis was carried out. So the rocket was designed and constructed, and the launch test proves that hybrid rocket's design was suitable. The hybrid rocket(weight : 9kg, diameter : 110 mm, height : 1.7 m) was launched successfully. But parachute was deployed on mid-flight and the mission could not finish its purposed flight. Some of problems were found in this activity but next launch vehicle will be improved.

  • PDF