• Title/Summary/Keyword: 설계 이상 현상

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The Actual Conditions and Improvement of the Eco-Forests Mater Plan, South Korea (우리나라 생태숲조성 기본계획 실태 및 개선방향)

  • Heo, Jae-Yong;Kim, Do-Gyun;Jeong, Jeong-Chae;Lee, Jeong
    • Korean Journal of Environment and Ecology
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    • v.24 no.3
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    • pp.235-248
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    • 2010
  • This study was carried out to the actual conditions and improvement of the eco-forests master plan in South Korea, and suggested its problems and improvement direction. Results from survey and analysis of limiting factors or constraints in the construction plans of eco-forests in Korea revealed that there were highly frequent problems involving site feasibility, topographic aspect, and existing vegetation. The results of survey on the status of land use indicated that the average ratio of the use of private estate was 29.7%, so then it was estimated that a great amount of investment in purchase of eco-forest site would be required. Results from survey on major introduced facilities showed that there was high frequency of introduction of infrastructure, building facility, recreational facility, convenience facility, and information facility, and that there was low frequency of introduction of plant culture system, ecological facility, structural symbol and sculpture, and the likes. There was just one eco-forest park where more than 500 species of plants grew, and the result of investigation indicated that the diversity of plant species in 11 eco-forest parks was lower than the standards for construction of eco-forest. Results from analysis of the projects costs revealed that investment cost in facilities was higher than planting costs, and that a large amount of investment was made in the initial stage of the project. There was no planned budget for the purpose of cultivating and maintaining the plants and vegetation after construction of eco-forest. The basic concepts in construction of eco-forests were established according to the guidelines presented by the Korea Forest Service; however, the detailed work of the project was planned with its user-oriented approach. Then the construction of eco-forest was being planned following the directions, which would lead to development of a plant garden similar to arboretum or botanical garden. Therefore, it is required that the architect who designs eco-forest as well as the public officer concerned firmly establish the concepts of eco-forest, and that, through close analysis of development conditions, a candidate site to fit the purpose of constructing eco-forest be selected, and also a substantive management plan be established upon completion of construction of eco-forest.

Identification of Deer Antler Species Using Sequence Analysis and PCR-RFLP of Mitochondrial DNA (사슴 미토콘드리아 DNA의 염기서열 및 PCR-RFLP분석에 의한 녹용의 종 감별)

  • Shin, Ki-Hyun;Shin, Sung-Chul;Chung, Ku-Young;Chung, Eui-Ryong
    • Food Science of Animal Resources
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    • v.28 no.3
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    • pp.276-282
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    • 2008
  • It is estimated that over 80% of deer antlers produced in the world are consumed in Korea. However, mislabeling or fraudulent replacement of costly antlers with cheaper ones is one of the most common problems in the domestic antler market. Therefore, there is a great need for the development of technology to identify species of antlers. This study was carried out to develop an accurate and reliable method for the identification and authentication of species or subspecies of antlers using DNA sequence analysis and comparison of mitochondrial cytochrome band D-loop region genes among antlers of five deer species, Cervus elaphus sibericus, Cervus elaphus canadensis, Cervus nippon, Cervus elaphus bactrianus and Rangifer tarandus. A variable region of cytochrome band D-loop genes was amplified using PCR with specifically designed primers and sequenced directly. The cytochrome band D-loop region genes showed different DNA sequences between the species of antlers and thus it is possible to differentiate between species on the basis of sequence variation. To distinguish between reindeer (Rangifer tarandus) antlers and other deer antlers, PCR amplicons of the cytochrome b gene were digested with the restriction enzymes NlaIV and TaqI, respectively, which generates a species-specific DNA profile of the reindeer. In addition, samples of 32 sliced antlers labeled Cervus elaphus sibericus from commercial markets were collected randomly and the mt DNA D-loop region of these antler samples was sequenced. Among the antler samples investigated, only 62.5% were from Cervus elaphus sibericus, and others were from Cervus elaphus bactrianus (25.0%), elk (Cervus elaphus canadensis) and reindeer (Rangifer tarandus). Our results suggest that DNA sequencing of mt DNA and PCR-RFLP methods using NlaIV and TaqI enzymes are useful for the identification and discrimination of deer antler species by routine analysis.

Effect of Sodium ion on the Anaerobic Degradation of Food Waste : Quantitative Evaluation, Inhibition Model (주방폐기물의 혐기성분해에 대한 나트륨이온의 영향: 저해 특성평가, 저해모델)

  • Shin, Hang-Sik;Song, Young-Chae;Paik, Byeong-Cheon
    • Journal of the Korea Organic Resources Recycling Association
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    • v.2 no.2
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    • pp.3-17
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    • 1994
  • The inhibitory effect of sodium ion on the anaerobic degradation of food waste was studied by an anaerobic batch toxicity assay and inhibition model. The anaerobic degradation activity of food waste spiked with over $2g\;Na^+/L$ of sodium ion was severely inhibited at the initial stage of the exposure. The inhibition response of anaerobic microorganisms on the sodium ion estimated from the methane production was differed according to the concentration of sodium ion. The relative acclimation time(RAT) and methanation rate(RMR), defined as the ratios of initial lag time and maximum methane production rate of the sample spiked with sodium ion to the control. respectively, were used to evaluate the acclimation and inhibitory effects quantitatively on the anaerobic microorganisms. When sodium ion was increased from $2g\;Na^+/L$ to $20g\;Na^+/L$, the RAT was exponentially increased from 18.9 to 90. but the RMR was linearly decreased from 0.97 to 0.02. The effects of sodium ion for the maximum methanation rate, first order kinetic constant and ultimate methane production were well evaluated by a generalized nonlinear expression model. it could be described by the uncompetitive inhibition mode. The sodium ion concentration causing 50% inhibition of methanation activity was about $11g\;Na^+/L$, and the critical sodium ion beyond to compelete inhibition was 20 to $21g\;Na^+/L$. The presented results could be used to obtain the design or operation parameters of the anaerobic process treating food waste of high salt.

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A Study on the Hull-dimension of 89 ton class Stow-net Vessel with Stern-fishing (89톤급 선미식 안강망어선의 선형치수에 관한 연구)

  • Park, Je-Ung;Lee, Hyeon-Sang
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.33 no.3
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    • pp.159-165
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    • 1997
  • This paper presents the optimum dimension of 89 ton class stow-net vessel with stern-fishing. The model of basic design is developed by using the optimization techniques referring to objective function and numerous constraints as follows; speed, fishing quantity, fishing days, catch per unit effort(CPUE), and weight/ratio of main dimensions, etc. Thus, the basic design of stow-net fishing vessel is built up by using the optimization of the design variables called the economic optimization criteria, and the objective function represents the criterion which is cost benefit ratio(CBR). The main conclusions are as follows. 1. S/W for decision of optimum hull size is developed in 89 ton class stow-net fishing vessel which is constructed with optimization of the design variables called the economic optimization criteria. 2. For optimum ship dimensions in 89 ton class stow-net fishing vessel, the hull dimensions can be obtained in the range of L= 27.3m, B = 6.6m, D = 2.80m, Cb = 0.695, T/D = 0.80, $\Delta$(displacement)=281.7ton with 10 knots.

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An Experimental Study on Development of the Opening Apparatus for Oil Boom (오일펜스 전개장치 개발에 관한 실험적 연구)

  • Jang Duck-Jong;Na Sun-Chol
    • Journal of the Korean Society for Marine Environment & Energy
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    • v.9 no.1
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    • pp.45-54
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    • 2006
  • The study was to review methods by which a ship can unfold and tow an oil boom by attaching the opening apparatus to an oil boom through experiments. The shape and dimension of the opening apparatus were designed with the measurement value of the towing tension load of the oil boom and the dimension of winch drum of the oil boom installed in the ship considered. For the field experiment to identify the performance of the opening apparatus, opening apparatuses were prepared to have the dimension of $3.0m^2$ and $6.0m^2$ which is 91% and 75% of the calculation value for type B and C respectively. As a result, T(kg), the value of tension in type B oil boom according to the towing speed(v) change when two ships are towed together were proved to be $T=920v^{1.1}\;and\;T=500v^{0.9}$ in case the distance is 100 m and 50 m. Based on the result, the dimension of the opening apparatus for type B and C oil boom was calculated as $3.3m^2$ and $8.0m^2$ respectively. When unfolding and towing by attaching the opening apparatus and 200 m of towing line at both ends of type B and type C oil boom, the maximum width of the opening apparatus was shown as 114 m and 95 m in average(width of opening/total length of oil boom: 33% and 57%) in the towing speed of 1.5 kt. It was evaluated that the opening apparatus could concentrate the spilled oil in a good performance. However as far as the increase rate of oil boom opening width according to the length of the towing line is debatable, the increase rate is remarkably reduced when it is lengthened from 100 m to 150 m and to 200 m although it showed extreme increase of 31% and 40% when the length of the towing line was changed from 50 m to 100 m. Therefore, it is inferred that the towing line should be maintained more or less 100 m to get good spread efficiency of the opening apparatus. Additionally, if the towing speed is faster than 1.5 kt, the opening width was narrowed because of the reduced spread efficiency and the shape of the oil boom can be unstable because of the partial sinking of the oil boom, run over waves, or flap of skirt. Thus the reasonable towing speed can be within 1.5 kt for the operation of the opening apparatus.

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Effect of Tightening Torque on Abutment-Fixture Joint Stability using 3-Dimensional Finite Element Analysis (임플란트 지대주나사의 조임회전력이 연결부 안정성에 미치는 영향에 관한 3차원 유한요소해석 연구)

  • Eom, Tae-Gwan;Suh, Seung-Woo;Jeon, Gyeo-Rok;Shin, Jung-Wook;Jeong, Chang-Mo
    • The Journal of Korean Academy of Prosthodontics
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    • v.47 no.2
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    • pp.125-135
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    • 2009
  • Statement of problem: Loosening or fracture of the abutment screw is one of the common problems related to the dental implant. Generally, in order to make the screw joint stable, the preload generated by tightening torque needs to be increased within the elastic limit of the screw. However, additional tensile forces can produce the plastic deformation of abutment screw when functional loads are superimposed on preload stresses, and they can elicit loosening or fracture of the abutment screw. Therefore, it is necessary to find the optimum tightening torque that maximizes a fatigue life and simultaneously offer a reasonable degree of protection against loosening. Purpose: The purpose of this study was to present the influence of tightening torque on the implant-abutment screw joint stability with the 3 dimensional finite element analysis. Material and methods: In this study, the finite element model of the implant system with external butt joint connection was designed and verified by comparison with additional theoretical and experimental results. Four different amount of tightening torques(10, 20, 30 and 40 Ncm) and the external loading(250 N, $30^{\circ}$) were applied to the model, and the equivalent stress distributions and the gap distances were calculated according to each tightening torque and the result was analyzed. Results: Within the limitation of this study, the following results were drawn; 1) There was the proportional relation between the tightening torque and the preload. 2) In case of applying only the tightening torque, the maximum stress was found at the screw neck. 3) The maximum stress was also shown at the screw neck under the external loading condition. However in case of applying 10 Ncm tightening torque, it was found at the undersurface of the screw head. 4) The joint opening was observed under the external loading in case of applying 10 Ncm and 20 Ncm of tightening torque. 5) When the tightening torque was applied at 40 Ncm, under the external loading the maximum stress exceeded the allowable stress value of the titanium alloy. Conclusion: Implant abutment screw must have a proper tightening torque that will be able to maintain joint stability of fixture and abutment.

A Study on Improvement for Fishing Gear and Method of Pound Net - I - Net Shapes of the Commerical Net in the Flow - (정치망 어구어법의 개발에 관한 연구-I - 현용어구의 흐름에 대한 형상 변화 -)

  • Yun, Il-Bu;Lee, Ju-Hee;Kwon, Byeong-Guk;Cho, Young-Bok;Yoo, Jae-Bum;Kim, Seong-Hun;Kim, Boo-Young
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.40 no.4
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    • pp.268-281
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    • 2004
  • A study was carried out in order to estimate the deformation of the pound net according to the current by the model test in the circulating water channel. The tension of the frame rope and the variation of net shape were measured to investigate the deforming of the model pound net in the flow. The results are obtained as follows; 1. The experimental equation between tensions (R) of the frame rope and velocity (ν)was found to be R=$19.58v^{1.98}$($r^2$=0.98) in case of the upperward flow with fish court net and R=$26.90v^{1.72}$($r^2$=0.95)at the upperward flow with bag net according to the velocity from 0.0m/s to 0.6m/s, respectively. 2. As the variation of flow speed inside of the model net was gradually decreased according as which is passed through netting panels, in case of the upperward flow with fish court net, the flow speed was about 70% of initial flow speed at 0.1m/s, 60% at 0.2m/s, 50% at 0.3m/s and 40% 0.4~0.6m/s at the measurement point(h) inside of the first bag net, respectively. In case of the upperward flow with bag net, as the flow speed was steeply decreased according as which if passed through the second bag net, it was 30~60% of the initial flow speed and was 20~30% inside of the first bag net and was about 10~20% inside of the inclined passage net. 3. In case of the upperward flow with fish court net, the variation of deformed angle of fish court net was from 0$^{\circ}$ to 70$^{\circ}$and that of inclined passage net was from 0$^{\circ}$ to 63$^{\circ}$and that of the second bag net was from 0$^{\circ}$ to 47$^{\circ}$ . 4. In case of the upperward flow with fish court net, the variation of deformed angle of the second bag net was changed from 0$^{\circ}$ to 70$^{\circ}$and that of the inclined passage net was from 0$^{\circ}$ to 55$^{\circ}$ and that of the fish court net was from 0$^{\circ}$ to 50$^{\circ}$. The depth ratio of the first bag net was changed from 0% to 35% and that of the second bag net was from 0% to 20% and that of the inclined passage net was from 0% to 35%. In the flow speed 0.5m/s, the inclined passage net was raised up to the entry of the bag net and then prevented it more over 90%. 5. To be increased the opening volume of pound net, it needs to attach the added weight outside of the fish court net, inclined passage net and bag net. At the same time, it needs to adjust the tension of the twine for maintenance of the shape.

A Case Study on the Effective Liquid Manure Treatment System in Pig Farms (양돈농가의 돈분뇨 액비화 처리 우수사례 실태조사)

  • Kim, Soo-Ryang;Jeon, Sang-Joon;Hong, In-Gi;Kim, Dong-Kyun;Lee, Myung-Gyu
    • Journal of Animal Environmental Science
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    • v.18 no.2
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    • pp.99-110
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    • 2012
  • The purpose of the study is to collect basis data for to establish standard administrative processes of liquid fertilizer treatment. From this survey we could make out the key point of each step through a case of effective liquid manure treatment system in pig house. It is divided into six step; 1. piggery slurry management step, 2. Solid-liquid separation step, 3. liquid fertilizer treatment (aeration) step, 4. liquid fertilizer treatment (microorganism, recirculation and internal return) step, 5. liquid fertilizer treatment (completion) step, 6. land application step. From now on, standardization process of liquid manure treatment technologies need to be develop based on the six steps process.

Analysis of Greenhouse Thermal Environment by Model Simulation (시뮬레이션 모형에 의한 온실의 열환경 분석)

  • 서원명;윤용철
    • Journal of Bio-Environment Control
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    • v.5 no.2
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    • pp.215-235
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    • 1996
  • The thermal analysis by mathematical model simulation makes it possible to reasonably predict heating and/or cooling requirements of certain greenhouses located under various geographical and climatic environment. It is another advantages of model simulation technique to be able to make it possible to select appropriate heating system, to set up energy utilization strategy, to schedule seasonal crop pattern, as well as to determine new greenhouse ranges. In this study, the control pattern for greenhouse microclimate is categorized as cooling and heating. Dynamic model was adopted to simulate heating requirements and/or energy conservation effectiveness such as energy saving by night-time thermal curtain, estimation of Heating Degree-Hours(HDH), long time prediction of greenhouse thermal behavior, etc. On the other hand, the cooling effects of ventilation, shading, and pad ||||&|||| fan system were partly analyzed by static model. By the experimental work with small size model greenhouse of 1.2m$\times$2.4m, it was found that cooling the greenhouse by spraying cold water directly on greenhouse cover surface or by recirculating cold water through heat exchangers would be effective in greenhouse summer cooling. The mathematical model developed for greenhouse model simulation is highly applicable because it can reflects various climatic factors like temperature, humidity, beam and diffuse solar radiation, wind velocity, etc. This model was closely verified by various weather data obtained through long period greenhouse experiment. Most of the materials relating with greenhouse heating or cooling components were obtained from model greenhouse simulated mathematically by using typical year(1987) data of Jinju Gyeongnam. But some of the materials relating with greenhouse cooling was obtained by performing model experiments which include analyzing cooling effect of water sprayed directly on greenhouse roof surface. The results are summarized as follows : 1. The heating requirements of model greenhouse were highly related with the minimum temperature set for given greenhouse. The setting temperature at night-time is much more influential on heating energy requirement than that at day-time. Therefore It is highly recommended that night- time setting temperature should be carefully determined and controlled. 2. The HDH data obtained by conventional method were estimated on the basis of considerably long term average weather temperature together with the standard base temperature(usually 18.3$^{\circ}C$). This kind of data can merely be used as a relative comparison criteria about heating load, but is not applicable in the calculation of greenhouse heating requirements because of the limited consideration of climatic factors and inappropriate base temperature. By comparing the HDM data with the results of simulation, it is found that the heating system design by HDH data will probably overshoot the actual heating requirement. 3. The energy saving effect of night-time thermal curtain as well as estimated heating requirement is found to be sensitively related with weather condition: Thermal curtain adopted for simulation showed high effectiveness in energy saving which amounts to more than 50% of annual heating requirement. 4. The ventilation performances doting warm seasons are mainly influenced by air exchange rate even though there are some variations depending on greenhouse structural difference, weather and cropping conditions. For air exchanges above 1 volume per minute, the reduction rate of temperature rise on both types of considered greenhouse becomes modest with the additional increase of ventilation capacity. Therefore the desirable ventilation capacity is assumed to be 1 air change per minute, which is the recommended ventilation rate in common greenhouse. 5. In glass covered greenhouse with full production, under clear weather of 50% RH, and continuous 1 air change per minute, the temperature drop in 50% shaded greenhouse and pad & fan systemed greenhouse is 2.6$^{\circ}C$ and.6.1$^{\circ}C$ respectively. The temperature in control greenhouse under continuous air change at this time was 36.6$^{\circ}C$ which was 5.3$^{\circ}C$ above ambient temperature. As a result the greenhouse temperature can be maintained 3$^{\circ}C$ below ambient temperature. But when RH is 80%, it was impossible to drop greenhouse temperature below ambient temperature because possible temperature reduction by pad ||||&|||| fan system at this time is not more than 2.4$^{\circ}C$. 6. During 3 months of hot summer season if the greenhouse is assumed to be cooled only when greenhouse temperature rise above 27$^{\circ}C$, the relationship between RH of ambient air and greenhouse temperature drop($\Delta$T) was formulated as follows : $\Delta$T= -0.077RH+7.7 7. Time dependent cooling effects performed by operation of each or combination of ventilation, 50% shading, pad & fan of 80% efficiency, were continuously predicted for one typical summer day long. When the greenhouse was cooled only by 1 air change per minute, greenhouse air temperature was 5$^{\circ}C$ above outdoor temperature. Either method alone can not drop greenhouse air temperature below outdoor temperature even under the fully cropped situations. But when both systems were operated together, greenhouse air temperature can be controlled to about 2.0-2.3$^{\circ}C$ below ambient temperature. 8. When the cool water of 6.5-8.5$^{\circ}C$ was sprayed on greenhouse roof surface with the water flow rate of 1.3 liter/min per unit greenhouse floor area, greenhouse air temperature could be dropped down to 16.5-18.$0^{\circ}C$, whlch is about 1$0^{\circ}C$ below the ambient temperature of 26.5-28.$0^{\circ}C$ at that time. The most important thing in cooling greenhouse air effectively with water spray may be obtaining plenty of cool water source like ground water itself or cold water produced by heat-pump. Future work is focused on not only analyzing the feasibility of heat pump operation but also finding the relationships between greenhouse air temperature(T$_{g}$ ), spraying water temperature(T$_{w}$ ), water flow rate(Q), and ambient temperature(T$_{o}$).

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