• Title/Summary/Keyword: 다이어프램 밸브

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Development of a diaphragm type actuator (다이어프램형 방식의 파일럿 액추에이터 개발)

  • Lee, Joongyoup;Jeong, Daeseong;Han, Sangyeop
    • Aerospace Engineering and Technology
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    • v.13 no.2
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    • pp.160-166
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    • 2014
  • The shutoff valve of a Liquid Rocket Engines (LRE) controls the flow of propellant between turbo-pump and combustion devices of LRE using pilot pressure and spring force. The shutoff valve is closed when the pilot pressure is removed from the diaphragm type actuator. During designing process of life cycle is when should be analyzed according to the characteristics of forces with respect to the opening and closing of diaphragm actuator. A valve has been designed to adjust the control pressure which is required to open a poppet and to determine the working fluid pressure at which a valve starts to close. During flow capacity test under room temperature as a part of life cycle tests, the leakage in diaphragm was occurred due to the leakage of sheet welding sections. The operating cycle of the diaphragm type actuator is about 61 times with 22 MPa of pilot pressure.

Development of Diagnosis System for Diaphragm Operated Globe Valve (다이어프램 구동형 글로브 밸브의 진단장비 개발)

  • Yang, Sang-Min;Shin, Sung-Ky
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.31 no.9
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    • pp.975-980
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    • 2007
  • Air-operated valve is one of principal valves that are used to control fluid flow in nuclear power plants. A periodic diagnosis for the safety of power plants is necessary. But there are many difficulties such as economic loss caused by income of high cost devices and a matter hard to deal with users. In this study, we developed the diagnostic system that users of power plants are easy to handle. The diagnostic system is composed of database module, diagnosis test module and analysis module.

Development of Eco-Environmental On/Off Diaphragm Valve (친환경 온/오프 다이어프램 밸브 개발)

  • Cheong, Seon-Hwan;Choi, Seong-Dae;Klm, Shin-Ho
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.6 no.4
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    • pp.28-35
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    • 2007
  • Currently, most of all valves using at the semiconductor & LCD manufacturing process are packless type. Such valves are needed to have the functions to protect perfectly from the leakage of fluid by using bellows and diaphragm instead of the grand packing. But not only those valves made in Korea are not available at this point, but also advanced foreign manufacturers do not open enough their data on the basic technology. Otherwise although they open the data a little, they are almost data about stainless steel for pneumatic valves. In this paper, it was focused on the fluid valves for chemical & DI water based on the data of steel valves which are already using commercially. And also this study concentrated to collect the basic developing data of Eco-On/Off diaphragm valve by ourselves.

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A Study on Flow Rate Characteristic and Dynamic Performance on Diaphragm Solenoid Valve (다이어프램형 밸브의 유량특성과 동적성능에 관한 연구)

  • Jeong, C.S.;Yang, S.Y.
    • Journal of Drive and Control
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    • v.10 no.3
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    • pp.27-33
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    • 2013
  • Solenoid valve has used in various industrial field extensively. A solenoid valve has different size, shape and method of operation accordantly to industrial field. Many researchers study on kinds of solenoid valve such as flow rate, dynamic, magnetic field, valve shape and operating method. But the flow rate characteristic and dynamic response time performance on the diaphragm valve are not studied. This paper describes the flow rate characteristic and dynamic response time performance on the diaphragm valve. At first, the diaphragm valve is simulated in AMESim simulation tool. AMESim model found that an effect of valve performance depends on parameter. The parameter is the diaphragm orifice area. And the performance test bench confirms the effect in this parameter. Finally, it finds out the flow rate characteristic and dynamic response time performance on the diaphragm valve.

Development of the Quick Exhaust Valve to Blowing the Intake Filter for the Thermal Power Plant (화력발전소 흡입필터 세정용 급속 배기 밸브의 개발)

  • Jeong, C.S.;Lee, H.U.;Jeong, Y.M.;Lee, C.D.;Yang, S.Y.
    • Journal of the Korean Society of Manufacturing Technology Engineers
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    • v.19 no.4
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    • pp.548-552
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    • 2010
  • The air suction filter of the power plant decrease the dust and impurities of suction air that reduce the life and efficiency of the boiler. The suction efficiency of the air filter falls with the dust and impurities when the time of use comes to be long. Therefore, the various contaminant of the filter must remove periodically. This paper presents a developed quick exhaust valve to use in the thermo-electric power plant. to removing contaminants on the filter, the blowing is done shortly by air pressure. The Air flowed out to the out side from the inside of the filter. The performance test of the developed valve is done by making a test-bench according to JIS and KS standards. The efficiency is found higher than the existing related valve.

Dynamic Modeling and Test of the Air-Operated Valve (공기구동밸브의 동특성 모델링 및 시험)

  • Cho T.D.;Lee H.Y.;Yang S.M.;Yang S.B.;Kwon B.S.
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 2005.06a
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    • pp.1808-1811
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    • 2005
  • The prediction of AOV(air-operated valve) performance is normally evaluated by the allowable opening thrust margin for the opening and closing stroke. However, it is not easy to carry out the dynamic test measurement for all the valves in the nuclear power plant due to the safety and operating conditions. The analysis of the available and required thrust for the valve is simulated as an alternate method to turn around this obstacle. The required air pressures to the stem displacement are discussed for differential valve pressure obtained by experiment. The result of the simulation is compared with that of the experiment. SIMULINK in MATLAB was used for the simulation and the results show good agreement with the actual test carried out with Fisher globe valve.

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A Study on the Strength Safety of a Gas Valve (가스밸브의 강도안전성에 관한 연구)

  • Kim, Chung Kyun
    • Journal of the Korean Institute of Gas
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    • v.22 no.1
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    • pp.60-63
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    • 2018
  • This paper presents the FEM analysis results on the strength safety of a gas valve for a LPG cylinder. Based on the FEM analysis, the maximum von Mises stress on the boundary zone between a safety valve and the upper area of the thread is 99.2 MPa for the supplied gas pressure of 3.5 MPa in which the gas valve is fully opened. The maximum von Mises stress of 99.2 MPa is considered as safety value, because that value is lower than the yield stress of a brass material. In this case, the maximum deformation at the upper right part of the pressure regulator is 0.002mm. The maximum deformation zone is not a meaning part of the sealing part such as an O-ring or a diaphragm of a gas valve and a pressure regulator. The proposed hybrid gas valve model in which is integrated with a conventional cut-off valve and a pressure regulator is recommended as a gas leakage free mechanism and minimized compact size for a LPG cylinder.

Effects of Flow Rate and Discharge Pressure with Compressing Spring in Non-diaphragm Type Stem of Water Pressure Reducing Valve (급수용 감압밸브의 비다이어프램 스템에서 압축스프링에 따른 유량 및 토출압력 효과)

  • Byeon, Jae-Uk;Kim, Chi-Ho;Park, Seong-Hwan;Lee, Myung-Won;Kang, Myungchang
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.18 no.5
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    • pp.103-109
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    • 2019
  • The pressure reducing valve for water is controlled by the load of the compression spring and the force of the fluid acting on the diaphragm of the stem. Repeated upward and downward reciprocation of the pressure-reducing valve stem damages the diaphragm, resulting in leakage. In this study, we designed a stem without a diaphragm and adjusted the stiffness of the compressing spring. In order to select the spring stiffness, springs offering a stiffness of -20%, -10%, 0%, and 10% with respect to the stiffness of the compression spring attached to the existing pressure reducing valve stiffness. A prototype for the pressure reducing valve was fabricated and the pressure change was evaluated for the target static pressure (6 bar) by testing the pressure characteristics after mounting the modified stem and each compression spring. Evaluation of the pressure characteristics was carried out using ASSE 1003 and KS B 6153. In addition, the flow rates were compared by internal flow analysis of the conventional pressure reducing valve and the pressure reducing valve using the modified stems, and the flow analysis was performed using Solidworks flow simulation 2018. The spring stiffness was constantly discharged at the target static pressure of 3.793 kgf/mm, and the flow rate was increased by about 15% compared with the conventional pressure reducing valve.

Structure Improvement of Preaction Valve to Reduce the Pressure Drop (압력손실을 줄이기 위한 준비작동식 유수검지장치 본체 구조 개선)

  • Hong, Seung-Tae;Jeong, Jae-Han;Nam, Jun-Seok;Kwon, Young-Kyu;Han, Chul-Su;Yoo, Seung-Joon
    • Korean Chemical Engineering Research
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    • v.53 no.1
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    • pp.16-21
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    • 2015
  • The body structure of diaphragm type preaction valve was improved in order to reduce the pressure drop. The pressure drop must be kept within 20.7 kPa to pass the revised (2012. 2. 9) standard for alarm valve and preaction valve. The pressure drop test was carried out by KFI (Korea Fire Institute) standard. The pressure drop of a preaction valve was higher than that of an alarm valve. Causes for increasing the pressure drop were investigated with the fluid flow in the valve. The preaction valve had more pressure drop factors (changes in velocity and direction) compared with the alarm valve. Inner structure of the preaction valve was changed to the clapper type to remove the pressure drop factors. In 80A and 100A size of preaction valves, the pressure drop was reduced from 80.9 and 171.0 kPa to 14.4 and 14.2 kPa respectively, after the change of the structure.