• Title/Summary/Keyword: 기준진동수

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Vibration Analysis of a Cooling Fan Gear Reducer of the Secondary Cooling Tower in HANARO (하나로 2차 냉각탑의 냉각팬 감속기의 진동분석)

  • Park, Young-Chul
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.34 no.7
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    • pp.935-941
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    • 2010
  • HANARO is an open-tank-in-pool-type Korean research reactor that generates 30MW of thermal power. It differs from power plant reactor in that the heat generated by HANARO is exhausted into the atmosphere through a secondary cooling tower, thus maintaining the core temperature constant. During every monthly inspection of the cooling tower, large vibrations that exceeded the permissible limit were observed at cooling fan gear reducer No. 4 of the cooling tower. The purpose of this study is to identify the origin of the large vibration and to repair it. FFT spectrum analysis is performed to identify the part that caused the large vibration. The results of the frequency analysis showed that the vibration frequency was 354 Hz, which is twice the natural frequency of the pinion gear. A check of the pinion gear revealed that there was a crack on the surface of the pinion gear. After the gear was replaced, the reducer operated normally.

A Study on the Effect of Artificial Cutting Slot on the Fragmentation and Vibration Propagation in the Full-scaled Concrete Block Blasting (콘크리트 블록 발파 실험을 통한 인공 슬롯 자유면이 진동전파 및 파쇄효과에 미치는 영향에 관한 연구)

  • Oh, Se-Wook;Min, Gyeong-Jo;Park, Se-Woong;Park, Hoon;Noh, You-Song;Suk, Chul-Gi;Cho, Sang-Ho
    • Tunnel and Underground Space
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    • v.28 no.6
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    • pp.692-705
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    • 2018
  • Ground vibration is one of the remarkable issues in tunnel blasting. In recent studies, to improve the fragmentation with reduction of ground vibration in tunnel blasting, a vibration-controlled blasting method with artificial cutting slot near the center-cut holes has been suggested. This study examines the effect of the different arrangement of artificial cut-slot on the vibration reduction and fragmentation by performing the full-scaled concrete block blast experiments and the numerical simulations with 3D-DFPA. The results show that the existence of artificial slot contributes to the improvement of vibration reduction, blast fragmentation and the efficiency of the cutting slot blast. It can be explained that the artificial slot play a free surface role and should decrease the burden between the cut holes. Crater volumes of the blasted concrete blocks were measured by 3-dimensional digital image analysis and compared with the ideal standard crater volume which can be calculated by theoretical standard blast design method. As a result, the ratio of burden and hole diameter which should achieve the standard crater in the cut-hole blasting were suggested.

A Study on the Model Test for Estimating Dynamic Vertical Load Added to Shallow Foundation for Machine (진동기 얕은기초에 추가되는 동적 연직하중 산정을 위한 모형실험 방안 연구)

  • Ha, Ik-Soo;Yoo, Mintaek
    • Journal of the Korean Geotechnical Society
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    • v.36 no.11
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    • pp.157-165
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    • 2020
  • At present, there are no clearly stated criteria or theories in calculating additional vertical dynamic loads that occur at the machine foundation due to vibration and reflecting them in the design at home and abroad. According to the domestic standard, although it is not a serious vibration condition, the additional dynamic load due to vibration is considered up to 100% of the static load. This is an extremely conservative design. The purpose of this study is to propose a model test method for evaluating the quantitative magnitude of additional dynamic loads that are generated at certain static loads due to vertical mechanical vibrations. As preliminary basic tests for the model tests, the test for evaluating the effects of reflective wave that may occur within a limited size soil box and the test for estimating the natural frequency of the devised model soil-foundation system were carried out. From the analysis of results for basic tests, a method to minimize the influence of the reflected wave was prepared, and the effect of the resonance of the model system was minimized during the model tests. After the basic tests, the main model tests were conducted. Through the proposed main test, the quantitative magnitude of additional dynamic loads caused by machine vibration on a shallow foundation for machine on medium dense sand foundations were evaluated. From the results of the model test, the feasibility of design applied at home and abroad was reviewed.

Frequency Shaped Optimal Control of Semi-active Suspension System Using an MR Damper (자기유변유체를 이용한 반능동형 현가장치의 Frequency shaped 최적 제어)

  • 김기덕;이재형;전도영
    • The Korean Journal of Rheology
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    • v.11 no.2
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    • pp.112-121
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    • 1999
  • An MR(Magneto-Rheological) fluids damper is designed and applied to vibration suppression of a 1/4 car model. The damping constant of MR damper changes according to input current which is controlled in a semi-active way. Several control algorithms are compared in simulations and experiments. The advantage of the proposed Frequency shaped LQ control is that passenger comfort is emphasized in the range of 4~8Hz and driving safety is emphasized around the resonance frequency of unsprung mass.

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Study on Establishing a Blast Guideline for Securing an Underground Crusher Room from Ground Vibrations (지하 조쇄실의 진동 안정성 확보를 위한 발파지침 수립 연구)

  • Choi, Byung-Hee;Ryu, Chang-Ha;Kim, Hyun-Woo;Kang, Myoung-Soo
    • Explosives and Blasting
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    • v.33 no.2
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    • pp.15-24
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    • 2015
  • In general, blast vibrations could make underground cavern unstable by causing relative movements between the surrounding rock blocks that are divided by discontinuities such as joints and faults around the cavern. In the study, a blast guideline was established to obtain the stability of a large-scale cavern for underground crusher room in an open pit limestone mine in Korea. The guideline was suggested in the form of a standard calculation method of the maximum charge per delay for a safe blast. The allowable level of peak particle velocity for the cavern was determined based on the result of a numerical analysis using FLAC2D. The ground vibration data required for the study was obtained from field measurements.

Analysis of Characteristics of Horizontal Response Spectrum of Ground Motions from Fukuoka Earthquakes Series (Fukuoka 연속 지진의 관측자료를 이용한 수평 응답스펙트럼 특성 분석)

  • Kim, Jun Kyoung
    • Tunnel and Underground Space
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    • v.24 no.5
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    • pp.354-365
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    • 2014
  • The horizontal response spectra using the observed ground motions from 15 Fukuoka earthquake series, including main earthquake (2005/03/20; Mw=6.5), were analysed and then were compared to both the seismic design response spectra (Regulatory Guide 1.60), applied to the domestic nuclear power plants, and the Korean Standard Design Response Spectrum for general structures and buildings (1997). 178 horizontal ground motions, without considering soil types, were used for normalization with respect to the peak acceleration value of each ground motion. The results showed that response spectrum have strong dependency on epicentral distance. The results also showed that the horizontal response spectra revealed higher values for frequency bands at two frequency bands (about 8 - 10 and 16- 20 Hz) than Regulatory Guide 1.60. The results were also compared to the Korean Standard Building Design Spectrum for the 3 different soil types and showed that thehorizontal response spectra revealed higher values for almost all period bands than the Korean Standard Response Spectrum (500 yrs; Return Period; Seismic province 1; SE soil conditions). Through the qualitative improvements and quantitative enhancement of the observed ground motions, the diversity of the observed ground motions should be considered more significantly to improve the certainty of response spectrum.

Appropriateness Evaluation of Train Vibration Evaluation Method Considering Vibration Levels of Retaining Wall Adjacent to Railway Tunnels (철도터널과 인접한 흙막이 가시설의 진동 수준을 고려한 열차진동 평가방법의 적정성 평가)

  • Donghee Woo;Yeongjin Lee;Yongjae Song;Kangil Lee
    • Journal of the Korean GEO-environmental Society
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    • v.24 no.10
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    • pp.5-13
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    • 2023
  • With the recent increase in development projects centered on urban areas, the construction of building structures is increasing in areas adjacent to the urban railway operation section. In this case, since ground vibration is generated by the train in operation and affects the adjacent structure, the building structure needs appropriate vibration reduction against train vibration generated at the adjacent location from the desing phase. However, the vibration levels calculated vary depending on the train vibration evaluation method, which means that the implementation of vibration reduction may vary depending on the train vibration evaluation method. Therefore, this study calculated the vibration level according to ground conditions, tunnel depth and separation distance between vibration sources and adjacent structures using numerical analysis and train vibration evaluation methods, and compared them to designning phase. And the appropriate separation distance between the tunnel and the adjacent structure was evaluated by comparing the vibration level with the allowable standards. As a result of the study, the Ungar and Bender evaluation method is evaluated as the most appropriate among the train vibration evaluation methods, and the appropriate separation distance between the tunnel and the adjacent structure is evaluated to be more than 4.5D.

Near-wake Measurements of an Oscillating NACA 0012 Airfoil (진동하는 NACA 0012 에어포일의 근접후류 측정)

  • Kim, Dong-Ha;Kim, Hak-Bong;Jang, Jo-Won
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.34 no.12
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    • pp.1-8
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    • 2006
  • An experimental study was carried out in order to investigate the influence of Reynolds number on the near-wake of an oscillating airfoil. An NACA 0012 airfoil was sinusoidally pitched at the quarter chord point, and is oscillated over a range of instantaneous angles of attack of $\pm$6$^{\circ}$. An X-type hot-wire probe was employed to measure the near-wake of an oscillating airfoil, and the smoke-wire visualization technique was used to examine the flow properties of the boundary layer. The free-stream velocities were 1.98, 2.83 and 4.03 m/s and the corresponding chord Reynolds numbers were 2.3${\times}10^4$, 3.3$\times$104 and 4.8${\times}10^4$, respectively. The frequency of airfoil oscillation was adjusted to fix a reduced frequency of K=0.1. The results show that the properties of the boundary layer and the near-wake can dramatically be distinguished in the range of Reynolds numbers between 2.3${\times}10^4$ and 3.3${\times}10^4$, on the other hand, it is similar in the cases of Re=3.3$\times$104 and 4.8$\times$104. This is caused by that the unsteady separation point is dramatically delayed in case of Re= 2.3${\times}10^4$.

Comparison of Sound Spectrums of Pyeonjong Remains at the King Sejong Memorial Museum and Pyeonjong Replica (세종대왕기념관의 유물 편종과 현대 편종의 음향 스펙트럼 비교)

  • Yoo, June-Hee
    • The Journal of the Acoustical Society of Korea
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    • v.28 no.3
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    • pp.222-228
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    • 2009
  • This study compared the sound spectrums of pyeonjong remains and pyeonjong replica to investigate tuning ways of bells. pyeonjong remains, exhibited at King Sejong Memorial Museum and pyeonjong replica, played at the National Center for Korean Traditional Performance Arts were analyzed. To get mode frequencies and mode shapes, pyeonjong replicas' sound spectrums were analyzed and modal analyses by TV holography were performed. Also pyeonjong remains' sound spectrum were analyzed. Nominal frequencies on the pyeonjong replica and remains showed differences in a range between 9.8 cent and 203 cent. Two facts were inferred as causes of the differences, the tuning conditions of pyeonjong remains were not good and C4 in western tempered scale was preferred as the sound standard of Kukak, whangjong. Relative ratio of higher mode frequencies to the nominal frequencies were calculated to figure out tonal differences between two pyeonjongs. The differences in relative ratio of higher mode frequencies except (3,0)a and (3,0)b modes were significants as well as beyond the just noticeable difference. These results implied that the tonal differences between two pyeonjongs could exist. More pyeonjong remains are needed to be investigated to confirm this result in addition to the analyses of alloy components and bell structure of pyeonjong remains and replica.

Distribution of vibration signals according to operating conditions of wind turbine (풍력발전기 운전환경에 따른 진동신호 분포)

  • Shin, Sung-Hwan;Kim, SangRyul;Seo, Yun-Ho
    • The Journal of the Acoustical Society of Korea
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    • v.35 no.3
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    • pp.192-201
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    • 2016
  • Condition Monitoring System (CMS) has been used to detect unexpected faults of wind turbine caused by the abrupt change of circumstances or the aging of its mechanical part. In fact, it is a very hard work to do regular inspection for its maintenance because wind turbine is located on the mountaintop or sea. The purpose of this study is to find out distribution patterns of vibration signals measured from the main mechanical parts of wind turbine according to its operation condition. To this end, acceleration signals of main bearing, gearbox, generator, wind speed, rotational speed, etc were measured through the long period more than 2 years and trend analyses on each signal were conducted as a function of the rotational speed. In addition, correlation analysis among the signals was done to grasp the relation between mechanical parts. As a result, the vibrations were dependent on the rotational speed of main shaft and whether power was generated or not, and their distributions at a specific rotational speed could be approximated to Weibull distribution. It was also investigated that the vibration at main bearing was correlated with vibration at gearbox each other, whereas vibration at generator should be dealt with individually because of generating mechanism. These results can be used for improving performance of CMS that early detects the mechanical abnormality of wind turbine.