• Title/Summary/Keyword: 곡사포

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Artillery Error Budget Method Using Optimization Algorithm (최적화 알고리즘을 활용한 곡사포의 사격 오차 예측 기법)

  • An, Seil;Ahn, Sangtae;Choi, Sung-Ho
    • Journal of the Korea Society for Simulation
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    • v.26 no.3
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    • pp.55-63
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    • 2017
  • In R&D of artillery system, error budget method is used to predict artillery firing error without field firing test. The error budget method for artillery has been consistently developed but apply for practical R&D of the weapon system has been avoided because of lacks of error budget source information. The error budget source is composed of every detailed error components which affect total distance and deflection error of artillery, and most of them are difficult to be calculated or measured. Also with the inaccuracy of source information, simulated error result dose not reflect real firing error. To resolve that problem, an optimization algorithm is adopted to figure out error budget sources from existing filed firing test. The method of finding input parameter estimation which is commonly used in aerodynamics was applied. As an optimization algorithm, CMA-ES is used and presented in the paper. The error budget sources which are figured out by the presented method can be applied to compute ROC of new weapon systems and may contribute to an improvement of accuracy in artillery.

An experimental study for developing of silencer to be adapted large gun (대구경 화포용 소음기 개발을 위한 실험적 연구)

  • Lee, Hae suk;Park, Sung ho;Kim, Sang min;Kang, Tae yeop;Kim, Heung soo
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2014.04a
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    • pp.558-563
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    • 2014
  • To reduce the transmission of large gun-generated noise from the firing test range to the community, we have tested a silencer to be used with howitzer(155mm KM114A2) after simulation. Numerical analysis was conducted by using a commercial CFD code, FLUENT. To analyze complex blast flow fields, the Spalart-Allmaras model was applied under 2 dimensional and axisymmetric conditions. Firing tests were also performed with the KM114A2 howitzer while the silencer was installed. This paper describes a result of comparison between results of computer analysis and test outcomes which were gotten by firing 155mm projectiles at the testing range. This paper will also be informative to the muffler design which will be adapted to 155mm large gun in the future.

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Experimental Study for Developing Silencer Adapted by Large Caliber Gun (대구경 화포용 소음기 개발을 위한 실험적 연구)

  • Lee, Hae-Suk;Park, Sung-Ho
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.25 no.9
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    • pp.593-598
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    • 2015
  • In this paper, the silencer for large caliber gun to reduce the propagation of gun-generated noise was studied. The results of structural analysis and firing test were described. Structural analysis was conducted by using a commercial program, ANSYS, and showed that there was not any structural problem. The sound pressure level was diminished about 10 dB by the silencer adapted in front of the gun and the soundness of the material was verified from the internal pressure measurement. The reduction of weight, improvement of durability and speed-up of actuating device have to be studied later to improve the usability of silencer for large caliber gun.

Improvement of Firing Elevation Driving Method for Towed Howitzer to Prevent Musculoskeletal Problems (근골격계 질환 예방을 위한 견인곡사포 고각조정 방법의 개선)

  • Park, Sung Ho
    • Journal of Korean Institute of Industrial Engineers
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    • v.42 no.2
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    • pp.122-128
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    • 2016
  • The purpose of this study is to improve the firing elevation driving method for towed howitzer to prevent the musculoskeletal disorders. To adjust the firing elevation, it is required to rotate the hand wheel and this work has been done manually in the firing test range as the same method as field artillery troops. In the firing test range, the motor-driven firing elevation adjustment device was developed to improve the working efficiency and safety. These were compared by using posture classification scheme of RULA and REBA. It was measured elapsed time to investigate the improved operational efficiency. The optimal posture of upper body to operate the hand wheel for field artillery troops was proposed.

A Study on the Design Improvement to prevent the stoppage phenomenon of Launch Support Device for Self-Propelled Artillery (자주포용 발사지지대의 멈춤현상 방지를 위한 설계개선 연구)

  • Kim, Sung Hoon;Park, Young Min;Noh, Sang Wan;Park, Dae Hoon
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.21 no.5
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    • pp.443-450
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    • 2020
  • This paper reports a design improvement study to solve the stoppage phenomenon caused by the launch-support device applied to K105A1. The K105A1 is a weapon system equipped with an old 105 mm towed howitzer in a wheeled vehicle, which provides superior maneuverability compared to track equipment. The launch support device serves to withstand fire impact and load. In this way, this device is fixed firmly to the ground in preparation for the shooting mission and is responsible for the critical performance, such as fixing the position of the vehicle. On the other hand, during the field test, a temporary stoppage of the launch support occurred, which caused a problem of not being fixed to the ground. To solve this problem, the cause of failure was analyzed by a replay test and parts inspection. In addition, the operating concept, method, and design were analyzed to derive the cause and solve the problem by changing the parts design. Finally, the performance and firing missions were performed normally by applying the changed design to K105A1. The performance stability and reliability of the launch support device were confirmed, which are expected to be of great assistance in the development of military equipment in the future.