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7톤급 터보펌프 산화제펌프의 고주파 신호 분석

High Frequency Signal Analysis of Oxidizer Pump for 7-tonf Turbopump

  • Bae, Joon-Hwan (Turbopump Team, Korea Aerospace Research Institute) ;
  • Choi, Chang-Ho (Turbopump Team, Korea Aerospace Research Institute) ;
  • Choi, Jong-Soo (Department of Aerospace Engineering, Chungnam National University)
  • 투고 : 2020.07.22
  • 심사 : 2020.10.27
  • 발행 : 2020.12.31

초록

7톤급 터보펌프 실매질시험에서 계측된 고주파 신호인 가속도와 압력섭동에 대한 주파수 분석(waterfall, frequency spectrum), 실효값(RMS) 계산 등의 신호 처리를 통해 산화제펌프의 신뢰성을 평가하였다. 계측된 압력섭동 신호 분석을 통해 산화제펌프의 누설 유로에 위치한 산화제 후방 플로팅 링에 의한 강한 압력섭동이 발생하였고 이는 산화제펌프 입구 및 출구 압력과 가속도 신호에도 영향을 주는 것을 확인하였다. 터보펌프의 가속도 실효값 계산을 통해 정격 운용 조건에서의 터보펌프는 양호한 진동 성능을 보여주고 있으며 가속도 회전수 성분 중 축계에 영향을 주는 회전수 동기 주파수 성분이 강하게 나타나는 것을 확인하였다.

7-tonf turbopump real-propellant tests in Naro Space Center were conducted and high-frequency signals from an accelerometer and pressure sensors installed on the casing and the inlet/outlet pipeline of LOX pump were analyzed to estimate the structural and hydrodynamic stabilities. Waterfalls, frequency spectrums and RMS(Root Mean Square) values of the measured signals were calculated and characteristic instability frequencies by the rotating cavitation and the rear floating ring seal(F.R.S) were investigated. Static pressures of the inlet/outlet pipeline and an acceleration of the pump casing are strongly affected on pressure fluctuation induced by the rear floating ring seal in the leakage path. Despite the acceleration RMS value seems totally small, the rotating-speed-related synchronous frequency affecting the shaft instability is distinctly observed in the frequency contour.

키워드

참고문헌

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