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Vibration Reduction Devices for Korean Utility Helicopter

한국형기동헬기 진동저감장치

  • Received : 2013.07.04
  • Accepted : 2013.11.27
  • Published : 2013.12.01

Abstract

Korean Utility Helicopter(KUH) is the first korean-developed helicopter. Its first flight was performed in March 2010 and then its development was completed successfully by June 2012. During flight test phase, KUH faced various vibration problems and appropriate vibration-reduction devices were designed and applied to solve the problems. The vibration-reduction devices were applied to main rotor blades, main gear box(MGB) supporting structure, cockpit, cabin and pilot seats to reduce rotor-induced 4/rev vibration. Also, dome-fairing was introduced in order to reduce the tail-shake vibration. This paper shows design technique and flight test results for vibration-reduction devices that have been incorporated into KUH.

한국형기동헬기(KUH)는 국내 최초로 개발된 헬기로서, 2010년 3월 초도 비행을 시작으로 2012년 6월 체계 개발을 성공적으로 종료하였다. 비행시험 단계에서 다양한 진동문제가 발생하였으며 이를 제어하기 위해 적절한 진동저감장치를 설계하고 적용하였다. 한국형 기동헬기의 주요 진동 성분인 $4{\Omega}$ 주파수 진동 저감을 위해 주로터 블레이드, 주기어박스 지지부, 조종실, 승객실 그리고 조종좌석에 진동저감장치를 적용하였다. 또한, 테일-쉐이크 진동 제어를 위해 돔페어링을 적용하였다. 본 논문에서는 한국형 기동헬기에 적용된 진동저감장치들의 해석 및 설계 기법과 비행시험 결과를 제시한다.

Keywords

References

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  3. Application and Performance Evaluation of Helicopter Active Vibration Control System for Surion vol.43, pp.6, 2015, https://doi.org/10.5139/JKSAS.2015.43.6.557