References
- Cohen, H., Rogers, G. F. C., and Saravanamuttoo, H. I. H., 1996, Gas Turbine Theory, Longman Group Limited, Essex.
- Bindon, J. P., 1989, "The Measurement and Formation of Tip Clearance," ASME Journal of Turbomachinery, Vol. 111, pp. 257-263. https://doi.org/10.1115/1.3262264
- Yamamoto, A., 1989, "Endwall Flow/Loss Mechansm in a Linear Turbine Cascade With Blade Tip Clearance," ASME Journal of Turbomachinery, Vol. 111, pp. 264-275. https://doi.org/10.1115/1.3262265
- Lee, S. W., Moon, H. S., and Lee, S. E., 2009, "Tip Gap Height Effects on Flow Structure and Heat/Mass Transfer over Plane Tip of a High-Turning Turbine Rotor Blade," International Journal of Heat and Fluid Flow, Vol. 30, pp. 198-210. https://doi.org/10.1016/j.ijheatfluidflow.2008.12.009
- Key, N., and Arts, T., 2006, "Comparison of Turbine Tip Leakage Flow for Flat Tip and Squealer Tip Geometries at High Speed Conditions," ASME Journal of Turbomachinery, Vol. 128, pp. 213-220. https://doi.org/10.1115/1.2162183
- Lee, S. W. and Chae, B. J., 2008, "Effects of Squealer Rim Height on Aerodynamic Losses Downstream of a High-Turning Turbine Rotor Blade," Experimental Thermal and Fluid Science, Vol. 32, pp. 1440-1447. https://doi.org/10.1016/j.expthermflusci.2008.03.004
- Lee, S. W. and Kim, S. U., 2010, "Tip Gap Height Effects on the Aerodynamic Performance of Cavity Squealer Tip in a Turbine Cascade in Comparison with Plane Tip Results-Part 1: Tip Gap Flow Structure," Experiments in Fluids, Vol. 49, pp. 1039-1051. https://doi.org/10.1007/s00348-010-0848-6
- Lee, S. W. and Choi, M. Y., 2010, "Tip Gap Height Effects on the Aerodynamic Performance of Cavity Squealer Tip in a Turbine Cascade in Comparison with Plane Tip Results-Part 2: Aerodynamic Losses," Experiments in Fluids, Vol. 49, pp. 713-723. https://doi.org/10.1007/s00348-010-0849-5
- Lee, S. E., Lee, S. W., and Kwak, H. S., 2011, "Tip Leakage Aerodynamics over Stepped Squealer Tips in a Turbine Cascade," Experimental Thermal and Fluid Science, Vol. 35, pp. 135-145. https://doi.org/10.1016/j.expthermflusci.2010.08.014
- Lee, S. W., Kim, S. U., and Kim, K. H., 2012, "Aerodynamic Performance of Winglets Covering the Tip Gap Inlet in a Turbine Cascade," International Journal of Heat and Fluid Flow, Vol. 34, pp. 36-46. https://doi.org/10.1016/j.ijheatfluidflow.2011.11.008
- 김선웅, 이상우, 2011, "터빈 동익 컷백스퀼러팁 하류에서 의 3차원 유동 및 압력손실," 유체기계저널, 제14권, 제1 호, pp. 48-54.
- Mhetras, S., Narzary, D., Gao, Z., and Han, J-C, 2008, "Effect of a Cutback Squealer and Cavity Depth on Film-Cooling Effectiveness on a Gas Turbine Blade Tip," ASME Journal of Turbomachinery, Vol. 130, pp. 021002-1-021002-13. https://doi.org/10.1115/1.2776949
- Treaster, A. L. and Yocum, A. M., 1979, "The Calibration and Application of Five-Hole probes," ISA Transactions, Vol. 18, pp. 23-34.
- Lee, S. W. and Yoon, T. J., 1999, "An Investigation of Wall-Proximity Effect Using a Typical Large-Scale Five-Hole Probe," KSME International Journal, Vol. 13, pp. 273-285.
- Abernethy, R. B., Benedict, R. B., and Dowdell, R. B., 1985, "ASME Measurement Uncertainty," ASME Journal of Fluids Engineering, Vol. 107, pp. 161-164. https://doi.org/10.1115/1.3242450