Abstract
A turbine control system which has been operated for years in a nuclear power plant was retrofitted with a newly developed digital control system. After completion of the retrofit, turbine valve tests were performed to ensure the integrity of each valve's control function. The sequence of each valve test is composed of a closing process and a reopening process. To minimize megawatt variation which normally occurs during the test sequence, we employed a kind of compensator algorithm in the new digital control system which also have been used in the old system. There were difficulties finding optimal parameter settings for our new compensator algorithm because the power plant didn't allow us to perform necessary tuning procedures while the turbine is on load operation. Therefore an alternative measure for the compensator tuning which is independent of the turbine actual operation had to be implemented. So, a process model for the test was required to overcome this situation. We analyzed the operation data of the test and implemented the process model by use of input and output variable relations. Also we verified the process model by use of another condition's operating data. The result shows that the output of model is similar to the actual operation data.