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Operating Characteristics of 0.4 MW-Scale Gas Dispersion Type FGD Absorber

0.4 MW급 가스분사식 배연탈황 흡수탑의 운전 특성

  • 안희수 (한국전력공사 전력연구원) ;
  • 김기형 (한국전력공사 전력연구원) ;
  • 박승수 (한국전력공사 전력연구원) ;
  • 박광규 (한국전력공사 전력연구원) ;
  • 김영호 (충남대학교 정밀응용화학과)
  • Published : 2008.08.31

Abstract

This study was carried out to investigate the effect of operating and design conditions of gas dispersion type of absorber on $SO_2$ removal efficiency. pH difference between upper and lower part of gas dispersing plate of absorber was 0.2, which was relatively low. This was supposed that recirculation capacity of absorbing liquid between froth zone and reaction zone of absorber be increased by oxidation air injection through liquid riser which acted as liquid pump. Test results showed that $SO_2$ removal efficiency was more sensitive than absorber ${\Delta}P$. High $SO_2$ removal even at lower pH resulted from very low concentration of $HSO_3^-$ ion in absorbing liquid because of direct supply of dissolved oxygen into froth zone. 96% of $SO_2$ removal efficiency was obtained under the condition of absorber pH 5.2, flue gas flow rate of $1,530\;Nm^3/hr$, inlet $SO_2$ concentration of 800 ppm, absorber ${\Delta}P$ of 250mmAq. The following equation by a multiple linear regression was obtained to describe the relationship between $SO_2$ removal and operating variables. $$f=1-{\exp}(-1.3939+1.060pH+0.0139{\Delta}P-0.00267G-0.000064SO_2Conc.),\;R^2=0.9719$$

Keywords

References

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