Case Study of Ground and Supporting System Failure in Soft Ground Deep Excavation

연약지반 깊은 굴착에서 지보재 및 지반 파괴 사례 연구

  • Published : 2005.03.25

Abstract

We find out many soft ground deep excavation cases where results of careless overexcavation accelerate the advance of loosening zone of adjacent ground, bucklings of struts and bottom heaves happen due to delayed supporting time. This article introduces a soft ground deep excavation case where steel pipe sheet piles were used with struts as an earth retaining system. There were 2 times of buckling in the supporting system and heaving of bottom ground due to overexcavation and insufficient penetration depth of the steel pipe sheet piles. The effort of this article aims to improve and develop the technique of design and construction in the coming projects having similar ground condition and supporting method.

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