Identification of Failure Cause for 300MW LP turbine Blade through Vibration Analysis

진동 해석을 통한 300MW급 저압터빈 블레이드의 손상 원인 규명

  • 김희수 (한국전력공사 전력연구원) ;
  • 배용채 (한국전력공사 전력연구원) ;
  • 이현 (한국전력공사 전력연구원)
  • Published : 2005.05.01

Abstract

The failure of blades frequently happened in the 300MW LP turbine until now and they are maintaining the blades periodically during outage. So the blade-disk system is analysed by FEM in order to identify the main cause of failure of blade row. It is found that the stress of root's hole is highest in comparison with other parts from the result of the steady stress analysis. Also, the two dangerous frequencies which is related to the resonance condition are found in the interference diagram. one is 1,516 Hz which is related to the operating speed. The other is 2,981 Hz which is related to the 1 nozzle passing frequency. The dynamic stress analysis is per-formed to identify more accurate root cause for failure of blade row. It is confirmed that the dynamic stress of the latter is higher than one of the former. From these results, it is concluded that the former has deeply something to do with the failure of blades more than the latter. Based on versatile investigation and deliberation, the change of blade's grouping is determined to avoid the resonance condition with the operating speed. After the blade grouping is changed, the former frequency vanish completely but the latter is still in existence in the interference diagram. Fortunately, It is confirmed that the dynamic stress of the new blade grouping is lower than one of the old blade grouping. 2 years has passed since modification and the LP turbine is operated well without failure so far.

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