An Experimental Study on the Self-excited Instabilities in Model Gas Turbine Combustor

모델 가스터빈 연소기내의 자발 불안정성에 관한 실험적 연구

  • 이민철 (한국과학기술원 기계공학과 대학원) ;
  • 홍정구 (한국과학기술원 기계공학과 대학원) ;
  • 신현동 (한국과학기술원 기계공학과)
  • Published : 2004.11.26

Abstract

Most of gas turbines is operated by the type of dry premixed combustion to reduce NOx emission and economize fuel consumption. However this type operation, combustion induced instability brought failure problems cause by high pressure and heat release fluctuations. Though there has been lots of studies since Lord Rayleigh to understand this instability mechanism and control the instabilities, none of them made matters clear. In order to understand the instability phenomena, a simple experimental study with dump combustor was conducted at the moderate pressure and ambient temperature conditions. From this model gas turbine combustor self-excited instabilities at the resonance mode(200Hz) and bulk mode(10Hz) were occurred and observed at the three points of view; pressure, heat release and equivalence ratio which are acquired by peizo-electric transducer, HICCD camera and acetone LIF respectively. From this results we could see the instability mechanism clear with the account of time scale analysis which explained by the propagation of pressure wave to the upward of mixture stream and convectional transfer of the equivalence ratio fluctuation by this pressure fluctuation.

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